Productivity Improvement of Gear Housing by Reduction of Lead Time
Productivity Improvement of Gear Housing by Reduction of Lead Time
Calculation of EOQ
Recommendations
Fig 1. Methodology
• Gear housing PQ 265 – Cavity 1,2,3,4. Picking the Casting From the bin 5
• Demand /Day - 1250(approx.)
Cleaning the fixture in first spindle 5
• Production Output/Day – 600/Machine with air
2.DATA COLLECTION
Clamping the casting in the fixture 12
2.1 Cycle Time : Cleaning the job removed from the first 5
spindle
S.no Setup Machining Production
Time Time output Unclamping the job from second 12
1 58 1.39 172 spindle
2 61 1.42 175
Cleaning the the fixture in the second 4
3 59 1.44 163 spindle with air
4 55 1.50 181
Clamping the job from the first spindle 12
5 60 1.51 177 in the second spindle
Pareto Chart of C1
Fig 4. Cause & Effect Diagram 900
100
800
Reasons for Low Productivity:
700
80
• Time taken for air gauge & height gauge 600
Percent
mins. 400
40
300
• Handling time for machining is around 55-
200
60 secs. 20
100
• The supply of castings is not standardized. 0 0
C1 NOGO Poor finish Inaccuracies in Machining Other
C2 672 85 50 20
• The main cause for high handling time is Percent 81.3 10.3 6.0 2.4
Cum % 81.3 91.5 97.6 100.0
clamping & Unclamping the job from the
chuck.
Tₐ = 480 – 50
30.88 30.96 31.04 31.12 31.20
O bserv ed Performance
PPM < LSL 0.00
Exp.
PPM
Within Performance
< LSL 28451.93
Exp. O v erall Performance
PPM < LSL 21402.15
Tₐ = 400 mins.
PPM > USL 0.00 PPM > USL 95000.05 PPM > USL 81620.44
PPM Total 0.00 PPM Total 123451.98 PPM Total 103022.59
D = 225 pieces
T = 400/675
Fig 5. Process capability
T = 0.59 mins
Improvements:
Actual Cycle time – 2.34 mins
• Setup time can be reduced by reducing the
time taken for clamping & unclamping of SWIP = Cycle time / takt time
the casting from the work fixture.
SWIP = 2.34/0.59
• A new hydraulic clamping device is
SWIP = 4
attached to the work fixture which is
operated by a button. 3.2 SAFETY STOCK CALCULATION:
• Reducing in-process inspection from 5 Month Demand
pieces to 10 pieces. June ‘14 23476
July’14 25433
August ‘14 25650
September ‘14 25864
October ’14 26247
November ‘14 21435
December ‘14 25512
January ‘15 22539
x n
Takt time is defined as the average unit production The average consumption /month = 23270
time required to meet the customer demand of a
product.
x
N
T = Tₐ/D n x
Standard deviation = dm n 1
Where, N
T = Takt time
Chart Title
The desired service level is kept as 85%
6
The lead time factor with normal distribution 5
according service level is – 1.04 4
3
Safety Stock = SS z * dm 2
1
0
SS = 1854
Clamping the job from the first 4 Fig 8. Process capability after implementation
spindle in the second spindle
2) http://www.stevepavlina.com/2007/05/33-rules-
to-boostyour-productivity, (Access on; 14/07/2012)
RESULTS & DISCUSSIONS:
3)http://www.ecoefficiency.com.au/portals/56/facts
The gear housing PQ25 component used in hets/foundry/ecofndry_process.pdf (over view of
production line of the company now has increased casting processes)(Access on; 29/07/2012)
its production. The productivity of the component 4)Vivekanand S. Gogi, Rohith D., Shashi Kiran K.,
by reducing the lead time and the safety stock is Suhail M. Shaikh, 2014, “Efficiency improvement
reduced from the current scenario. of a plant layout”, International Journal of
Innovative Research in Science, Engineering and
Technology (IJAERS), Vol. 3(4), pp. 11203-11209.
A new hydraulic clamping fixture is 5) Pramod P. Shewale, Manmath S. Shete, Prof.
introduced into the CNC machine which DR. S. M. Sane, 2012, “Improvement in plant
automatically holds the work piece. layout using systematic layout planning (SLP) for
The set up time taken for machining increased productivity”, International Journal of
operation is reduced from 60 secs to 33 Advanced Engineering Research and Studies
secs (IJAERS), Vol. 1(3), pp. 259-261.
The process capability of the process is
increased to 1.78. 6). Mayank Dev Singh, Raval Apurv J, Patel
The standard work in process inventory is Dhaval G, Parth Varmora J, 2013, “Overall
productivity improvement in casting and fastening
reduced to 4 from 25.
industry”, International Journal of Mechanical and
The safety stock to be maintained in the Production Engineering (IJMPE), Vol. 1(1), pp. 43-
process is reduced to 1854.
7). Arash Ghodrati, Norzima Zulkifli, 2013, “The
REFERENCES :
impact of 5s implementation on industrial
1)Prof. DR S.M. sane, promod p. shewale, organizations performance”, International Journal
of Business and Management Invention, Vol. 2(3),
Manmath S. shete, “Improvement in plant layout
pp. 43-49.
using systematic layoutplanning (SLP) for