Small, High-Pressure Liquid Oxygen Turbopump
Small, High-Pressure Liquid Oxygen Turbopump
Small, High-Pressure Liquid Oxygen Turbopump
R=19770020459 2020-05-22T11:42:29+00:00Z
• NASA CR-135211 _
: INTERIMREPORT -
SMALL,HIGH-PRESSURE
LIQUIDOXYGEN
TURBOPUMP
/
• A. Csomor, and R. Sutton
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A small, high-press.ire, liquid oxyge_ ¢urbopump was designed, fabricated, and tested. The pump
was of a single-stage, centrifugal type; power to the pump was supplied by a single-stage) partial-
emissfon, axial-impulse turbine. 0esign conditions included an operating speed of 70,000 ¢pm,
pump discharge pressure of 2977 N/cm 2 (4:318 psia), and a pump flovrate of 16..4 kg/s (36.21 1b/set),
The turbine was propelled by L02/LH 2 coBbustion products at 10_1 K (:1874 R) inlet temperature,
and at a design pressure ral:io of 1.424. The approaches used tn the detail analysis and design
of the ¢urbopump are described, and fabrication methods are discussed. Data obtained fro-, gas
generator tests, turbine performance calibration, an,'- turbopump testing are presented.
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FOREWORD
Summary .................. 1
Introduction ................... 2
Discussion .................... 5
Analysis and Design ............... 5 !
, ASE Engine Configuration .............. 5
Turbopump Requirements 5 '
Turbopump Configuration Selection ........... ii
Hydrodynamic Analysis of the Pump ........... 15
Turbine Aerothermodynamlc Analysis ........... 26
Axial Thrust Control ............... 40
Bearing Des_ ;n ................. 40
Seal Design ................... 54
Rotodynamlcs .................. 67
Material Selection ................ 67
Heat Transfer Analysis ............... 77
Stress Analysis ................ 84
Gas Generator .................. 104
Fabrication ................... 117
Component Fabrication ............... 117
Turbopump Assembly ................ 121
Testing ................... 137
Gas Generator Testing ............... 137
Turbine Calibration ................ 160
Turbopump Testing ................. 170
Appendix A
Design Ground Rules ............... 243
Appendix B
, Mark 48-0 Turbopump Assembly Drawing RSO09820E ........ 247
Appendix C
Mark 48-0 Turbopump Test Printouts ............ 249
Appendix D
References .................... 279
A_pendix E
Distribution List .................. 281
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ILLUSTRATIONS
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78. Mark 48-0 Volute Castings .... I19
79. Mark 48-0 Turbopump Housing Fabrication Process . . . 120
80. Mark 48-0 Inlet, Volute, Inducer, Diffuser and Rotor . 122
81. Mark 48-0 Turbine Rotor Blade Electric Discharge
Machining ...... 123
82. Mark 48-0 Rotor on the Gisholt Balancing Machine . . 124
83. Mark 48-0 Turbopump S/N 01-0 Runouts . . . 126
84. Mark 48-0 Turbopump Front Bearing Cartridge Preload . 127
• 85. Mark 48-0 Turbooump Rear Bearing Cartridge Preload 128
86. Mark 48-0 TurbopumF S/N 01-0 Pump Diametral Clearances 129
87. Mark 48-0 Turbopump S/N 01-0 Bearing Fits ...... 130
88. Mark 48-0 S/N 01-0 Seal Diametral Clearances .... 131
89. Mark 48-0 Turbopump S/N 01-0 Turbine End Clearances and
Fits . ............ 132
90. Mark 48-0 Rotor Push-Pull ....... 133
91. Mark 48-0 Turbopump Assembly ...... 135
92. Hark 48-0 Turbopump Assembly ..... 136
93. LO2 Turbopump Injector Water-Flow Test, Leakage Noted
Prior to Rebraze Cycle .......... 138
94. LH 2 Turbopump Gas Generator Injector, P/N _S005024E,
U/N 3M, Test 016-029 ........... 147
95. LO2 Turbopump Gas Generator Injector, RSJ05024E-161,
U/N 2, Test 016-031 ............ 148
96. LO2 Turbopump Gas Generator .......... 150
97. Combustion Skin Temperature No. 3 (T_3t 016-048) . . 152
98. Combustion Gas Temperature (Tes_ Olo-048) ........ 153
99. Chamber Pressure (Test 016-048) ......... 154
I00. LO 2 Turbopump Gas Generator Installation, Test 016-048 . . . 155
I01. Condition of Combustor, Posttest 016-048 ....... 156
102. LO 2 Injector Unlt 2 Performance Map ....... 159
103. Mark 48-0 Turbine Calibration Layout ........ 161
104. Mark 48-0 Turbine Calibration Assembly Runouts ..... 163
105. Mark 48-0 Turbine Calibration Build Flts (inch) ..... 164
106. Mark 48-0 Turbine Calibration Assembly ........ 165
107. Mark 48-0 Turbine Calibration Installation ...... 166
108. Mark 48-0 Turbine Calibration Installation ....... 167
109. Mark 48-0 Turbine Performance ........... 169
II0. System I, Gaseous Hydrogen Turbine Drive ...... 171
iii. System II, Gas Generator Turbine Drive ....... 172
112. Series l_Mark 48-0 Turbopump Testing ....... 173
113. Mark 48-0 Turbopump Test Installation ....... 174
114. Mark 48-0 Turbopump Test Installation ...... 175
115. Mark 48-0 Turbopump Test Installation ........ 176
116. Lima Stand Turbopump Installation ......... 177
117. Lima Stand Turbopump Installation .......... 178
118. 48-0 Turbopump Installation ............ 179
119. Typical Main Hydrogen Servo Valve Characteristics
Lima Stand - PRA ................ 188
120. Mark 48-0 Turbopump Start and Cutoff Characteristics Gas
Generator Hot-Gas Drive .............. 193
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TABLES
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SUMMARY i
The objective of this program was to establish the technology for small, high- i
= pressure liquid oxygen (LOX) pumping capability. Turbopumps in this category
are needed for applications in small, high-performance, reusable, versatile,
staged-combustlon rocket engines. To accomplish this objective, analysis and
design effort was expended to produce specifications and shop drawings in Fuffl-
cient detail to permit fabrication of test hardware.
To obtain high performance and minimize weight, the rotor speed was established at
7330 rad/s (70,000 rpm). The pump design included a slngle-stage centrifugal im-
peller preceded by an axlal-flow inducer to reduce the net positive suction head
(NPSH) requirements. Rotor axial thrust control was provided by incorporating a
self-compensatlng, double-acting balance piston as an integral part of the impeller
rear shroud. Power for the pump was developed by a slngle-stage, partlal-admlsslon
turbine using the combustion products of liquid hydrogen (LH2) and LOX as the
propellant. The rotor was supported on two ball bearings at each end. The pump
end bearings were cooled by recirculating LOX. The turbine end bearings, located
outboard of thq turbine disk to provide auxiliary power takeoff capability, were
cooled by LH 2. Controlled gap seals were used to accomplish sealing along the
rotor.
Hardware was fabricated for two complete turbopumO assemblies. To provide a hot-
gas source for the turbine, a gas generator was designed, fabricated, and tested.
The turbine was calibrated at Wyle Laboratories with gaseous nitrogen as the
driving fluid and a torquemeter was used to measure output. The turbine efficiency
was measured at 51%, 9% below the predicted value at the design point.
i The turbopump assembly was tested at Lima stand of Rocketdyne's Propulsion Research
Area (PRA). Eighteen tests were conducted on one turbopump assembly, with LOX
as the pump fluid on all but three tests. (Liquid nitrogen (LN2) was initially
used to verify integrity.) The turbine was propelled by ambient-temperature
gaseous hydrogen on seven tests, and by hot gas on the remaining tests. Speeds
in excess of the design level, up to 7765 rad/s (74,191 rpm) were explored. Pump
' discharge pressures ranging up to 3175 N/m (4604 psia) were generated with flow-
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rates up to 0.013 m3/s (193 gpm). The turbine was exposed to a maximum inlet
temperature of 1133 C (2040 F).
&nalysls of the fluid dynamic performance of the pump revealed a need for addi-
tional development effort in the following areas: the data indicated a low
suction performance either because the inducer generated insufficient head or
because of blockage at the impeller inlet. The diffuser through-flow area was
smaller than required for good diffuser performnce. Finally, the resistance
of the passages for the balance piston return ilow was too high, resulting in a
reduced balance range for the piston.
I ,
1
1
INTRODUCTION
This program was initiated to provide the required LOX turbopump technology base
for subsequent development of a high-performance, staged-combustion rocket engine.
Technology items of particular inte1_st during the course of this program included
establishing the fluid dynamic parameters and design details for a small-capacity,
high-pressure LOX pump, and low-pressure-ratio, partial-admission turbine; opera-
tion of a balance piston with no axial rubbing features; balance and operation of
a high-speed rotor; high DN bearings in LOX; hydrogen-environment embrittlement
protection; and fabrication of small components with limited accessibility for
generating internal passages. To provide a hot-gas source for the turbine, work
was also performed on hlgh-pressure, concentric-element, O2/H2 injector gas
generators.
The objectives of this program were to design, fabricate, and test a high-pressure
LOX turbopump capable of meeting the performance requirements of the 88,964 N
(20,000 pounds) thrust, staged-combustion-cycle engine, demonstrate its basic
capability, and identify any _reas where additional effort due co technology
limitations is required to place a future engine program on a solid basis.
Rocketdyne has assigned the designation "Mark 48-0 Turbopump" to the smal_ high-
pressure, liquid oxygen turbopump design generated under this contract. The two
terms will be used interchangeably throughout this report.
3
DISCUSSION
The objective of this program was to establish the technology base for small,
high-pressure, liquid oxygen pumping capability for application on the Advanced
Space Engine (ASE). The basic performance parameters for the ASE have _een es-
tablished in a preliminary design task, the results of which are reported in
Ref. i.
lhe small, high-pressure, liquid oxygen turbopump effort performed under this con-
tract was directed toward establishing the technology for the main oxygen
turbopump.
Turbopump Requirements
The performance requirements for the Mark 48-0 turbopump are listed in Table i .
The pump is required to deliver 16.4 kg/s (36.21 ib/sec) of liquid oxygen starting
with an inlet pressure of 68.9 N/cm 2 (i00 psia) provided by the low-pressure pump,
to a discharge pressure of 2977 N/cm2 (4318 psia). The propellant gas for the
turbine is a mixtu:e of free hydrogen and steam resulting from the combustion of
liquid hydrogen and liquid oxygen. The gas is provided at a temperature of 1041 K
(187':R) and an inlet pressure of 2320 N/cm 2 (3366 psia). The total gas flowrate
available is 1.34 kg/s (2.92 ib/sec). The horsepower requirement of the pump is
matched by adjusting the pressure ratio across the turbine. Since turbine pressure
ratio has a strong influence on the attainable engine combustion pressure in a
staged combustion cycle, it is to be maintained at the lowest possible level. As
noted in Table I , the mechanical operating requirements included multiple starts
with long operating durations and potentially long coast times between operations.
The values noted illTable I deviate slightly from the requirements expressed in
the original contract work statement. Refined computer runs of the engine balance
indicated minor shifts in the required pump discharge pressure, turbine inlet
temperature and pressure, and turbine hot-gas flowrate. The revised value= were
incorporated in the requirements with the NASA Project Manager's approval.
In the area of the pump, the combination of low flowrate and hlgh discharge pres-
sure imposed a difficult impeller fabrication task because of the relatively narrow
passages required compared with the outer diameter. The desire for high effici-
• en_y, eoupact packaging, end light we_ht plaeed the rotor speed into the 6282 to
9423 rad/s (60,000-to 90,000-rpu) range, pushlq bearims l_ff value to the 1.5 x
106 um rim limit noted in the Destsn Ground Rules (Appendix A). The burim8
.
6
J
Pump
Type Centrifugal
Propellant Liquid oxygen
Inlet pressure 68.9 N/cm2 I00 psia
Inlet temperature 90-95.5K t62 to 172 R
Discharge pressure 2977 N/cm2 4318 psia
Hass flo_ 16.4 kg/s 36.21 Ib/sec
Number of stages One
d
Turbine
Thermal cycle defined as enqlne start (to any thrust level) and shutdown
7
operation at high DN values in a turbopump installation as well as the dynamic
behavior of the rotor at high speeds needed to be demonstrated. Because of the
high operating speed involved, the bearings would not be able to take an appreci-
able axial thrust load. This condition dictated that an axial thrust balance
device be employed which, in liquid oxygen, would have to be of the nonrubbing
type. The operating characteristics of such a device also required evaluation.
In the turbine, the low-pressure ratio (approximately 1.4) and low arc of admis-
sion (28%) presented a combination for which no empirical data were available.
Performance predictions based on calculations needed to be validated or modified
by measured performance data.
From a structural consideration, the requirement for 300 thermal cycles was signif-
icant in that it established low-cycle-fatigue criteria and eventually necessi-
tated incorporating a liner in the turbine manifold to limit the maximum thermal
gradients in structural walls.
In addition to the performance criteria noted in Table i , the contract work state-
ment included c_.:tain ground rules relating primarily to the structural analysis
and mechanical design of the turbopump. These ground rules are enclosed in
Appendix A.
Turbo_ump Descriptio n
I
of Mark 48-0. I
7
i
Liquid oxygen is introduced to the pump through the axial-flow inlet of 4.214 cm J
(1.65_ inch) diameter and passes through a four-bladed, constant-outer-dlameter, j
tarered-hub inducer which raises the pressure to an intermediate level. From the
inducer the liquid proceeds _nto a centrifugal impeller containing four partial
and four full blades. Subsequently, it is diffused in a radial diffuser which
incorporates 13 guide vanes. Downstream of the diffuser, liquid oxygen is col-
lected, further diffused in a volute section, and delivered through a single
2.54 cm (i.00 inch) diameter duct.
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The pump shaft and the turbine disk are designed as an integral part. On the out-
board end, a stub shaft is used with a stud and nut to extend the rotor. Two
pairs of angular-contact, 20 mm ball bearings are used to support the rotor. The
pump-end bearings are cooled by recirculating liquid oxygen tl,rough them. The
outboard shaft seal is pressurized with liquid hydrogen, and the leakage toward _
the outboard side is used as bearing coolant. A small amount of liquid hydrogen
is bypassed around the seal and introduced to the bearing directly as a redundant
source of coolant. The bearings in each pair are axially preloaded against each
other with Belville springs to prevent ball skidding. The turbine-end bearings _,
are free of other axial loads. The outer-race sleeve of the pump-end bearings is
axially retained so that the bearings absorb rotor axial thrust during transient
periods when the balance piston does not control the rotor axial position.
Under conditions other than early transient stage during startup or at the end of
shutdown, the rotor axial thrust is neutralized by a self-compensating balance
piston• The rotating member of the piston is the rear shroud of the impeller.
To operate the piston, high-pressure liquid oxygen from the impeller discharge
passes through a high-pressure orifice located at the outer diameter of the im-
peller into the balance cavity. From the cavity, the liquid passes through a low-
pressure orifice near the impeller hub into the sump. From there the liquid oxy-
gen is returned to the eye of the impeller through axial passages in the diffuser
vanes and radial holes in the diffuser and inlet. Thrust-compensating effect is
achieved by virtue of the fact that the high- and low-pressure orifice openings
vary with the axial position of the rotor, and the pressure force on the rear
shroud of the impeller varies correspondingly; e.g., an unbalanced load toward
the pump inlet causes a reduction in the high-pressure orifice gap and an increase
in the low-pressure orifice gap. This, in turn, causes a reduction in the pressure
force of the impeller rear shroud, introducing a compensating load change•
Because of the danger of explosion when rubbing in liquid oxygen, the balance
piston orifices were designed as noncontacting type, formed by the axial proximity
of close clearance, 0.038 mm (0.0015-inc_average, diametral, cylindrical surfaces.
To preclude mixing liquid oxygen from the pump with the uombustion products from
the turbine, the two regions are separated by three dynamic seals. All three
seals are of the controlled-gap type, with two seal rings in each. The controlled-
gsp concept was selected for this application primarily because Jt has low drag
• torque, a "must" for idle-mode starts. This concept also minimizes power absorp-
tion during steady-state operation, and permit_ very long service life. Pump fluid
is contained by the primary LOX seal. The oxygen _lich flows past this seal is
drained overboard from the cavity formed by the primary and intermediate seals.
A slinger containing pumping ribs was included upstream of the primary LOX seal
to reduce the pressure at the seal gap to a level that will vaporize the fluid•
The objective was to reduce the mass flowrate through the seal with this technique.
On the turbine side, because of the high pressure involved, sealing and drainage
was accomplished in two steps. An overboard drain was included downstream of the
first ring, which reduces the pressure between the two rings to 79 N/cm 2 (115 psia). '
, The small amount of turbine gas which leaks past the second ring is drained over-
board with a drain cavity pressure of approximately 14 N/cm (20 psia).
i
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To provide separation of the pump and turbine fluids, an intermediate seal was
incorporated between the two drain areas with a GHe purge which maintains the
cavity between the two rings at 35 N/cm 2 (50 psia).
Within the above-specified limits, the most important options which had to be Con-
sidered were those relating to the type of axial thrust control concept and type
of impeller and diffuser to be used, and whether an inducer was necessary at the
pump inlet. Each of these features was studied with respect to advantages and
disadvantages, and the conclusions are discussed below. A summary is enclosed
in Fig. 3 .
Impeller With or Without Inducer. The higher the pump speed that can be selected,
the higher the obtainable performance and the smaller the pump envelope and weight _
will be. Therefore, the speed was selected based on the given bearing DN value
(
limitation as well as axial thrust control considerations, which limit the mini-
mum impeller diameter that can be used to achieve thrust balance. If we assume
a speed of 7853 rad/s (75,000 rpm), which corresponds to a DN value of 1.5 x 106
for a 20 mmbearing a pump suction specific speed of 24,000 would be required
(available NPSH 170 feet). This suction specific speed, however, can be obtained
only by using an inducer. It is for this reason that the inducer-impeller
combination was selected.
i! Axial Thrust Controlp Integral versus Separate Balance Piston. The advantage of
the separate balance piston is that its size can be selected such that any axial
thrust condition can be controlled. The disadvantages, however, outweigh this
advantage: pump length and weight increase, and pump performance decreases since
balance piston leakage losses and disk friction increase. Using an integral
impeller-balance piston system reverses the advantages and disadvantages of the
separate pistons: Weight, length, and performance losses are minimized; however,
thc thrust balancing range is limited, being a function of the impeller size.
11
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To ensure that sufficient thrust control could be achleved with the integral sys-
tem, a parametric trade study was made. The results of this study, summarized in
. Fig. 4 , showed that axial thrust control could be achieved if the impeller diam-
eter was maintained above 5.8 cm (2.3 inch). Based on this, the integral impeller
balance system was selected.
Vaneless or Vaned Diffuser. This option was considered only because a vaneless
diffuser is easier to manufacture. The pump efficiency, however, increases when
a vaned diffuser is used. A vaned diffuser reduces the velocity in a short length,
the flow path length is reduced and, therefore, the friction losses. (For ex- *
perimental results see Ref. 2 , page 17, Fig. 6). A second advantage of the i_
vaned diffuser is that the pressure around the periphery of the impeller is more
uniform, resulting in reduced radial loads. For these reasons, the vaned diffuser
configuration was selected.
13
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Pump Speed Selectiu,,, the speed selection involved a cor_p:,,se between several
considerations. It iacluded a design study, critical spe_ _ malyses as a function
of bearing stiffness a×lal thrust control calculations. ,: bearing DN value, and
the effect of speed on pu_p performance. From the des'/ .....
_dy and critical speed
analyses, the use of c 20 am bearing resulted which, _r ,:'n, fixed the maximum .:
speed at 7850 rad/s (75,6:)0 rpm) based on the 1.5 ". ::'',_ limit imposed In the
Design N/ram
35,000 Ground(2Rulesblo
x (see Appendix A). the
Ib/in.)/bea_ipg, At se,:om_
an esr i,
....::
' al_earlng stiffness
is located of rad/s
at 5550
(53,000 rpm); meanwhile, the third is !ocated at _, :00 rad/s (i00,000 rpm). Thus,
from the standpoint of critical rotor freq_enc_,_ , the speed range of 6912 rad/s
(66,000 rpm) to 8376 rad/s (80,000 rpm) was ac_,_able after a 20% allowance was ' ,,,.,
i made for margin. Another criterion to be consl!ered was the axial thrust control.
• With a selected impeller head coefficient of 0.4? (see Impeller Design) an impel-
! ler diameter of 6.0_ cm (2.38 inches) would result In a speed of 7850 rad/s (75,000
rpm). This diameter was only slightly larger than the 5.84 cm (2.3 inches) impel-
ler diameter thrust capability limit established by the parametric study (Fig. 4 ).
To ensure that enough axial thrust capability margin was incorporated, the impeller
diameter was established at 6.48 cm (2.55 inches), resulting in an operating speed
of 7330 rad/s (70,000 rpm).
Inducer Inlet Flow Coefficient. The available nominal inlet pressure to the pump
is presently established at 68.94 N/cm 2 (i00 psi). Initially in the program, thls
value was 52.91 N/cm 2 (76.75 psla) minimum, and the presented inducer analysis was _
based on the latter pressure level. The NPSH available at the inducer inlet at {
52.91 N/cm 2 (76.75 psi) inlet pressure and 95.5 K (172 R) inlet temperature is
320 J/kg (107 feet) which corresponds to a suction specific speed of 111.5 rpm
<m3/s)172(j/kg)3/4 L31,867 rpm (gpm) I/2 (ft)3/4]at 7320 rad/s(70,000 rpm). To obtain
the maximum margin on suction performance, particularly In vlew of the degradation
of obtainable suction specific speed due to the small-slza inducer, an Inlet flow
i coefficient _ = 0.085 was selected. Wlth this flow coefficient, larger-slze in-
i ducers h_ve the potential of reaching a corrected suction specific tpeed of 192.5
, rpm (m3/s)l/2/(J/kg)3/4 [55,000 rpm (gpm) I/2 (ft)3/4, see Fig. 4, page 12 of NASA
i Report SP8109]. A second consideration In selecting 0.085 as the flow coefficient
'I was the limitation imposed by the inducer blade angle. With inducer tlp and hub
diameters of 4.19 cm (1.65 inches) and 1.78 cm (0.7 inch), respectively, the inlet
blade angle of the tip becomes 0.15 tad (8.5 degrees). A lower flow coefficient,
which theoretically yields higher suction specific speeds and therefore a larger
design margin, would r_quire even smaller blade a,_gles. To provide sufficient
flow passage area, the inducer tlp diameter would have to be increased and the
blades made thinner. As a consequence, the blades would be higher stressed, and
f_brlcatlon would become more difficult. Furthermore, the diameter ratio of the
impeller would be unfavorably affected and, as a resulr, the pump efficiency would
drop. Therefore, the selected flow coefficient c¢ 0.085 represents the lower limit
and, hence, the optimum choice for this application.
Inducer Inlet: Blade Anl_.es. _he blade centerllne was canted forward 0.16 rad
(9 degrees) from the radial direction to counteract the hydraulic loads oy cen-
trlfuga] forces. A 2.09 tad (120 degrees) sweep was used to ease the blade stress
conditions.
15
As noted above, the blade anFle at the inlet tip was estab1_shed at 0.15 rad (8.5
degrees) in conjunction with the selection of the flow coefficient and tip diameter, i
Angles at other radii were determined by the relationship
r tan B
cos (n.16 rad)= constant
where
r = radius
The resulting blade angle at the hub is 0.339 rad (19.4 degrees).
Inducer Discharge Blade Angles. The inducer discharge blade angles were dotermined
by the _mpeller suction capability, which was selected as Ss = 2.569 rad/s
(m3/s)i/2/(J/kg) 3/4 (7000 rpm (gpm)i/2 (ft)3/4). Since the impeller front wear-
ring flow as well as the balance piston flow is returned to the inlet of the
impeller, downstream of the inducer, the following impeller flow was used:
ib/sec
The value of the balance piston flow used in the impeller analysis was derived
from a preltmlnary analysis. It is larger than the flow which results when the
final tolerances are used. (See Axial Thrust Analysis section of this report)
Based on this impeller flowrate and Ss, the required impeller inlet NPSH is 2690
J/kg (900 feet). Assuming an available inducer inlet head of 52.9 N/cm (76.75
palm) results in a minimum inducer required headrlse of 2346 J/kg (785 feet).
The inducer discharge angles were de_ermlned by using a head rise requlrement of
301 f/kg (900 feet). This was done to account for the size effect. The discharge
blade angles from hub to tip are determined by the relation
r tan B = conqtant
Thio does not produc_ an ideal constant head output from hub to tip, but eases
the fabrication considerably. First the angle at inducer discharge rms is
calculated:
= g
(4.192 - 2.292 ) ffi 9.67 cm2 (Sl)
where DT and DH are the inducer tip and discharge hub diameters, respectively.
If the blockage is assumed to be 0.8,
= q
Cm (A) (0.8)
(229) (144)
= 61.2 ft/sec (English)
- (449) (1.5) (0.8)
Cm 2
ffi
arc tan
2 rms u - c
rms u2
l-ms
18.6
= arc tan 124 - 27.1 ffi 0.19 radian (Sl)
The total turning at the rms radius is 0.107 radian (6.16 degrees). Assuming
r
a deviation angle of 0.044 tad (2.5 degrees) results in a blade discharge angle
i i-
| 17 i
Figure 5 shows the blade angle distribution as a function of the axial length,
and Fig. 6, the blade loading, which was calculated using Rocketdyne's VELDIS
computer program.
Impeller Design. With the inducer design established, the inlet eye diameter of I,
the impeller is alsc fixed (4.19 cm; 1.65 inches). The required pump head rise is _
25,974 J/kg (8690 feet) which, at 7330 rad/s (70,000 rpm), corresponds to a stage _"
specific speed of 4.1 rpm (m3/s)i/2/(J/kg)3/4 (1174 rpm (gpm)i/2/(ft)3/4). From
this, using the available experience documented in Fig. 5 of NASA Report SP 8109,
dn impeller diameter ratio of about 0.65 has to be selected to obtain a high pump
efflclency. Therefore, the impeller tip diameter is set to 6.48 cm (2.55 inches)
whict, with the selected speed of 7330 rad/s (70,000 rpm), results in a required
head coefficient of _ - 0.4725. From Fig 16 of NASA Report SP 8109, the minimum num-
ber of blades required to obtain _ = 0.4725 is found to be between five and six,
Since a four-bladed inducer has been selected, it is desirable to also have four
blades at the impeller inlet. This will ensure minimum impeller inlet blockage
and, at the same time, ease producibility. However, an impeller with only four
full blades results in blade surface velocity gradients exceeding the limits.
Therefore, four partial blades were added.
The final determination of the blade angles and shape is a function of blade load-
ing, stress, and producibility, all of which are also affected by the shroud con-
tour. Its curvature, therefore, was made moderate to avoid separation. The shroud
shape also has to be coordinated with the blade thickness required by stress.
The tip width was established as 3.81 ,_0 (0.15 inch) which corresponds to an impel-
ler discEarge flow coefficient of _ = 0.151.
For the design point, the incidence losses are assumed to be zero.
I ,,I I I o_
I I I L I I I
! 19
,: j
, , I .... " ............ T i
+
/
The loss values for the pump design point performance calculation are shown in 1
Table 2 . These values are selected based on Rocketdyne's experience. For the 4
calculation of off-design performance, the loss coefficients were varied.
+
Vaneless
Inducer Impeller Space Diffuser Volute
The blade angle distribution is shown in Fig. 7, and the results of the blade
loading analysis, calculated using Rocketdyne's two-dimensional axisymmetric
blade-loadin_ analysis computer program, are shown in Fig. 8 and 9. Figure i0
shows the predicted pump performance map, which is calculated using Rocketdyne's
loss isolation compuuer program.
Vaned Diffuser Design. The impeller is followed by a radial vaned diffuser, This
type is selected to provide maximum efficiency and, with proper volute design, a
more nearly constant static pressure around the periphery of the impeller, thus
minimizing radial bearing loads.
The radial clearance between the impeller discharge and diffuser inlet is set at
0.i inch, which corresponds to approximately 4% of the impeller diameter. Thus,
the diffuser inlet diameter is 2.75 inches. The diffuser exit diameter is set at
3.65 inches, or 1.43 times the impeller diameter. The diffusion is produced by
13 vanes. Hydrodynamic loads are insignificant compared to the tensile load.
The cross-sectional area, therefore, must be selected to carry this load. Rocket-
dyne's diffuser computer program was used to determine the vane shape (Fig. ii).
Volute. The diffuser discharges into a volute folded over toward the pump inlet.
This type is used to minimize the outside diameter and to create a stable second-
ary flow pattern, which reduces volute losses.
21
I • , , I I [ '+ ..........
i......
23
1 ,i
/
i
.t
/
].2,000 / / _'_
u. 10_
_ I / / ._ so.ooo
20OO
30,000
I I _J I I
0 00 5 10 15 20 2.5
OIFFUStil ¢R_CROE
25
! 1 I ! I t [
The volute area distribution and location of each area wlth respect to the tongue
is calculated as a function of wrap angle, 8.
360 x CUln"
0 = rln" bd__/r
W 0.144 r
The total wra R angle Is 6.28 radlans (360 degrees) and Q, the f]owrate, Is ex-
pressed In fta/sec. The coefficient makes allowance for blockage to boundary layer
buildup. Figure 12 shows the resulting area di_rlbutlon as a function of the
wrap angle.
The design analysis was conducted utilizing Rocketdyne's turbine design computer
programs'whlch have been developed and verified wlth rocket engine turbine opera-
tional data and experimental turbine test data. The gas path element wa_l friction
and turbulence losses were established from the expansion and kinetic energy
coefficients, which are a function of the blade deflection angles and blade size.
The program establishes gas path energy distribution and exit energy losses, and
adjusts the turbine diagram efficiency. Table 3 presents a summary of the turbine
design data, including the design requirements. Table 4 is a st,mmary of the
energy balance for the turbine design, and Table 5 presents the turbine blade
path summary.
The turbine manifold was designed to minimize the inlet flange velocity head
energy loss. Inlet flange velocity head energy is a significant part of the
available energy i,, a low-pressure-ratio turbine. The manifold torus was sized
to maintain the inlet flange velocity constant over the single arc of admission.
The nozzle inlet was designed for minimum incidence within the structural
constraints.
i
J 26
I t t I l t |
1
t
3.0 --
0.40 -
2.0
_sU _ 0.30
_o.,o
_l.o _ _ .-.-
I
1 o. to
l
I t
i
- o
_o
I
60
I
IOO
I
t4o
I
180
DEGREES
L
zzo
I
260
I
300
I
3_0
I I __..__.1 I I I I I
I 2 3 4 5 6
WRAPANGLE, RADIANS
I
i Turbine Available Energy (Total to Static _hlt-S) 0.813
J/kg x
I I (gJ&hw/2_Um2)
+1
|
1 27
I
1
, ,+ , j I I I ; I
OPTI HUM DIAHETER
•-.t-w
_'-.J O,0"600596
< -- _7 INCHES)
,c
0 [ -
_" O. 592 -
Z
'_ 0.588-
LI_ I,
Z
N
g
0.._4 -
0.580 I I . I I i I
4.2 4.4 4.6 4.8 5.0 5.2 5.4 1.6
TURBINE MEAN DIAMETER, INCHES
i I I I,_.
II 12 13 14
TURBINE HEAN DI/_iETER, r.m
Energy Available
kJ/kg Btu/Ibm Energy,
Additional Losses
Tip Clearance Loss 17.4 7.5 2.1
i
! Partial-Admission Losses
_ Rotor Windage, Inactive Arc 44._ 19,1 5.6
Jet expansion Loss in Rotor 4.2 1.8 0.5
End of S_ctor Pumping Loss 15.8 6.8 1.9
Turbine Specific _rk 485.1 m 208.6 59.8
Turbint Available Energy 811.3 348.9 I00.O
- 28
J' I
--_..............
] _ i, - ...... I, Ii ---"..... I! ...... I L '
{
TABLE 5. MARK 48 LO 2 TURBINE BLADE PA?_[ SUMMARY |.
(METRIC UNITS)
J
TUR,BINE GAS PATH
¢/////]/1/
/111177"7",,
% \
Star,on i _
29
":_
• l "_t-....T............. ' '
Jr _
/"
TABLE 5. (Concluded) !
(ENGLISH UNITS)
NOZZLE ROTOR
1 - 2 -- 3
STATION I 1
Vorsepower, hp 856 E T
The rotor blade inlet angle was set for zero incidence. The rotor outlet angle
of 25 degrees was selected for high work output and low leaving loss. For the
selected rotor axial width of 0.76 cm (0.300 inch), the rotor kenitic energy
coefficient was 0.589 pe_ Ref. 4 . Rotor outlet kinetic energy is represented
by W 2 in F_g.14 and 15. The rotor leaving loss velocity is represented by C2 of
291 m/s (955 ft/sec). Rotor kinetic energy loss was 0.123 x 106 J/kg (57.8 Btu/ib).
The vector diagram specific work shown in Fig. 14 and 15 was 0.567 x 106 J/_g
(244 Btu/Ib) for the flow through the nozzle and rotor passages. Additional losses
exterior to the flow passages reduce the turbine work output. These additional
losses, summarized in Table 4, include tip clearance losses and partial-admission
losses.
Tip clearance loss was determined using the empirically established efficiency
ratio data reported by Cordes in Ref. 5 for an unshrouded impulse turbine as a
function of tip clearance/blade height ratio. The radial tip clearance established
by mechnaical design considerations was 0.127 mm (0.005 inch) which resulted in
clearance/blade height ratio of 0.0175. Tip clearance losses are significant for
unshrouded, high-turning "-otating blades. Any increase in operating tip clearance
will result in significant efficiency degradation.
The summation of the gas path losses, tip clearance losses, and partial_admlssLon
losses resulted in a turbine output specific work of 0.485 x lO 6 J/kg (_08.6 Btu/ib
as listed in Table 4.
Nozzle Vane Profile. The nozzle profile was designed to accelerate a,ld direct the
turbine flow correctly to achieve design performance. The low-turning, radially
convergent design was selected for use with the tang_ntlal inlet, constant-
velocity, low-pressure-loss, turbine inlet manifold. The 0.79 radian (45 degree)
nozzle inlet angle was selected as a structural and performance compromise.
:i
_l+'+ _
FLOWPASSAGESPE(,IF IC WORK
-U AC
m u
"" Figure 14. Turbine Gas Path Calculation Velocity Vector Diagram (Netric Unite)
C
_4006 f,..
: Um - 1435 _"
FLOWPASSAGESPECIFIC WORK
mm Um A Co- I
gJ
lib
Um +(C1 cos " CSl4.
-
W2 cos {_'2" Urn)
gJ
1435 (4006 cos 16° + 2038 cos 2:)° - 1435)
" ..... 3l.i7 X 778.2 ....
= 22.4 Btu/lbm
i Flgure 15. Turbine Gu Path Calculation Veleclty Vector Olagram (P-n811sh Units)
The nozzle outlet throat area w_s determined from the gas path calculation throat '_
flow area and the passage fillet area. The gas path flow area includes the effects
of the nonideal gas characteristics and compressibility for the high-pressure
hydrogen/oxygen combustion products. _
The nozzle profile Is shown in the turbopump housing drawing in Fig. 16. The
profile has a straight back suction surface from the throat to the trailing edge.
The trailing edge has a 0.195 mm (0.0075 inch) radius to minimize nozzle wake
intensity. The straight back suction surface angle was set at 0.25 radian (15
degrees). The pressure and suction surfaces upstream of the throat are defined
by circular arcs. The profile section is adequate to carry the structural loads
resulting from the high pressure in the torus. The nozzle inlet was sized to
accept the manifold torus velocity with minimum losses and blockage.
The profile surface velocity distribution was calculated for the pitch diameter
section assuming constant blade height using the Douglas-Neumann analysis program •
reported in Ref. 7. The suction and pressure surface velocity distribution are
shown in Fig. 17. The velocity distribution showns gradual acceleration, with
maximum overspeed of I.I of the exit velocity. The analysis ,confirms the fluid
turning required of the flow passage. The actual Inlet/outlet velocity ratio
would be lower than indicated because thenozzle inlet height is larger than
assumed.
Rotor Blade Profile. Maximum axial width was used for low weight, consistent
with mlnimummanufacturable throat opening• Blade spacing was set to give a
prime blade number for an aerodynamic loading coefficient (Zwelfel number) con-
sistent with previous rocket engine turbine practice.
Rotor blade throat area was determined from the required gas path throat flow area
ratioed by the actual arc of admission to equivalent full-admission flow area plus
the rotor root fillet area. Throat opening at the mean diameter was determined
from the rotor total throat area divided by the number of blades and the blade
height.
The rotor blade profile at the mean diameter is shown in Fig. 18. The profile
was designed in accordance with Rocketdyne's established practice for this type _
of Inpulse bLding. This procedure calls for zero incidence angle according to
the gas path calculation and a slightly convergent passage to provide a smooth
velocity pattern. The velocity distribution for the rotor blade is presented in
Fig. 19 .
The rotor blade height overlaps the nozzle outlet height by 1.143 mm (0.045 inch)
• or 19%, ,_sindicated in Table 5. Nozzle/rot:or blade axial spacing was set at i
3.175 mm (0.125 inch) to minimize nozzle wake effects at the rotor inlet. Rotor
33
i
/ _._J.S 1=,14
1I
I I I I I I I
Y (ARC LENGTH)
I K (AXIAL LENGTH)
36
i I
o.
/
The predicted turbine flow parameter characteristics are shown in Fig. 21 The
flow parameter as defined in Fig. 21 is a function of turbine pressure ratio and
rotational speed over the square root of inlet temperature ratio. The _low para- ,,,
meter characteristics were determined from an Iteratlve computer calculation
matching flow element areas with turbine operating conditions.
#
n
It should be noted that Fig. 21 is constructed for gaseous hydrogen as the working
fluid; however, it can be used also for LO2/LH 2 combustion products by applying
proper corrections for fluid properties.
0.7r
0.6
; U/Co - MEANVELOCITYRATIO
!
k i
38 i,_
Ptl - TURBINE TOTAL INLET PRESSURE
tI t2 J
""-" 1.80 /
i 3.4
1.4o
_! z" 3.2
3.0
; _ 28'
2.6L
0 10o 200 3oo _oo 5o0
I I I I
0 50 IO0
39
,, _ ,; , w#, _ , ii ..'._mllmll M r_
y I
I I ! I I |
f
The configuration finally selected is shown in Fig. 22. The forces actillg on tur- 1
blne, impeller, and slinger are calculated for nominal design conditions using
the pump map shown in Fig. 23. For the forces acting on the slinger, it is
assumed that vapor is generated on the slotted slinger side.
The total balance piston travel is set to 2.54 mm (0.010 inch). Both the high-
and low-pressure orifices are of the nonrubbing type. The diametral orifice
clearance is set to 0.066 and 0.0178 mm (0.0026 and 0.0007 inch), respectively.
Figure 24 shows the pressure behind the impeller and slinger as they are
affected by the different balance piston positions. In Fig. 25 the net balance
piston restoring force is shown as a function of the balance plston travel.
The Mark 48-0 bearings are 20 mm bore, angular-contact ball bearings arranged in
two spring-preloGd pairs. The forward pair is located immediately behind the
pump impeller and is cooled by LOX. The aft pair is located on the downstream
side of the tuzSine disc and is cooled by LH 2.
The Mark 48-0 bearings are identical to those designed earlier for the Mark 48-F
turbopump. Dual use o@ the same bearing is technically feasible because the
design speed of the fuel pump is higher, 9948 rad/s (95,000 rpm) than that of
the LOX pump, 7330 rad/s (70,000 rpm). Economy in procurement was also effected
by purchasing only one type of specially designed bearing.
The internal geometry of the bearing was optimized for 9948 rad/s (95,000 rpm)
and formalized into the Rocketdyne Soulce Control Drawing, RESII74 (Fig. 26).
There was no existing bearing with satisfactory features, so a special bearing
was designed and fabricated with the following features:
The pitch diameter and outer race outer diameter were made different
than those existing for a standard metric envelope to accommodate, at
minimum size, =he thicker inner race cross section required to
it
40 1_
'
_--_ i.... ,- _ i I b, i i • 1
DIFFUSER F HIGH-PRESSURE ORIFICE
t
!
BALANCE PISTOH
CAVITY
ESSURE
IHPELLER ORIFICE
t
BALANCE PISTON
SUHP
61
t * '
t I
I' [ I ' b
, t l I
43
; '_ t E'
....... I...I........... ,..-_............... : ...I.............. I ............
........
•
1
'.
.........
,...... l .._,._,....b..l
:'::_.
.............................
• : .... ,
. ::'"."
..
.........
.
1
...................
.:" "": :'::
1.........
:t:."
,.........
I " "i'"""I " ' " '
"" .:."
I.....I..:-:-,
"'..:"',
..
""|':::
:
:;::1::':,":':.
".. :
•
,
;...
. ,
"
m
. |
N/cm 2
1_ PSIO
-CONSTANT)
t
"" L._..-L;
3 :: !_ i:
I: -' ::2
:" : .T:-
F _": :_?"
_" _..;'!')_"
=_ _ 1ii! ....
,. , ._i_ii_
. ?_
K
o g t)_t_
0 0.002 O. 001t 0.006 0.008 0.010 INCH
44
i
i
I
!
14
)
10" ,.2
UJ
0 ;0 0
0 0.002 0.004 0.006 0.008 0.010
INCH
'
o '
0.06 o_,.... o._s ' o.2
' -'_o.E
mm
45
L..-.
.... CHARACTERISTIC :'rENG-I.iSN uNITs sI UNITS
ENVELQPE DIMS.- o
+oOOOl_
BORE .787Z5 -,,,<,_tZoo
D°A. 20 mm
OUTER DIA. 39 an
WIDTH (_NDIVIDUAL RINGS) _.
fi.3,54
.3937 :'._
+ DO_ I0 am
(ACROSS BEARING) o,.,393"..ooz 10 m
INTERNAL _EQMETRY-
PITCH DIA. 1,175 DIA. (REE) 29.8 mm
RACE RADII (OUTER RACE) 52_0F" BALL DIA. (REF,)
(INNER RACE) 9,,_OF BALL DIA. (REF.)
DIAMETRAL CLEARANCE (UNFITTED) .0020 TO .0025 IN. O.051 TO 0.058 mm
(OPERATING) °OOII TO .0OI4 IN, (REF.) 0.028 TO 0.036 m_
,,(i
I
iiIIOll _ IB 4b
46
.051 TO 0,058 mm
.O28 TO 0.036 mm
4.76 mm
.51 TO 0.64 mm
,08 TO 0.22 mm
3.96 mm V/_"....
I
3. Race Radii. The race radii, which are expressed as curvature (percent
of ball diameter), were selected to obtain maximum fatigue llfe consis-
tent with practical manufacturing limitations• The outer race conforms
closely to the ball surface with a 52% curvature. Lower curvatures
closer conformity) is avoided because excessive nonrolling action will
occur in the ball-race contact. In addition, contact angle will vary
rapidly for small changes in bearing internal clearance due to manu-
facturing tolerances, press fits, and thermal expansion.
The bearing fatigue llfe is maximized if the lives of the inner and
outer races are equal. Therefore, the inner race curvature of 53%
was selected to balance the race lives. Use of a higher (less conform-
ing) curvature on the inner race is a reversal of commercial practice
for low-speed bearings. It was done here to maintain reasonable llfe,
contact angle, and clearance for the overall bearing while maximizing
the fagltue llfe of the outer race, which is adversely affected by ball
centrifugal forces at high speeds.
4. Race Shoulder Heights. The race shoulders were made deep enough to con-
tain the ball contact "prints" at the contact stress-llmlted axial load.
This configuration takes full advantage of the bearing's potential capa-
city and at the same time does not excessively restrict the coolant flow
area.
5. Cage Dimensions. The cage is outer land guided, so its outer diameter
is dictated by the outer race inner diameter (dependent on bearing pitch
diameter, ball diameter, and shoulder, helght) and adequate minimum
clearance. Cage diametral clearance, 0.076 mm (0.003 inc_ minimum at
ambient temperature, is based on experience with larger cryogenic bear-
ings and scaled to bearing size. The cage inner diameter was selected
to maximize coolant flow area and to ensure that the ball equators
would meet the cylindrical section of the ball pockets with a minimum
of 0.254 mm (0.010 inch) margin. The ball is then prevented from "plow-
ing under" the cage. The resulting diametral clearance between the cage
inner diameter and the inner race outer diameter is 1.778 _n (0.070 inch)
to 1.930 mm (0.076 inch), resulting in a minimum coolant flow area of
86.6 mm2 (0.134 in.2). The cage axial cross-sectlonal area is 170 mm2
(263 In,2). To provide adequate cage wear-llfe and strength, the cage
web thickness between the ball pockets was held to 3.81 mm (0.150 inch)
47
{
The cage ball pocket clearance was made large, 0.51 to 0.64 mm (0.025
inch) to permit ball position adjustments during operation without
excessive cage forces. Adequate pocket clearance has been found to
greatly reduce the amount of heat generated at the cage where radial
loads or misalignments occur.
iiI; 48
4
J
I00
19mm BORE
E = 1.136
_ I0
I
I0 i00 5O0
AXIAL LOAD, POUNDS
I , , I
IO0 IO00
AXIAL LOAD, N
49
i000 _
d - 0.1975 INCH
n - I0DESIGN:
I BEARING
- E = 1.175
= 20 DE£ EFS
- _0
T - 0.52
0
t. - 0.53
I
SPEED= 95,000 RPM
o RADIAL LOAD = 5 POUNDS
{ "-"
o
m
FATIGUE LIFE
tOO 97 HOURS
REQUIRED PRELOAD
97 POUNDS
AXIAL LOAD, N
I00
I0
I0 100 1000
AXIAL LOAD, POUNDS
I I I
100 500 I000
AXIAL LOAD, N
*' 52
-0.02 -- -o.om[ I I I i I I I
o IO0 200 3oo 400 500 600 700 800
POUNDS
L I I i +
o I 2 )
NX tO) _.
AXIAL LOAD
Figure 31. Hark 68-F Bearing Axial Deflection Versus Axlal Load
+
_ 53 i
t
|
2. Compensation for the increased loading by speed effects,
therefore avoiding unnecessary increase in axial load with
attendant reduction in life.
Seal Design
Main Shaft Seal System. The oxidizer seal system is designed to contain the
high-pressure LOX and turbine hot gas and maintain safe separation of the oxi-
dizer and fuel-rich, hot-gas drain cavities. The seal system (Fig. 32 ) consists
of a rotating slinger containing pumping ribs upstream of the primary LOX seal
to reduce the pressure from 1637 to 79 N/cm2 (2375 to 115 psia). The LOX is
vaporized in the slinger pumping region to reduce the seal leakage. The LOX seal
leakage is drained overboard from the cavity formed by the primary and inter-
mediate seals.
The intermediate seal is purged with gaseous helium at 35 N/cm 2 (50 psia) to
maintain a pressure barrier between the oxidizer aiLd hot-gas drain cavities for
safe separation of the combustible fluids. Approximately one-half of the purge
gas leaks out through each side of the intermediate seal and mixes with the seal
leakage for overboard drainage.
The high-pre_sure 1631 N/cm 2 (2365 psia) turbine hot gas is contained with a
double seal and a two-stage drain system. The primary turbine seal and over-
board drain reduces the pressure to 41 N/cm 2 (60 psia). The secondary turbine
seal further zeduces the pressure to Ii N/cm 2 (16 psia) in the drain cavity
formed by the intermediate and turbine seals.
The system allows failure of one seal at a time without the hot-gas pressure _x-
ceeding the intermediate seal purge pressure. The seal drains are sized to
acco,,roda_e the additional leakage of a failed seal without exceeding safe pres-
sure levels. Table 6 presents a summ_ry of the seal leakages and pressures for
nominal and failed conditicns.
A bypass vent hole is provided in the seal housing to ensure sufficient bearing
coolant flow in the event of low seal leakage.
The three-element seal and purge system provides fail-safe operation in the event
of one seal failure at a time. A summary of the leakages and pressures for
nominal and failed conditions is given in Table 7.
54
) 1 I I _....t i l !
55
...... i
J I I :,JL I _ I •
60
1977020459-073
Detail Deslsn. All of the sealing elements utilize a floatlng-ring, controlled-
gap seal ring. The floating-ring element consists of an inner carbon or AmCerMet
rlng for wear resistance, and an outer Inconei X-750 rlng for strength and ther-
mal expansion/contraction control. The outer ring material is selected to pro-
vide the same thermal expansion and contraction rate as the shaft material, so C
that a constant clearance gap is maintained as the temperature changes. The
outer rlng is sufficiently strong, relative to the inner ring, to control the
diameter of the composite ring. The inner ring is maintained in compressive
hoop stress with an interference fit.
L RI NG
"ARBON
RING
l _, _ 1
PRESSURE LOAD
The axial force induced by differential pressure (Fig. 34 ) loads the floating
rlng against the stationary housing to provide a static seal. A wave spring is
provided to ensure sufflclent contact load to maintain a static seal. The seal
rlng is partially pr_.ssure balanced by relieving the axial contact surface
and minimizing the houslng-to-shaft clearance to reduce the unbalanced axial-
pressure-lnduced load. The floating-rlng element is restrained from rotation
wlth two antlrotation tangs that engage slots In the housing.
61
/
The seal ring clearance gap was established by first performing a thermal analy-
sis to determine the temperature gradient in the turbopump shaft seal area. The
shaft temperature distribution is shown on Fig. 43 (page 78) for the main shaft
seals and on Fig. 47 (page 83) for the turbine bearing seal.
The seal ring design was optimized by utilizing a computer program in which the
temperature, pressure, m_terials, and overall dimensional data are input. The
computer calculates the seal ring stresses and deflections for varying radial
sections of the retaining band and insert. The seal ring dimensions were then
selected, consistent with the proper stress levels, to provide the minimum
change in clearance gap. The static ambie-t seal rlng clearance gaps were
established, consistent with the clearance differential, to provide the resulted
operating clearance gaps. A summary of the seal ring stresses, deflections, and
clearances is given in Table 9.
Static Flange Seals. All static flange seals are of the pressure-sensltlve metal
spring type (Fig. 35). The seals were designed and fabricated for each specific
ap_llcatlon by Hydrodyne Dlvislo_ of Donaldson Co. Inc. The base material was
Inconel X-750 wlth a 0.0076 m (0.0003 inch) thick silver plating applied to
improve sealing effectiveness.
LOMPRESSURE
SIDE
HIGHPRESSURE
SlOE
Impeller Wear Rings. Internal recirculatton of LOX arolmd the impeller front
is controlled by step labyrinth wear rings (Fig. 36). The nominal dtametral
clearance between the rotating member and stationary platfor_ is eet at 0.15 mm
(0.006 inch). With this clearance, eolm rubbing contact is expected because of
eccentricities and deflection. To moderate the effect of rubbing, a 0.25 mm
(0.010 inch) thick layer of silver plating is applied to the stationary platforms.
[
CP
4J 4=;
63
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65
/
Rotordynamics
The critical speeds of the rotating assembly were calculated by the lumped para-
meter method in which tLe rotor is simulated by a series of mass points whose
spacing approximates the mass distribution of the actual hardware. The calculated
mass oroperties of the rotating assembly are given in Table I0; a schematic of
the rotordynamlc model is shown in Fig. 37.
The initial approach was to have all four bearings share in carrying the radial
i Fig.
load. 38. It is evident
The predicted that speeds
critical the second
for critical speed fallsare
this configuration essentially
indicated on
in the
I operating speed of 7330 rad/s (70,000 rpm), which is not an acceptable condition.
! To resolve this problem, the radial constraint on the outboard pmnp bearing was ""
] removed. The critical speed prediction for this case is presented in Fig. 39.
I Since this configuration provides a satisfactory margin around the operating
speed, it was accepted for the final design. The radial constraint is removed
from the outboard pump bearing by making the bearing sleeve bore larger than the
outer race diameter by 0.25 nun (0.010 inch).
The mode shapes for the first, second, and third critical speeds as a function
location along the length of the rotor are given in Fig. 40.
Material Selection
o
The materials selected for the more significant components of the Mark 48-0 {
turbopump are inJicated in Fig. 41. In Table Ii specifications and properties
for these materials are summarized.
_,_ principal criteria for choosing the materials in the pump were: strength
and ductility at cryogenic temperature, LOX compatibility, resistance to corro-
sion, thermal contraction coefficient, and ease of fabrication.
The impeller, inlet housing, diffuser, and volute were all made of Inconel 718.
Inccnel 718 is a nickel-bas_ precipitatlon-hardenable alloy which has both
excellent strength and ductility at cryogenic temperatures. The same material
was used for these four parts because it was desirable to have a common thermal
coefficient to maintain control over critical radial and axial clearances. Silver
plating was applied to the inlet housing in the inducer tunnel and on the impeller
front wear ring labyrinth lands to permit light contact with the rotating parts
in these areas with a minimum of local heating. For the same reason, the station-
ary lands o£ the balance piston low- and hlgh-pressure orifices were also plated
with silver.
67
Dlametral Hass
Joint Hass Group Distance Homent of Point Hass Moment
Number Number Along Axls Wet Mass Inert;_, _ID) , of Inertia, (Ip)
(J) (G) (X) (W), gm gm cm- gmcm2 i
! I 3.05 81.2 85.4 100
2 -- 4.57
3 -- 5.33 +
4 2 6.1 332.0 7_0 1165
5 -- 7.16
6 3 8.33 42.6 2!.7 36.6
7 4 9.09 29.9 13.5 24.0
8 3 9.96 42.6 21.7 36.6
9 5 i1.10 75.3 54.4 92.5
I0 o 12.10 232.7 509 974
il -- 13.21
12 7 14.12 161.5 190 246
13 -- 12.95
14 8 16.84 172.4 2r9 214
15 8 19.30 172._ 209 214
16 9 21.76 1026.9 6903 13420
17 -- 22.86
18 I0 24.51 194.6 290 244
19 -- 25.91
20 II 26.92 38.6 22.2 37.8
21 12 27.69 24.0 26.9 52.5
22 II 28.58 3S. 22.2 37.8
23 14 29.72 43.1 25.2 37.2
24 15 32.39 132.4 201 101
Total 2840.7 !
68
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69
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72
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FIRST CRITICAL
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K _
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N
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• 76
/
Two alloys were in primary contention for the rotor (Astroloy and Waspaloy); b _th
would have satisfied the structural requirements. The decision to use Waspaloy
was based on procurement time and cost considerations.
The high operating pressures and temperature dictated the use of Rene'41 for
the main structural walls of the turbine manifold. Rene'41 is a double, vacuum-
melted, precipitation-hardenable, nickel-base alloy. Although difficult to
fabricate because of strain-age cracking in weld heat-affected zones, it has
superior strength in the operating temperature zone of the Mark 48-0 turbine
manifold.
The turbine nozzle and the seal support section of the housing were made of
Haynes 188 which is easier to fabricate, has adequate strength, and is uL_affected
by the heat t c,_atment cycle to which the Rene'41 details have tu be subjected ""
after assembly welding.
The main section of the rear bearing sulport, which is primarily in a cryogenic
environment, was made of Inconel 718. However, the section which forms the tip
seal over the rotor blades required a special consideration because of a need
to minimize the blade tip clearance growth at the high operating temperatures.
To accomplish this, Inconel 903, an iron-nickel-cobalt base alloy with excellent
properties at the operating temperature and a very low thermal expansion coeffi-
cient was selected.
Heat transfer calcu]atlons were made to establish the thermal conditions on those
components that would be subject to high temperatures or thermal stresses. These
included primarily the turbine wheel and turbine manifold; but calculations were
also made to determine the critical diameters of the shafts in the dynamir seal
areas during operation.
77
.......... I - I 1 i
B
306 K--
(260 R) _ / f . _ •
v, i m
: I I I I I I I 1 ] I i I I I I I I I I I
78
1057 (1903) (1857) 1031
944 11701] _ (17001 944
(14001 779
778 (
11000) 556
385 (69: - _t_'_ (907) 504
--" 556 (1000)
-- t! _ DEGREES RANKINE)
-- 286 (5141 --- 170 (306)
- t
280 1505 " 118 1212)
__ ; _
_ _./_, '",_"_,
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272 (490) : _ _ 86 11551
) 1112"J , 11241
118 (2121 67 (1211
7! 72 _ 69
14 ) 113(] 1 11251
: 102(1841 I-- I
'_ 79
1 ,,, i i _ I ] i i
very )ow temperature; only at the rim does the temperature level increase to
approach the gas temperature. The temperature of the turbine blades during i
steady-state conditions is equal to the gas temperature.
Analysis of the turbine manifold included both transient and steady-state condi-
tlons. Because of idle-mode start planned for the Advanced Space Engine, the
start transients did not xmpose _ny significant thermal gradients on the mani-
fold. Steady-state thermal grandients and resulting strains were also acceptable.
In contrast, the cold-gas shutdown purge introduced severe transient thermal
gradients that would have precluded meeting the 300 life cycle requirement with p
a safety factor of four. The shutdown temperature characteristics are illustrated
in Fig. 45. To improve the situation, a 1.57 mm (0.062 inch) thick Inconel 903
liner was included in the design, which acts as a thermal shield for the main
s=ructural walls during cutoff transients. The predicted temperatures (Fig. 46)
are such that the 300 life cycles can be achieved with adequate safety margin.
Figure 47 presents the results of the analysis relative to the thermal profile
of thL aft-stud shaft in the area of the outboard seal.
i
t
81
1398
.,,.
.-38 34_ '8 I 142 186J 204
• ., /,4/ 3,o/. _o
ii,,oi,,.i
•2 -260J / I 348/ 439 i
Kelvin Scale
1032
111 ----_T _ 3
111 170 | /I I
248 317 415 448
Fahrenheit Scale
82
83
I I I I I 1 I #
Stress Analysis
Impeller. A finite element model of impeller back plate was constructed and used
to establish stress, strain, and deflection levels. The analysis was based on a
maximum required operating speed ef 8063 rad/s (77,000 rpln) ar,
d the pressure load
schedule shown on Fig. 48. The basic sizing of the impeller was perfornled using
the following cast Inconel 718 properties.
This was to provide the flexibility of producing the impeller either by casting
or machining from a wrought alloy. Tie first two impellers were fabricated by the
latter method; consequently, they have higher safety f=c=ors by a ratio of 1.6:1.0.
Based on cast properties and a notch factor of 2.0, the burst speed was relcul_ted
at i0,000 rad/s (95,500 rpm), which establishes the allowable operating speed at
8335 rad/s (79,600 rpm) using a 20% margin. The factcr of cafety on the _pllne
was 3.83 based on shear ultimate. The factor of safety on th _ vane stresses was
calculated at 1.93. The radial and tangential stress profile resulting from cen-
trifugal effects on the backplate is plotted in Fig. 49, as a function o_ radial
location. Figures 50 and 51 present effective stress profile and maximum effec-
tive stresses resulting _rom combined centrifugal and pressure loads. The effec-
tlve straln profile from the combined loading is shown in F_g. 52; Fig. 53 sho_s
the deformed structure of the impeller with radial and axial deflections indicated
at the cri_ic_l location of the balance piston hlgh_pressure orifice lip. The
' Goodman diagram for the vanes, taking into account centrifugal and pressure ef-
fects, is included in Fig. 54. It shows that the calculated alternating s,:ress
of 1944 N/cm 2 (2820 psi), 30 percent of pressure loading, is far below the allow-
able 6984 N/cm 2 (I0,000 psi) for a mean stress of 43,300 N/cm 2 (62.0C0 psi).
Inducer. The inducer blade stresses were computed 5y dividing the blade into a
series of ple-shaped s_ctlons, loading each section with pressure and centrifugal
forces, and _alculatJng the measurements and stresses at the blade root. The com-
puted stresses and factors of safety were:
84
i
",L , I it l :__ I I I
8Jo2 N/cm2
(4212 PSI)
2e' .. N/cm2
(412! .PSI) _PS I) 2891
2904 Nlcm 2 N/cm2 (4194 PSi) _AX
N/cruZ (1553 PSI) HIN
2625 N/cm2
(3806 PSi) /--2279 N/cm2 (3306 PSI) MAX
• ._
f (665 PSI) HIN
85
J
/
60, I
J
4o- 56 l
I
-,
- .....
i. "5
52 -- +
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,8 ! I
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EI_IU_-- I1404E5
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! 2 3
RADIUS, cm
i!
_ i 86
I
! , I .,,II I I
1.3--
N - 775)00 RPM 10,547 Nlcm2
1.1-- _k_
1J0-- 18,820NOcm
2.
- (27.300 PSO)
.9--
2 J--
6 z n
Ic
.5-
! .4-- IH[
-- 36436 Nlcm2
.3- (61,400PSl)
.1 m
!
i 87
i
(
I
,443 N/cm2
(19,500 PSi)
HAX. EFFECTIVE
N = 77,000 RPH
88
.I I I l I I I I I
/ _ _,'_-_o. 000374
0.000757
N = 77,000 RPM
AXIAL DI $PLACEHENT E
O.OSl mm (0.00]99 INCH),_ I
__k
l
1
" "_0 .OI24mm
(0°00049 INCH)
RADIAL DI SPLACEHENT
N- 77,OOORPH
9O
+
A Goodman diagram for the inducer blade (Fig. 55 ) shows that the calculated alter-
hating stress of 11,424 N/cm2 (16,571 psi) is well below the allowable alternating
stress of 23,800 N/cm 2 (34,500 psi) at the mean stress of 14,675 N/cm 2 (21,291 psi).
Turbine Wheel. The finite element model of the turbine disk used for heat transfer
analysis was also utilized to calculate the stress and strain levels. Using a
conservative assumption of 866 K (ii00 F) for an avecage disk temperature and
corresponding properties of 93,760 N/cm2 (136 ksi) for ultimate strength, 73,100
N/cm 2 (106 ksi) for yield strength and 15% elongation, the burst speed was calcu-
lated at 10,158 rad/s (97,000 rpm). The maximum allowable operating speed, with
a safety factor of 1.4 on the ultimate is 8587 rad/s (82,000 rpm).
The radial and tangential stress levels as a function of radius are presented in
Fig. 59. The effective strain proflle Is shown in Fig. 60 and 61 for the maximum
and nominal gas temperature condition. Radlal and axial deflectlons were estab-
lished at the rim to permit pro_er setting of assembly clearances. The rim de-
flections are indicated in Fig. 62. The stress rupture llfe of the disk , as a
function of temperature, is shown in Flg. 63; included in the curve is a safety
factor of 1.4. Figure 64 is a modified Goodman diagram of the stresses in the
turbine blades at a gas temperature of 1055 K (1900 R). It shows that the calcu-
lated alternating stress of 2070 N/cm 2 (3000 psi) is well below the allowable al-
ternatlng stress of 8270 N/cm2 (12,000 psi) at a mean stress of 27,600 N/cm2
(40,000 psi).
TurblneManlfold. The turbine manifold was analyzed for steady-state and tran-
slent conditions using a finite element model (Fig. 65). Because of the type of
idle mode start planned for the ASE, the start transients did not present struc-
tural problems. The engine cutoff on the other hand is characterized by a cold
hydrogen lag in the preburner, which introduces severe thermal gradients in the
manifold walls. To reduce these thermal gradlents, a 1.57 mm (0.062 inch) thick
Inconel 903 liner was incorporated in the inlet torus. The strain profiles with
the llner are i_aluded in Fig. 66 for steady-state conditions and.Fig. 67 for
cutoff. The maximum strain observed is 0.0037 for steady-state a_d 0.0058 for
cutoff transient.
The maxlmumpressure-induced stress level in the manifold is 27,600 N/cm2 (40 k_i)
with the resulting safety factor of 3.5 on pressure stresses. The steady-state
effective stress profile, including thermal effects is shown in Fig. 68; the maxi-
mum stress level is 64,000 N/cm 2 (93 ksi). Similarly, the stress distribution
under cutoff transients is shown in FiB. 69; the maximum stress observed is
68,100 N/cm 2 (98.8 ksi), which results in a factor of safety of 1.4, based on a
tensile ultimate of 96,500 N/cm2 (140 ksi).
i 92
i
/
- N/cm2 N/cm2
_ 6340 PSI ) (6340 PSI)
- N/cm2
--
m
(9980 PSI )
M
- I I 0 N/cm2
-- (3060 PSi)
-- 6,890 Nlcm2
_ (24,5oopsi)
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Gas Generator
The gas generator was designed as a piece of special test equipment to provide
the drive gas for turbopump testing. The requirements that are _mposed to meet
the basic intent of such a facility item were: (_) stable operation at all op-
erating points, (2) repeatable high performance, (3) uniform exhaust gas temper-
ature profile, (4) reliable ignition, and (5) durability and long llfe.
The gas generator design uses separate injector and combu_tor assemblies which
are attached with a bolted flange (Fig. 70). The injector has five coaxial in-
Jection elements which are designed for stable operation, hlgh-performance and _'
complete mixing. The nominal operating parameters for the injection elements are
given in Table 12, Analysis of the element design, using the Rocketdyne steady-
state combustion model, indicated complete combustion within a distance of 3.5
inches from the injector face (Fig. 71). The output from this model was also used
to conduct a Prlem analysis to evaluate the sensitivity of the combustion process
to transverse acoustic modes in the combustor. The results of this analysis in-
dicated the gas generator will have stability superior to the J-2 and J-2S engines
(higher A), which exhibited dynamic stability to all but intermediate size bombs
(Fig. 72). The injector element was also designed with adequate injection pres-
sure drop (P/Pc " 0.13) to isolate the gas generator from feed system coupled
modes.
10#
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IGNITER l
ASSEHBLY I
LO2 INLET _
INJECTOR-_ /
109
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The injection elements are a self-contained design in which each element is built
as a brazed assembly for individual calibration (Fig. 73). The elements have a
recessed oxidizer post with four centering devices for positive alignment within
the fuel sleeve. The element material is CRES 304L. j
The injector body is an all-welded assembly fabricated from CRES 347. The injec- "
I tor elements and NARIoy faceplate are brazed into the injector body. GRAYLOC
i fittings are used as propellant inlets to interface with the test facility. An
envelope was retained in the center of,the injector for use of the spark igniter.
The combustor is an all-welded assembly of the combustor body, elbow, and transi-
tion section. Added margin for complete mixing and a uniform exit temperature
has been provided by using the elbow to induce circulation. The combustor is
cooled by film coolant injected from orifices at the periphery of the injector.
The film coolant temperature is shown in Fig. 74 as a functlon of the distance
from the injector face.
Acoustic absorbers were placed in the combustor wall, directly below the injector
face, to provide added stability margin by damping acoustic modes in the combus-
tot. A sur_ary of acoustic absorber experience (Fig. 75) shows that the design
open area of the gas generator acoustic absorber lies in a favorable position.
A welded transition section was used between the gas generator and turbine mani-
fold because analysis showed that the high temperature in this area would prohibit
effectlng _ positive seal with a flanged Joint. The joint is fabricated by weld-
ing the Inconel 625 transition piece to the Rene' 41 turbine manifold (Fig. 76).
This weld is then heat treated. After the Inconel 625 gas generator transition
piece is welded to the combustor elbow, the two transition pieces are joined with
an electron beam weld. Th_ gas generator transition piece has a liner section
which extends over the transition piece welded to the turbine manifold. This
forms a thermal barrier which ensures that the life of protected transition piece
is consistent with that of the turbine manifold. The design of the transition
section allows the gas generator to be removed and rewelded to the turbJne mani-
fol_ without harming the heat treat or weld between Rene' 41 an,_ Inconel 625 since
the _ework can be made in the protected Inconel 625 transition pieces.
i
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116
FABRICATION
Cqmponent Fabrication
The methods employed in fabricating the major components of the LOX turbopump are
discussed in the following paragraphs. _,
!
i Inducer. The inducer blades were machined from K-monel bar by pantographing. No
difficulties were encountered in its fabrication. Figure 77 shows the completed
inducers. _,
Impeller. The impeller internal flow passages were generated by electrical dis- a-
charge machining. Electrodes were introduced from the inlet as well as the dis-
charge side to form the blade surfaces. Some difficulty was experienced in obtain-
ing a smooth trdnsition between the inlet and discharge, in the area where the
leading edge of the partial blade is located. The difficulty was presented by a
combination of small passage width (3.81 mm, 0.15 inch) and small blade angle at
the discharge (0.49 rad, 28 degrees) and large blade wrap angle (2.65 tad, 152
degrees). One set of impellers were scrapped because of dlmcontinuity in the
passages as a result of a machine indexing error. The delivered impellers were
accepted only after several hand rework operations were performed to obtain a
smooth transition.
Diffuser. The diffuser was machined from an Inconel 718 forging by conventional
methods with the exception of the vane surfaces which were generated by electrical
discharge machining. No difficulties were encountezad in fabricating this part.
%
Volute. Because of the contoured surfaces included in the volute, it was mor_
econo_ :al to produce it by casting. The investment casting technique yielded an
excellent quality part from the standpoint of conformance to drawing dimensions
and surface finishes in the flow passage. The unmachined castings are shown in
Fig. 78.
Turbine Manifold and Housing. The fabrication process of the housing is illus-
trated with a series of photographs in Fig. 79. It was the most costly of the
LOX turbopump parts, and it required the longest time to complete.
The housing (Fig. 79A) was machined from a Haynes 188 forging. Intersecting
holes were drilled o_ electrical discharge machined and capped by welded plates
to provide drain ports for the primary hot-gas seal, secondary hot-gas seal, and
primary LOX seal, as well as purge passage for the intermediate seal. In addition,
six instrumentation ports and passage_ were incorporated.
The nozzle (Fig. 79B) was also fabricated from Haynes 188 forging, with the flow
passages generated by electrical discharge machining. The throat area of one of
tbo two nozzles fabricated was 5% over the nominal required per blueprint. It
was estimated that this would degrade the efficiency of the turbine 2.7% but would
reduce the engine chamber pressure only 0.165 x 106 N/m 2 (24 psi). The deviation
was accepted.
i I17
ORIGINALPAGE IS
0_] POOR QUALITY |
118
*\ OF p(_R QLIAL_TY
J
(A)
(O)
d
_0LDOUT FRAME
I
% L •
................ m
(G) (HI
11)
120
!
i The main structural details of the _anlfold were machined from Rene' 41 and Joined r
by welding. The two principal details are shown in Fig. 79C with the inlet trans-
ition welded to each cylindrical half. Hastelloy was used as the principal weld
I filler metal, but an Incoloy 88 weld overlay was applied on the inside surface of
; each Rme' 41 joint to minimize hydrogen environment embrlttlement. An example _
i of the weld overlay is shown In.Fig. 79K for the closeout weld that Joined the :
two manifold halves. Figure 7_F through 791 show the housing and manifold in
successive stages of assembly. Difficulties were encountered in obtaining sound
welds where the inlet and discharge transitions were attached to the manifold
halves, primarily because varying material thicknesses and difficult-to-fit coni-
cal welds were involved. Repeated grindouts and weld repairs were made before
penetrant and radiographic inspection criteria could be satisfied. On future
parts, it is recommended that these transitions be machined.integral with the
manifold halves.
Rotor. The rotor (Fig. 80) with the pump inlet, volute, diffuser, and inducer,
was machined as an integral piece from Waspalloy forging. The unshrouded blades
were generated by electrical discharge machining, plunging radically inward
with an electrode plate which formed both sides of the blade concurrently. The
electrical discharge machining setup is illustrated in Fig. 81.
Rear Bearin_ Support. The rear bearing support was a welded assembly, with the
main support machined from Inconel 718 and the discharge gas straightening vanes
from Inconel 903. Copper plating and Incoloy 88 weld overlay was applied to the
transition ring that supports the straightening vanes, since this area is poten-
tially subject to hydrogen environment embrittlement factors such as high strain
and high-pressure hydrogen at close to ambient temperature.
Turbopump Assembly
Rotor Balance. The Hark 48-0 rotor operates at a maximum speed of 8063 rad/s
(77,000 rpm); as a resultta high degree of precision in its balancing is impera-
tive. A Gisholt dynamic balance machine with a capability for detecting 6 x 10 -4
In (25 _inch) radial motion was used. For the Mark 48-0 rotor m ss of 2.84 kg
(6.25 pounds) this translates into machine accuracy limit of 0._8 _a cm (0.07 gm
inch), which would cause a radial load of 98 N (22 pounds) at the design speed of
7330 rad/s (70,000 rpm). The rotor was supported in the balanct cradl_ by two
pairs of turbopump bearings, each pair axially preloaded in the bearing cartridge
exactly as in the turbopump assembly (Fig. 82). Balancing was initiated using
the main rotor and the rear stub shaft assembl_ and wax cozrections wtre made in
the plane of the turbine wheel and the stub shaft.
J 121
,i
f I
t23
Figure 82. ttark48-0 Rotor on the Gisholt Balancing Hachine
i ....
/
t
Turbopump Buildup. The buildup of the turbopump was accomplished in the following ,_
sequence:
2. Front and rear bearing inner race spacer thicknesses were established
to provide the desired bearing preloads. The final preload character-
istics obtained are shown in Fig. 84 and 85.
3. The slinger hub thickness was adjusted to obtain .3.175 mm (0.125 inch)
turbine nozzle to rotor blade axial clearance.
i0. The rear bearing seal was installed in the rear bearing support, and the
created subassembly was installed on the housing.
12. The diffuser subassemblv including the front bearing package and the
_ volute were added to the pump end of the housing.
14. Measu,'ements were taken to esrabllsh the impeller, slinger, and turbine
wheel a'£al clearances.
i 125
.0005
.0127 =.
.0004 in.
.Ol02um
.0076
in.
.0279 nm
.0004 tzm_
]
.0102 0
.0003 in.
.0076 mt
.0006 in.
.0152 mm
126
!' !
i 127
12_
&
Figure 86. Mark 48-0 Turbopump S/N 01-0 Pump Diametral Clearances
129
1"-.o178,m
[.-.0oo7 in
, \ L.OO-
L.OO14 in
r.o66o ms __
,, L-.OOO7 in
r-.o178 .m
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_l r / //' "-"L-..°oo7 in
i Ftsure 87. Hark 48-0 Turbopump SIN 01-0 karin8 Fits '
t
Ftsure 88. Mark 48-0 S/_ 01-0 Seal Dtametral Clearances
: 131
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133
17. The instrumentation sleeve rear cover, three Bently proximity indicators,
speed and temperature probes were installed.
18. The shaft seals and external flanges were checked for leakage rates.
20. The turbopump was weighed. The total weight was 54.5 kg (120 pounds),
including gas generator body and auxiliary gear drive features.
134
ORIGINAL
PAGEIS
OF,
POORQUAlifY/
, 135
.I
TESTING
In conjunction with the hot-streak/erosion problem encountered with the LH2 turbo-
pump gas generatJr combustor, the two LO 2 turbopump gas generator injectors wure
dimensionally inspected and water-flowed to evaluate impingement patterns and
I coaxial-element, quantitative-flow distributions During tb_ hydrogen-side, water-
i flow tests on both injectors, leaks were observed between the fuel sleeves and the
injector-face _mterial. A microscopic inspection of the braze joints in the
affected areas revealed voids in the braze material. Both injectors were rebrazed
successfully at Rocke_dyne. A vacuum _eak check of the oxidizer manifold showed
no evidence of interpropellant leak path_ within the internal LO 2 posts/injector
joints. Figure 93 shows the resu!_ c the initial water-flow tests showing the
leakage areas. (Note: The outf c I0 elements of the injector are plugged since
the same injector pattern is u_ed for the LH 2 turbopump gas generator injector.)
Table 14 presents the dimensio_ml inspection results on injector P/N RSOO5024E-161,
Units 1 and 2, while Tables 15 and 16 presents the results ef the water-flow tests
after the rebraze cycle. Prior to the water-flow tests on each injector, the LO 2
posts were mechanically aligned with special fixtures. Subsequent to the water-
flow tests, the posts were checl.ed to en_ure correct alignment.
Table 17 presents an overall test summary of the LO 2 turbopump gas generator devel-
opment testing, while a more detalled discussion of various aspects of the program
is included below.
Pr___c.pellant
Servovalve Operation. The performance of the gas generator depends on
a closed-loop pressure fuel back sib_nal using propellant injection pressures as
the control parameter. The hydrogen and oxyge,L servovalve injection set i_ressures
are predetermined based on the required performance level and the hydraulic resist-
ance of the individual injector system. The gas generator Ferformar .e is balanced
to achieve the desired flowrates through the injector by the use of a Rocketdyne-
prepared GE-Timeshare computer program (RECAL 2). This informstion is translated
into s_rvovalve controller settings, which are manually set prior to the rest.
Test:_ 016-030 and -031 failed to achieve main propellant tgnltion because of tbe
system characteristics of both the gas generator injector a,Ad the facili=y LO 2
servovalve controller. The objective of these tests was tJ demonstrate the igni-
tion transition characteristics of the LO 2 turbopump injector. The test sequence
i 137
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i 144
[ Test L Accumulated
. , I _'_
I Test Ouratlon, Duration I
Number Test 0atel Objective seconds Te_ts seconds Remarks
0i6-030 10-7-75 Rain Propellant 0.0 I 0.0 Igniter stage OK. Heinstage (H/S) not achieved
Ignition (RPI) due to servovalve system response.
016-031 10-7-75 RPI 0.0 2 0.0 Ma;nstage not achieved. Cutoff Inltleted at
time HLV started to open. Sequencing for next
test modified.
016-035 11-6-75 Rainstage 0.0 6 4.32 Fuel injector temperature continue gate cutoff - •
Performance safety sequence problem.
016-038 11-7-75 Hainst_ge 0.0 9 11.32 Ignition detect .cutoff - spark proble_
Performance
i Duration
016-0k2 11-11-75 Halnstage IS.0 13 31.32 I Objective achieved.
, Duration
016-0E3 %1-11-75 Halnstage 0.0 Ik 31,32 Ignition detect cutoff - spark problem.
Duration
OI6-Ohk 11-12-75 _alnstage 0.0 15 31.32 Ignition detect cutoff - spark problem.
0uration
016-0_8 12-_'75 Nainstage 33,0 J 16 6_.32 Premature cutoff et 33 seconds malnstage due to
145
p
J I I i |
i
times were based on the successful test sequencing demonstrated during the testing
of the LH 2 turbopump gas generator. In the case of the LO 2 turbopump gas generator,
two phenomena occurred:
i. The hydrogen lead flow was about one-half that of the LH2 gas generator
and required a significantly longer period during the fuel lead sequence
for the fuel injection temperature to decay below 88.89 K (-300 F), which '_
is a control gate to permit the main LO 2 valve to open, and _
2. Since the hydraulic resistance of the L02 side of the injector was higher
than the LH 2 turbopump gas generator LO 2 injector, the same injection
purge lockup pressure of 1268 N/cm 2 (1850 pqig) resulted in a LO 2 injec-
tion pressure (during fuel lead) of about 762 N/cm 2 (lll3 psig). As a
result, the actual opening of the main LO 2 servovalve was delayed, and ="
the tests were terminated when the mainstage d_ration timer expired.
Basically, the problem can be attributed to a lack of sequence character-
ization experience with the LO 2 turbopump gas generator system as well
as the required short mainstage duration. Figure 94 depicts the LO 2
servovalve system operation for the LH 2 turbopump gas generator, while
Fig. 95 shows the empirically observed results of tests 016-030 anC -031.
Note the difference in the control delay time between Fig. 94 and 95.
An open-control enable signal is given to the LO 2 valve system, but the
actual start of servosystem operation is delayed until the fuel injection
temperature drops below 88.89 K (-300 F). The LO 2 turbopump gas genera-
tor hydrogen injection priming takes about 0.2 second longer due to the ,.
reduced flowrate. The LO 2 servovalve controller system was designed with
a control pressure ramp time of about 2.0 seconds to reach the desired
set pressure; therefore, the pressure ramp rates vary depending on the
level of the injection set pressure. That is, Pc buildup may be expected
to increase with higher L02 injection set pressures (higher required
chamber pressures, or increased hydrauli_ resistance of the injector).
Since the controller feedback control was based on monitoring LO 2 injec-
tion pressure, no opening command of the main LO 2 valve is signalled by
the controller system because of the existing LO 2 injection pressure,
which is the result of injector purging during the hydrogen-lead phase.
Once the controller system internal set ramp rate pressure exceeds the
actual monitored LO 2 injection pressure, the main LO 2 valve starts to
open to maintain the required LO 2 injection pressure. Main propellant
ignition is normally experienced about'0.35 second after opening of the
main LO 2 valve. Pretest calculations had shown that the 1267 N/cm 2
(1850 psig) LO 2 system purge lockup pressure was necessary to maintain
an acceptable gas generator mixture ratio during LO 2 feed llne LO 2 expul-
sion at cutoff. Actual LO 2 feed line LO 2 expulsion time was 3 seconds
as compared with i second for the LH 2 turbopump gas generator.
Although tests 016-030 and -031 did not achieve main propellant ignition, signifi-
cant data were obtained to characterize the LO 2 turbopump gas generator sequencing
control. Adjustment of the starting sequences from tests 016-030 and -031 was
successful in achieving the first main propellant ignition test of the LO 2 turbo-
pump gas generator. A main chamber pressure of about 2068 N/cm 2 (3000 psig)
was obtained for a mainstage duration of 0.32 second. A posttest inspection of
the injector and combustor revealed no damage.
146
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147
Combustor Exit Plane Temperature Profile. During testing of the LH 2 turbopu_@
gas generator, a large thermal gradient, wall to gas core, existed at the combus-
tor exit plane. Eight thermocouples were used during that period and recorded
temperature gradients of about 27B K (500 R). A modification to the combustor
(90-degree meter bend) solved the problem by enhancing the mixing of the gas pro-
ducts prior to exiting the combustor. The LO 2 turbopump gas generator combustor _
was fabricated very close to the geometry of the initially designed LH 2 turbopump
(. combustor. The major difference existed in the chamber characteristic length, L*,
I. which increased as a function of the exit nozzle a_ea change, or about 2.2 times
the LH2 turbopump gas generator combustor L*. It was concluded that the LO 2 tur-
bopump gas generator combustor would be tested in the as-fabrlcated condition to
observe the actual thermal gradient during hot fire before any modification, simi-
lar to the LH 2 turbopump gas generator combustor, could be considered. Four exit
plane thermocouples (chromel-alumel) were inserted in the thermocouple exit ring
at various insertion depths: 0.175, 0.196, 0.425, and 0.575 inch. In addition,
prior to the last test (016-048), eight external-skin thermocouples were attach@d
to the combustor exit to obtain hegt transfer information on the long test as well
as providing additional redlines as a safety precaution during the long test.
Figure 96 presents a schematic of the gas generator combustor locating the external
and internal thermocouples. Table 18 presents the results of the exit plane tem-
perature study fop all mainstage tests conducted during this phase of testing.
Only one data slice is shown, but the data are representative of the entire applic-
able test.
Prior to test 016-048, eight thermocouples were attached to the combustor outer
wall as previously discussed (Fig. 96). Five of the upper combustion zone skin
thermocouples were monitored as redlines 1033 K (1860 R maximum) to ensure ade-
quate safety precautions for the projected long-duratior test. Previous calcu-
lations had indicated that the gas wall temperature and outsid_ wall temperature
would reach thermal equilibrium in about 100 seconds of mainstage duration. Figure
97 shows skin temperature No. 3, the maximum observed temperature for the eight
locations versus the test time base. Figures 98 and 99 present graphs of the
combustion gas temperatvre and chamber pressure versus the test time base for
! test 016-048. Figure I00 shows the gas gene_atcr Installation prior to test 016-
: _48, indicating the locations of the skin thermocouples. Figure I01 shows the
ond_tion of the combostor with the injector removed. No erosion or other damage
_o either the combustor or injector was noted.
! Throughout the test program, a uniform gas temperature (minimum thermal gradient)
had been recorded across the gas generator exit plane. The average temperature
variation of the four-thermocouple measurem_,it was about 20 K (36 R), or about
2% of the operating temperature. Since the gas generator combustor unit will
provide the required hot-gas temperature with a minimum thermal gradient and a
sufficient thermal margin in the hardware, it is concluded tha_ the existing LO 2
turbopump gas generator injector and combustor design is acceptable for use with
the LO 2 turbopump testing.
149
'1
1 [I ..,--- LH
2 INLET
INJECTOR _ _ =,ll
TURBINESIMULATION _ __ BODY
SKIN TEMP#2
TEMP #4
THERMOCOUPLE
RINO
; i
' 1
i, 150
L _
TABLE 18. LO 2 IIJRBOPUMP GAS GENERATOR COMBUSTOR TEP_ERATURE STUDY
(Metric Units)
Average ,,
Total Overall Nainstage Ex Temperature
l Test OG GG Combustor Exlt Varia,ion
Test Duration, Pc,2 Flow.ate, _lxture Temperature, (4 Heasurements).
t No. seconds N/cm k_/sec Ratio K K
I I
OI6-032 0.32 _ TOO SHORT FOR PERFORMANCE
016-033 2.0 2097 1.456 0.713 74ta 19
016-034 2.0 2234 i.247 1.19 1030 52
016-036 2.0 2275 1.418 0_7_; ; 800 17
0_6-037 5.0 2279 1.431 0.759 795 24
016-039 5.0 2316 1.466 0.777 808 13
0!6-042 15.0 2309 1.383 0.888 92_ 8
016-048 33.0 2306 1.370 1.023 1077 7
I +J+__ _J
(English Units'1
Average
. Total Overall Maln_tage Fxlt Temperat
Test GG GG Combustor Exit Variation
Test Duration, Pc, FIr_rate, Hixture T_mperature, (4 Measuremen ),
No. seconds psla :b/sac Ratio R R
"' I
016-032 0.32 = TeO _HORT FOR PERFORMANCE
, 016-033 2.0 3042 3.209 0.713 1340 34
016-034 2.0 324O 2.749 !.19 1854 94
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mainstage performance obtained during the gas generator testing phase (1975).
Also included in Table 20 is the gas generator performance during the hot-flre
8 testing of the Mark 48 oxidizer turbopump (1976).
As discussed earlier, the performan e level ot the gas generator is balanced using
a GE-computer program (RECAL 2), which uses as input parameters, the LO 2 and hydro-
gen injector hydraulic resistances, required chamber pressure, flowrate, and mix-
ture ratio. The control function used to obtain the required performance is the
applicable syste_ injection pressure, which is obtained by the use of servocontrol ,m.
valves in a closed-loop mode. Figure 102 is an injector performance map for L02
turbopump injector, P/N RS005024, Unit 4"0. 2, in the region near the design level.
While testing the turbopump, a variation from the design level was necessary due
to the off-nominal turbine pressure ratio; however, the off-nominal condltions
proved to be no problem _n the recalibration procedure.
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159
Turbine Calibration i
J The basic test setup is illustrated in Fig. 103. Power developed by the turblne
was absorbed by a Mark 4 pump which reclrculated water from a reservoir. A Lebow
in-llne torquemeter was installed between the turbine and the power-absorbing pdmp
to indicate the torque developed by the turbine.
Prior to at,sembly, the turbopump rotor was balanced dynamically. The radial run-
outs on the significant rotor diameters were measured, and are noted in Fig. 104.
Similarly, measurements were taken to establish the critical internal radial and
axial clearances, and are presented in F_, 105. Figure 106 shows the assembled
turbine calibration unit.
The testing was performed at Wyle Laboratocy, E1 Segundo, California, during the
period 4 through 9 February 1976. The installation of the test unit in the
facility is illustrated in Fig. 107 and 108.
A total of Ii tests were made, with GN 2 working fluid, at velocity ratio (_/Co,
total to static) ranging from 0.115 to 0.606, and turbine speeds from 523 to
1885 rad/s (5000 to 18,000 rpm). A tabulation of turbine test data appears in
Table 20, and a plot of turbine test efficiency is shown in Fig. 109. Turbine
efficiency w_ calculated with Lebow torquemeter torque and isentropic available
e.,ergy (total to-statlc) across the turbine. At a design velocity ratio of 0.343,
the turbine total-to-statlc measured efficiency was 51% compared with a predicted
value of 59.8%. Calculations show that with the measured performance the press re
ratio of the turbine would have to be increased from the design value of 1.424 tc
1.54 to generate the required power level.
The combination of low-pressure ratio (1.42) and low arc of admission (28.5% of
circumference) places this turbine in an operating region in which turbine techno-
logy has not been developed. Potential improvement in the performance may be
realized by increasing the number of active nozzle passages and reducing the
throat width to obtain the required total throat area. Depending on the engine
installation, improvements in the exhaust manifolding may be possible to minimize
the pressure losses charged to the turbine.
- _ 260
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Calibcatton Layout _!
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164
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168
• SINGLE ROW, PARTIAL ADMISSION
• ACTIVE ARC = 28.5%, IO3 DEGREES
0.5-
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0.1 223.8 _//kh s
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169
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Turbopump Testing
Test Discussion: Testing of Mark 48-0 turbopump P/N RSOO9820E, S/N 01-0, began
in the Lima test stand of the Rocketdyne Propulsion Research Area (PRA) on 9 July
1976 and was concluded on ii August 1976. A total of 18 turbopump tests for an
accumulated duration of 266.8 seconds was accomplished on the turbopump assembly.
The test effort was divlde_ into two main categories: Performance mapping, using _
GH 2 as turbine drive media, with LN 2 and LO 2 as the pumped fluid; and integrity
i testing, using a LO2/LH 2 gas generator as the turbine drive gas media, with LO 2
as the pumped fluid. Gas generator injector P/N RS005024-131, S/N 2, a coaxial
five-element design, was used during the hot-fire {esting.
Facility propellant supply and dlschargh systems are shown schematically in Fig. II0
(GH2 turbine drive system) and Flg. Iii (gas generator turbine drive system).
Figures 112 through 115 show the turbopump assembly in various views installed in
the test stand during the initial LN 2 testing phase. After the third test (016-
013), blast protection screens were added because of the amount and proximity
of the two propellant combinations (LO2/LH2). Figures 116 and 117 show the pro-
tective blast screen installed as a precautionary measure in case of hardware
failure during the LO 2 pumping test phase. Figure I18 shows the pretest chill
conditioning during the hot-gas testing phase, with gas generator injector (L02
unit 2) installed.
ObJectl,,e: Checkout and integrity test of turbopump at 3141 rad/s (30,000 rpm)
using LN 2 as the pumped fluid and GH 2 as turbine drive media.
Analysis: Prior to the test, a turbopump H-Q map chart was prepared for the
X-Y plotter system which enabled the controller operator (GH2 spln
valve and turb_pump discharge throttle valve controller) to evaluate
the turbopump real-tlme performance. The system responded closely
to the H-Q analytical predictions. A posttest review of the data
revealed a turbine pressure ratio of 2.12 rather than a deslred 1.4
to 1.6 value. The hlgher-than-deslred pressure ratio was caused
by too large a turbine discharge orifice (D = 1.7668 cm, 0.6956 inch).
Prior to the next test, a turbine discharge orifice of 0.5765 inch
was installed. A turbop_mp shaft torque check through the LO 2 inlet
showed the torque to vary from 10.6 to 49,4 mN (15 to 70 in-oz). A
visual examination of the rear bearing was accomplished by removing
the rear bearing housing. No visual discre_ancies were noted.
170
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171
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172
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OF POORQUALITy
173
ORIGINAL PAGe;IS
174 OR POOR QUALITY
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FLgure ll6, Lima Stand Turb'_l:,ump
Instal],_ "m
ORIGI_A_ PAGE IS
177
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Figure I17. Lima Stand Turbopump Installation
179
i I ) ) I t L _ |
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E E E E E E E
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I_ . 0 0 0 0 0 0
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Duration: 9 _conds
Objective: Locate the first and second turbopump critical speeds using LN 2 as
the pumped fluid and GH 2 as the _urbine drive media, t_"
Results: The test was terminated prematurely by the turbine radial accelero- y
meter vibration safety cutoff (VSC) system at i0 g rms and 4814 rad/s
(45,979 rpm).
! Analysis: The speed of the turbopump was brought up to about 2094 rad/s (20,000
! rpm) where adjustment of the throttle discharge valve was made to
i correct the pump performance to the design Q/N position At that ,b-
._ time, the spin valve was opened manually by the controller operator.
E Ldently the rate of speed increase was insufficient in the region
of the critical speed range. Cutoff was initiated by the VSC system
after accumulating I0 g rms count over 200-msec duration. A review
of the data revealed the first critical speed, to be about 4115 rad/s
(39,300 rpm). The second critical speed was not well defined due to
the abbreviated test duration. Another test was necessary to define
the second critica_ speed and to verify the value of the first criti-
cal speed. The turbine pressure ratio for this test was about 1.4,
with a 1.464 cm (0.5765 inch) turbine discharge orifice.
Duration: 5 seconds
Objective: Locate the first and second turbopump critical speeds using LN 2 as
the pumped fluid and GH 2 as the turbine drive media.
Results: Satisfactory test. All objectives attained. Maximum turbopump rpm
achieved was 6488 rad/s (61,965 rpm).
Analysis: Experience gained in the previous two tests defined the overall res-
ponse of the controller-GH 2 turbopump systems. As a result of the
second test (016-012), a throttle valve setting of 39% open was
required to maintain the design Q/N curve. For this test, just
prior to opening the GH 2 spin valve, the throttle valve was adjusted
to 39%. Since it was desired to limit the total turbopump accumulated
time in LN 2 service, the test required a rapid increase in the turbo-
pump speed to the targeted 6282 rad/s (60,000 rpm). The normal pause
at about 2094 rad/s (20,000 rpm) was eliminated. From the time the
GH 2 spin valve was opened to the time the maximum rpm (6488 tad/s,
617965 rpm) was achieved took about 3 seconds. A 2-second dwell
at 6488 rad/s (61,965 rpm) was followed by a planned controller
operator cutoff. All objectives were attained with verification of
the 4115 rad/s (39,300 rpm) first critical speed and a determination
of the second critical speed to be about 5228 rad/s (52,800 rpm).
Following this test, a visual inspection of the turbopump revealeJ
no damage or discrepancies. The facility system was prepared for the
next series of tests using LO 2 as the pumped fluid.
183
i
I
/
Duration: 70 seconds
Objective: Obtain head-flow data at 3141 rad/s (30,000 rpm and 6282 rad/s _
(60-000 rpm) using LO 2 as the pumped fluid, y
Results: Objectives partially attained. H-Q data was obtained at 2513 to
3036 rad/s (24,000 to 29,000 rpm) but, during the transition in
speeds, the rate of increase within the critical speed region was
slow enough to accumulate 200 msec of 15 g rms level, which triggered
, the VSC cutoff system at 5497 rad/s (52,500 rpm). _.
Analysis: The test progressed smoothly from tank pressurization, throttle valve
adjustment and H-Q excursion in the 2513 to 3036 rad/s (24,000 to
29,000 rpm) region. Upon increasing turbopump speed by manually
adjusting the GH 2 spin valve, the turbine radial accelerometer
triggered the VSC cutoff system. No damage was noted to the hard-
ware. _or the next test, the turbine discharge orifice was changed
to 1.628 cm (0.6411 inch) to target a 1.6 turbine pressure ratio.
Objective: Obtain H-Q mapping at turbopump speed of 6282 rad/s (60,000 rpm).
Results: Objective partially attained. Some H-Q mapping was achieved at
637 rad/s (60,850 rpm), but the test was terminated prematurely
by the window observer due to a fire ii_ the test area.
Analysis: A posttest analysis revealed the location of the fire to be 0ehind
the stand bulkhead and in a facility line connection. Real time
television coverage of the test area, with replay c_pabllities,
was a definite asset to the testing effort. At the start of the
test, the pump discharge throttle valve was adjusted to 39% (390
dlal setting), and the turbopump speed rapidly increased until an
indicated 6282 rad/s (60,000 rpm) was reached. After a period of
stabilization, an H-Q excursion from nominal to high head/low flow
was achieved. During the excursion back through nominal H-Q toward
low-head/high-flow region, cutoff was initiated. No damage to the
turbopump system was evident. A turbine pressure ratio of 1.68 was
achieved with the 1.628 cm (0.6411 inch) turbine discharge orifice.
).84
i
J [ [ l I l J L
Duration: 12 seconds
" Objective: Obtain H-Q performance at a turbopump speed of 6282 rad/s (60,000rpm).
Results: The test was terminated prematurely by the turbine radial accelero-
meter VSC system at a turbopump speed of 5444 rad/s (52,000 rpm).
Analysis: At the start of the test, the GH 2 spin valve was opened to obtain
a stabilized turbopump speed of 3141 rad/s (30,000 rpm). After
stabilization, it was planned to rapidly increase the turbopump
speed through the first and second critical speeds to the targeted a-
6282 rad/s (60,000 rpm). Again, since the speed control was manual,
the rate of speed increase _i,rough the second critical was insuffi-
cient, and the test was terminated by the VSC cutoff system. No
hardware damage was sustained.
Duration: 37 seconds
Objective: Obtain H-Q performance at 6282 to 7329 rad/s (60,000 and 70,000 rpm).
Results: Achieved satisfactory H-Q data at 6282 rad/s (60,000 rpm), but the
test was terminated prematurely at 6700 rad/s (64,000 rpm) by the
turbine radial accelerometer VSC system before any H-Q mapping
could be obtained at 7329 rad/s (70,000 rpm).
Analysis: The test proceeded smoothly through the first targeted H-Q mapping
phase at 6282 rad/s (60,000 rpm). While adjusting the GH 2 spin
valve to achieve 7329 rad/s (70,000 rpm), the VSC cutoff system
- initiated cutoff at 6700 rad/s (64,000 rpm). This speed level does
not correspond to any projected critical speed region and, in fact,
no operational parameters indicated any reason for the premature
VSC cutoff. Checkout of the VSC system failed to show any abnor-
mality within the facility data acquisition system. This test
concluded the Series I GH 2 turbine drive test effort. The turbo-
pump system and facility were modified for hot-fire testing using
the gas generator.
185
i
l I I I l ,
Duration: O. second
Results: The test was terminated prematurely by the ignition detect system
of the gas generator. YI
Analysis: At "ignition OK" (combustion temperature greater than 700 K (800 F),
the automatic comparator circuit initiated cutoff due to an indi-
cation that the Igniter failed to ignite. A posttest failure analy-
sis revealed the most probable cause to be in the spark exciter
electrical network. A replacement spark exciter system was installed
and a successful visual spark test was accomplished prior to the
next test.
Results: Satisfactory test with a maximum speed of 6034 rad/s (57,629 rpm)
achieved.
Analysis: Prior to test 016-018, the turbine discharge orifice was changed
from 1.628 cm (0.6411 inch) to a 1.766 cm (0.6952) inch) diameter,
with a well-rounded entrance condition, to obtain a 1.72 turbine
pressure ratio with the hot-gas turbine drive. Actual measured
turbine pressure ratio for this test was 1.85. Performance of the
gas generator system was near nominal with a chamber pressure (tur-
bine inlet pressure) within 41 N/cm 2 (59 psi) o£ the target condi-
tion (Pc target = 1307 N/cm2 (1896 psia); actual = 1266 N/cm 2 (1837
psia) with a turbine inlet temperature of 978 K (1761 R). Start
and cutoff transients of the gas generator system were normal. The
characteristic velocity (c*) efficiency of the gas generator injec-
tor was 98.9%.
Duration: 0.58
:S6
/
Analysis: The maximum _pm achieved was 6122 rad/s (58,378 rpm). Start and 7
cutoff sequences were normal, with no damage sustained by either
the turbopump or gas generator systems. This test was scheduled
for a test stand propellant duration (_50 seconds mainsta_e) at
the same performance conditions as the previous test. A posttest
review of records showed the fuel injection pressure to be lower _
than the servocontroller set pressure, which lowered the fuel injec- _ _
tor hydrogen flowrate, increased the gas generator mixture ratio,
and resulted in an elevated combustion temperature which triggered
the overtemperature redline cutoff circuitry. Fuel injection pres-
I sure was about 120 N/cm 2 (175 psi) lower than the controller set
pressure. The controller was readjusted for the following _est
1,sing the on-line site data.
6bjective: Turbopump performance at 6282 rad/s (60,000 rpm) for test stand
duration (--50 seconds).
Results: Objectives partially achieved. The maximum rpm attained was 6575
rad/s (62,800 rpm) with steady-state performance until a premature
cutoff by the combustion temperature redline.
Analysis: Review of the scaled data revealed that the main fuel valve was
operating at about 2.5% open, or in a high-flow gain region. Figure
llggraphically depicts the problem. Note that, in the near-closed
position, relatively large fluctuations in flowrate can be expected
with small changes in valve position. The result of the fluctuation
• could cause the noted overtemperature in the combustor due to a sudden
increase in the gas generator mixture ratio. A similar problem
existed with the main LO2 valve during the early development testing
' of the LH2 turbopump gas generator system. The problem was solved
by changing the plug trim to a linear (flow increases proportionally
with valve position) design. A main fuel valve plug trim change was
; not deemed necessary because of the fuel-lead sequence and the nor-
mal operating position of the main fuel valve being in the 15% (oxi-
dizer turbopump gas generator) and 50% (hydrogen turbopump gas genera-
tor) open position at full 2344 N/cm 2 (3400 pslg) chamber pressure.
The effect_w gas co_bustion discharge flow area (turbine and dis-
charge orifice) for the present oxidizer turbopump, required opera-
ting the gas generator _t approximately two-thirds power. The net
result was that lower fuel injection pressures were required for
the lower flowrates The LH 2 tank pressure for_this test had been
lowered from 3B03 Nicm 2 (440 psig) to 2758 N/cm Z (4000 psig) (gas
generator testing to turbopump testing) to force the main fuel valve
to open further and stay outside of the hlgh-flow gain region. For
the next test, the LH2 tank pressure was reduced further to 2413
| _ N/cm2 (3500 prig) Gas generator performance remained normal, with
no damage sustained to either the gas generator or turbqpump system.
187 '_
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Analysis: Gas generator performance during igniter stage and fuel lead was
normal. Test terminated near the second critical turbopump speed.
No damage noted in either the g_s generator or turbopump system.
Results: The test was prematurely terminated by the turbine radial accelero-
meter VSC cutoff system at 20 g rms and a maximum speed of 7196
rad/s (68,725 rpm).
Analysis: All aspects of the test appears nomnal with the exception of the
apparent high g level at 7196 rad/s (68,725 rpm). No damage
noted to the hardware.
1119 _
Test No. 15: (016-025)
Test Date: 8-9-76
Objective: Turbopump performance at 7329 radls (70,000 rpm) and duration capa- |_
billty of test stand (_50 seconds). Y_
Analysis: A review of the records show that the fuel injection pressur_ was
again about 69 N/cm2 (I00 psig) lower than the required set pres-
sure as shown on the controller dlal. The resulting hlgher-than-
desired mixture ratio forced the combustion temperature over the
reallne. Actual targeted combustion temperature was ]033 K (1860R),
with an actual temperature of 1087 K (1957 R) recorded, which was
slightly over the redllne. For the next test, a slight power
increase was planned to ensure that the turbopump speed would be
at or above 7329 rad/s (70,000 rpm). Maximum speed for this test
was 7140 rad/s (68,199 rpm), and insufficient data were available
to ascertain whether the targeted 7329 rad/s (70,000 rpm) would have
been attained. The turbine inlet temperature redline was raised
to 1089 K (1960 R).
4
Test No. 17: (016-027)
" Test Date: 8-.11-76
* Objective: Turbopump performance at 7329 rad/s _70,000 rpm) and duration capa-
bility of the test stand (--50seconds). _
Results: Test prematurely terminated by turbine inlet overtemperature.
Analysis: Data analysis revealed the fuel injection pressure was again about
69 N/cm 2 (i00 psig) lower then the controller dial set pressure
requirement. The maximum speed achieved was 6582 tad/L, (62,867
rpm). No damage wa_ noted in the turbopump or gas generator sys-
tems. Fox the next test, a site data correction will be applied to
the fuel controller to increase the fuel i_ljection pressure by 69
N/cm 2 (i00 psig).
Objective: Turbopump performance and H-Q excursion at 7329 rad/s (70,000 rpm),
and duration capability of the test stand (--50seconds).
Results: The test was terminated prematurely by the intermediate seal purge
supply low-pressure redline circuit.
Analysis: All test objectives, except the demonstration of the test stand
propellant duration, was achieved satisfactorily. Maximum speed
achieved was 7191 rad/s (68,685 rpm). Figure 120 shows the gas
generator chamber pressure profile for the test with the average
turbopump speeds indicated during the various phases of the test.
As can be noted from Fig. 120, pumped idle-mode operation is nearly
achieved during the igniter/main purge _tart phase of the test. The
test proceeded smoothly through main propellant ignition, until after
about i0 seconds of malnstage, manual control of the turbopump dis-
charge throttle valve was initiated to first obtain high-head/low- !
flow conditions. During the planned excursion toward thp low-head/ _
_igh-flow region, cutoff was initiated automatically by the inter-
mediate seal purge supply pressure redline when the pressure dropped L
below 103 N/cm 2 (150 psig). Normal pressure setting at start _s !
138 ±7 N/cm 2 (200 _i0 psig). A review of the records show a ro1,_ ant
decay in the pressure from start until cutoff. After cutoff the
purge supply pressure recovered to the pretest value. An evaluation
of the intermediate seal pt,rge flow during various portions of the
test indicates that the purge flow rate increased from about 0.006
kg/s (78.3 ft3/min; 0.0135 ib/sec) _t s_art to abot,t 0.007 kg/s
(89.4 ft3/min; 0.015 ib/sec at cutof c. These flowrates match the
" observed changes in the purge system pressure. For the last I0
seconds of malnstage overation, the purge flowra=e remained essen- I
191
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195
I
20 30 40 50 60 70 80 90
REFERENCE
TIME, SECONDS
800 I "l I : I l i
I ' I I TEST016-0281
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REFERENCE
TIME, SECONDS
197 1
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REFERENCE
TIMEr SECONDS
ORIGINALPAGE I_
OF POOR QUAMT_
199
l
Pt_p Hydrodynamic Performance. The following discussion wlll cover, in order,
the pt_p head rise, pump ef_Ic_,,cy, axial thrust, and bearing coolant flow as
determined from the test data and co_pared with the original predictions.
Pm_ Head Rise. The Dump hea_ rise is determined by the relationship i_
Vd2 - Vl 2 Y_
H'- 14__(Pal-
40 Pi) +
where Pd and Pi are _he measured static pressures at the discharge and inlet of
the pump, respectively, and Vd and Vi are the average velocities at the dis-
charge and inlet, respectively. These velocities are not measured but are a
function only of the measured flowrate and the geometric diameters of the dis-
charge and inlet ducts. Therefore, the test head rise depends on the two pres-
sures and the flow measurements, all of which are considered to be the more
accurate parameters measured in test. The test data were generally sliced to
get steady4tate performance whenever the test duration was long enough to per-
_tc this. The data slices used for evaluating the hydrodynemic parameters vere
generally approximately 0.23 second in duration and were never less than O.10
second. This slice time is typical of those generally used at Rocketdyue for
steady-state data reduction programs.
Figure 1_6 is a plot of the pump overall head rise as a function of flow, where
both data end the predicted head are scaled to a speed of 7329 rad/s (70,000
rpm). The scaling was accomplished using the affinity laws which have been
thoroughly substantiated as applicable for LO2 and LN2. The _ata consist of 66
data points from 15 tests, with test speeds varying from 1628 rad/s (15,550 rpm)
to 7768 rad/s (74,190 rpm), and with ptmped fluids of both LO2 and LN2, primar-
ily the former. The symbols used for the data points distinguish the different
operating speed ranges tested. There was no indication that the results were
dependent on the ptmp e_ fluidmeditm.
The low-speed data show fairly good agreement with the predicted head rise,
but Nay be indicating a slightly steeper H-Q slope than predicted (this will
be discussed more fully at a later point). However, as speed increases, the
test data deviate more from the predicted curve, falling short of the curve at
the higher flowrates. This type of deviation is typical of that experienced
when cavitation is limiting the performance. To investigate :his deviation,
the ratio (Its) of the test head rise divided by the predicted head rise was
calculated and plotted as a function of suction specific speed (Nss) in Fig.
12_ The initial plot tended to indicate a great deal of data scatter without
clear trend. Hoover, when different symbols were used to represent the di_-
ferent inlet flow coefficients (_tn) tested, the data showed a clear trend.
For all coefficients, there is a tendency of the head ratio to drop as Nss
increases. However, as flow coefficient Inereasas, thls dropoff occurs at
8uceeaslvely lower values of Nee. To illustrate thl8 trend, the data of Fig.
127 are repeated in Fi8.128, with curves drawn to represent the various flow
coefficient rsnpa tabulated. This trend again is strongly indicative of
0
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i _Slll OV3H O]131O]lld/3_lN 3V_lH IS]J.
202
.I I ! I[ i
/
!
The cavitation appears to occur at much lower values of Nss than would be ex-
pected from the design, considering it does have an inducer designed for good
suction performance. This would indicate the more likely possibility that the I_
impeller is cavitating rather than the inducer. This could be caused by_ V
3. Too much hot cryogenic being pumped into the impeller eye from the _"
balance plston/bearlng area
Arguments will be presented later that there is not a large amount of balance
piston flow being returned to the impeller eye. With low circulation, the fluid
may be heating up significantly and returning to the impeller eye at much higher
temperature than expected. To further define the source of the problem, two
further steps of data analysis were attempted:
i. A theoretical inducer head rise curve was used to esti_mte the inducer
performance. This inducer head was added to the inlet NPSH to permit
ralculation of the impeller NPSH and Nss. (It was assumed in chess
c_Iculations that there is no fluid entering at the impeller eye
except the inducer flow, and that the fluid vapor pressure at the
imoeller inlet was identical to that upstream of the inducer.)
2. The noncavitating head rise was assumed to be steeper than the pre-
dicted noncavitating head. The test data at low speed were used to
estimate this new head rise curve, which is shown in Fig. 129.
Figure 130 shows the impeller suction specific speed calculated by the procedure
discussed in item (i) above. The data follow a trend typical of cavitation
performance. At lower flow coefficients, the data are relatively flat until an
Nss of i.I rad/s (m3/s)i/2/(j/_g) 3/4 3000 rpm'gpml/2/ft3/4 is reached where the
head starts to drop. At hi_her flow coefficients, the head begins to drop at
lower Nso values, approximately i.I rad/s (m3/s)172/(J/kg) 3/4 2200 rpm'gpml/2/
ft
3/4. _Note that an expanded scale is used in Fig. 130 for the abscissa.)
These are relatively low values, but if there is much heat added to the flow
by the return flow from the front wear ring and from the balance piston area,
the actual Nss for each of these points could be significantly higher. However,
it must be admitted that one of the key potential technology Droblema associated
with such small-scale hardware is that of achieving a good suction performance.
The results of the procedure outlined in item (2) above are shown in Fig. 131.
The approach tended to bring together the data at the lower values of Nss as
expected, but the data fall on a sloping line rather than a horizontal line.
In fact, the trend of the data is so contrary to the expected trend (as was
observed in Fig. 130) that it is concluded that the head rise curve presented
204
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205
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207
in Fig. 129 does not properly reflect the noncavitating head. In all further :_
calculations, the origina] pledicted head rise is used for the theoretical
value.
Figure 132 the first of the four figures, presents the static pressure rise
across the impeller and inducer. (There was no static pressure measurement
made at the inducer discharge.) The data show the same general trends as the
head rise data (Fig. 126); there are some cases, however, where the impeller
static pressure rise is higher than design, but the pump head is lower and
vlce-versa. The data of Fig. 132 actually have more spread than the data of
Fig. 126, considering the difference in the scales of the ordinates in the two
figures. The data definitely tend to indicate that there is insufficient head
being generated by the Inducer-lmpeller combinatloD.
Figurel33presents the static pressure rise across the vaned diffuser. These
data indicate a different potential problem. At low flows the proper diffusion
appears to be achieved but, as flow increases, th_ diffuser performance proMres-
slvely degrades. This is indicative of a diffuser _nismatch which could be caused
t
208
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212
by either a flow angle mismatch at the leading edge, or a flow passage that is
too small to pass the flow. The latter appears to be more likely in view of
the fact that, for lower-speed data at the real high flows and the real low
flows, the impeller pressure rise was in fair agreement with prediction (Fig.
132J, yet the diffuser pressure rise is continually dropping as flow increases.
_gain, this is a typical problem experienced with very small pumps _n that _P
boundary layer blockage or blockage due to fabrication mismatch or secondary-
i flow effects can so easily represent a much larger percentage of the through-
flow area than is normally experienced in larger pumps.
Figure 134 presents the pressure recovery through the volute and indicates a
larger amount of data scatter, but the data art :ver_here equal to or above
the design value. Figure 135 is a composite of Fig. 133 andl34, and represents
the static pressure rise across the total diffusion system frcm impeller dis-
charge to pump discharge. This composite shows the same trenas as would be
expected based on the trends and relative amplitudes of Fig. 133 and 134.
Pump Efficiency. The data reduction program was written to calculate the
pump efficiency by assuming a known turbine efficiency based on calibration
results (p_esented in the turbine section) and backing out the pump efficiency
from the machine efficiency. This machine efficiency is calculated from test
data as the pump dellvered horsepower divided by the turbine inlet available
energy. The pump efficiency obtained by this procedure is shown in Fig. 136.
As can be readily be seen, this calculated efficiency shows very poor agreement
with the predicted efficiency, especially at the higher flow coefficients; how-
ever, the higher flow coefficient data were obtained from lower-speed tests
where the results would be much more susceptible to data inaccuracies. The data
are all below the predicted efficiency line even though the head rise did in
" some cases meet its head objective.
Many of the test slices at higher speeds had a sufficient temperature rise
across the pump to permit a calculation of the isentropic efficiency. This cal-
culation has the advantage of using only test data from the pump, specifically
pump inlet and discharge pressures and temperatures. These temperatures are
much mor_ reliable than the turbine temperatures, but the temperature differen-
tials must be large enough to minimize instrumentation inaccuracy. The data
slices with temperature rise of ii to 17 K (20 to 30 F) were used, and the
results are presented in Fig. 13% The data show better efficiency than those
calculated from the machine efficiency. These results also would appear much
more reasonable in that they are more consistent with the performance degrada-
tion noted in the pump head. A_ such, the isentropic efficiency data are con-
sidered to be the most representative, and show the pump running generally about
5 to i0 points low at the lower flow coefficients, the actual amount, however,
being rather strongly dependent on flow coefficient.
213
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The balance piston is double aLting in the sense that both the high- and low-
pressure orifices are sensitive to axial position. A sketch of the balance piston
is shown in Fig, 138. Since operation in LO 2 prohibits _ny significant metal-to- _'
metal contact of rotating and stationary parts, the balance piston is designed to
have a radial gap , • both orifices at all times. These _aps are a fenction of
speed and, based on calculations from the Stress Dee_rtment, _hey the relationships:
where N is pump speed in rpm, These gaps must be kept as small as practical to
avoid a rubbing problem because the axial thrust range is signific_itly decreased
if these gaps are allowed to be too large. Review of the hardware after the rom-
plete test series indicated no rubbing occurred in the balance piston area.
The pressure drop across the total balance piston consists of three individual
pressure drops:
Dur_mg the Mark 48-0 testing, the following static pressure measurements were
made:
216
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_t
217 i
l I ! ] I I i
J
The balance piston force was calculated for the full range of the axial travel
[i.e., from 0.0 to 0.25 mm, (0.010 inch) gap on the high-pressure orifice], and
the axial position at which the measured balance cavity pressure was matched
was determined. Because of the time consumption involved in obtaining solutions
for a given data slice, five data slices were analyzed which are representative
of the testing performed.
The ratio X/6 of high-pressure orifice gap (X) to total balance piston travel (6)
for these cases varied from 0.212 to 0.353. These five cases are summarized in
Table 22 showing also the total thrust range. In addition, Table 22 shows the
_hrust at the point of match, and defines and presents the range factor which
varies from 0.52 to 0.78.
Figure 141presents the thrust range as a function of the pump speed for the cases
presented in Table 22. Assuming that the pump pressures vary essentially with
speed squared, the thrust range also should v_ry close to speed squared. (This
is an approximation because pump Inlet pressure does not vary with speed
and the radial gaps of the balance piston are closing with speed, which makes
the balance piston more effective at higher speeds.) Lines are drawn on Fig. 141
at a slope of ? to 1 to represent a speed squared relationshi,_. The parameter
KT is defined in Fig. 141, and four of the cases vary from 81 to 112% of the
design value of this parameter. Case 17-8 is found to be 68% of KT design.
Case 17-8 has an internal recirculation hole and no overboard bleed. It was found
during the analysis that the flow in the recirculation passage in this case becomes
a two-phase flow with very low density. This causes a higher back pressure in the
balance piston sump and, therefore, poorer balance piston performance.
,i
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219
,. I I i l l_ ,.
-6
#
TABLE 22. HARK 48-0 BALANCE PISTON PARAMETERS
®
(_) Thrust at
Speed Thrust Range Hatch Point O Q
Range X/6 at _p_
Test No.. rad/s rpm kN pounds kN pounds Factor Hatch Point y
14-8 2738 26157 4.4 984 10.6 2394 0.78 0.353
As a general assessment, it can be said that this test series showed the balance
piston to _e operating in a satisfactory manner, particularly on those tests
where part of the flow was b_ed overboard and, thereby, the return cavity pres-
sure was reduced. To improve the margln In an internal reclrculatlon mode, the
size of the return flow passages should be enlarged.
Bearing Coolant Flow. Examination of the bearings posttest showed that the
bearings had been overheated. There are two possible explanations:
• I t
" I 221
" I
i
I
I
i¢ Regardless of the LN 2 operation, however, there are indications that the I_ 2 flow
i through the bearings could be substantially less than was desired and that the
temperature of the coolant was potentially higher than expected. The data _
'F have already been used to show that the balance piston thrust range in some cases Y
! was less than the design range. This limitation was attributed to the higher
resistance downstream of the balance piston sump. This same high resistance
tends to restrict the coolant flow.
;• The overheating condition would be made worse by the possible larger loads ,=.
carried by the bearing due to the inability of the balance piston to develop
_; the thrust range desired in some instances. The load tracks on the bearings
were wider than usual, indicating variable loading conditions.
The thizd factoc affecting the bearing temperatures is the temperature of the
coolant fluJd itself in and around the bearings. Figure 142 shows the temperature
in the balance piston return flow area as a function of speed. Many of the
temperatures experienced are actually warmer than any encountered previously with
LO 2 bearings. It is desirable to keep the temperature down to approximately ii0 K
(200 R). The data in Fig. 142 show temperatures as high as 160 K (290 R) at
speeds of 60,000 rpm. The higher temperatures noted on the earlier tests were a
cause of concern that led to the action of opening an instrumentation line as an
overboard bleed of the balance piston flow return cavity. This rhange was made "
effective on test 19 and subsequent and, even though the return port was small,
the data of Fig.142show that there was a definite tendency to lower the tempera-
ture in this cavity. Subsequent tests were able to get to speeds of 7330 rad/s
(70,000 rpm) or higher without exceeding approximately 130 K (235 R). Thus, the
overheating inlti_lly must be at least partially due to insufficient coolant flow-
rate out of this cavity area. Thls same problem leads to a higher back pressure at
the balance piston sump, and results in the lower thrust range previously reported.
Further analyses to explore the coolant flow problem should be cor,ducted. These
analyses can be expected to cover the effects of the heating due to power disk
drag on the back side of the impeller and on the slinger. Preliminary analyses
indicate that, at 7330 rad/s (70,000 rpm), the impeller back side power dlsk drag
could easily result in a temperature increase of 17 K (30 R), wlth the flows calcu-
lated in analyzing the balance piston performance. Thls could explain the tem-
peratures observed during tests.
, 223 •
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Turbine Performance. Turbine test data for the performance analysis were obtained
with instrumentation located as follows:
Tests ii through 18 were conducted with GH 2 turbine working fluid, and tests 19
through 28 utilized LO2/LH 2 preburner combustion products to drive the turbine.
For the initial tests, ii through 13, liquid nitrogen was used in the pump, while
tests 14 through 28 were run with LO 2 in the pump.
The turbine was tested as an individual component at the Wyle Laboratories for
purposes of calibration. These calibration tests were performed with better
instrumentation and test operating condition control than is achievable in the
turbopump tests. The testing and results from the calibration secies have been
discussed previously, and the data from those tests are consiaered to be the
best data for defining turbine efficiency. However, the data from the turbopump
tests were used In a twofold manner:
Data from test 24-1 are used as a sample case in the discussions dealing with data
reduction procedure and turbine demonstrated performance, because it is the LO2/
LH 2 turbine test with the velocity ratio closest to that of the turbine design
(0.345).
i •
i 225
i I [ I ! .....
I I I I
Turbine rest efficiency is calculated with the following analysis proced_le based
on turbopump tests:
At the outset of the turbine analysis, the turbine inlet pressure is adjusted for
an estimated 2% pressure loss. The fluid loss starts at the station where the
total inlet pressure is measured, and is sustained for the flow distance up to
the nozzle entrance plane. The loss assigned to this calculation is based on
experience with similar design turbine installations, manifolds, _ud working
fluids, and is charged to the engine system in a staged combustion cycle. Turbine
inlet tot_l enthalpy is calculated at the entrance to the nozzle. Thus,
415.9
n T/P machine = 1476.6 = 0.2817
The calculated turbopump machine efficiency versus turbine velocity ratio plot is
presented in Fig. 143; the performance data are representative of test speeds
ranging from 1623 to 7768 rad/s (15,500 to 74,191 rpm). All the data are below
the predicted machine efficiency curves, which was to be expected based on the
low pump efficiencies presented in the previous section.
A check of turbopump test data near the turbine design velocity ratio (Um/C o -
0.345) indicates th_ machine efficiency varies from 0.272 to 0.333; this :represents
an approximate ±10% maximum variation from the average machine efficiency of 0.300.
Figure 144 presents the turbine efficiency calculated by dividing the machine
efficiency (Fig. 143) by the pump isentropic efficiency (Fig. 137). The data
bracket the calibration curve, but show a definite trend of variation with turbine
velocity ratio. At the extreme values of U/Co, the datasm off by 10 efficiency
i points, being 10 points high at high U/C o and 10 points low at the other end.
226
|
J I_ I Ill _ , ! .............. I P ! ...... I
I I i I I
0"060 O.| O.2 0.3 0.4 0.5
TURBINE VELOCITY RATIO, U/CO (TOTAL TO STATIC)
227
o.7
_o.5 0
o 0.4
O_ CALIBRATION
oC_o PERFOR_NCE
z
_w 0°3
uw
TURBINE EFFICIENCY
0.2 CALCULATEDFROR_CHINE
EFFICIENCY AND PUHP
ISENTROPICEFFICIENCY
ml II J
o0 I 1 I I
0.1 0.2 0.3 0.4 0.5
'' i 228
b
Such scatter in turbine efficiency based on the available data is not surprising
and, in fact, is the very reason that a more carefully controlled turbine calibra-
tion effort was conducted prior to the turbopump testing.
The precision of turbine pressure, temperature, working fluid mass flow, and speed
test data affect test results. The plots in Fig. 145 and 146 were made to illus-
trate quantitatively how turbine inlet temperature and turbine presaure ratio
influence turbine performance. With the turbine test parameters from test 24-1
as a reference (and using as an example a calculated turbine efficiency rather than
the calibration value), the turbine inlet temperature and pressure ratio were
perturbated, i.e., temperature from 814 to 926 K (1467 to 1667 R) and pressure
ratio from 1.587 to 1.880 total to static. Estimates of how these data shifts,
due to instrumentation error or other causes, can affect turbine perfornmnce calcu-
lations are tabulated below and plotted in Fig. 145 and 146.
Efficiency Change
Variable Percent Change (Points)
No allowance has been made for the precision of the speed and turbine inlet pres-
sure data.
Another factor which influenced the turbine performance is the turbine mass flow-
rate data. For these tests, the total LO2/LH 2 turbine Wt was established with
four separate oxidizer and fuel venturi meters (LO2 and LH 2 flow at the preburner,
and GO2-GH 2 flow to the igniter); mass-flow was calculated ith flow coefficients
at the respective flow stations. Furthermore, problems were experienced with the
venturl measurements on several tests, which necessitated calculating flowrates
by secondary means. Therefore, if all the above factors are taken into considera-
tion (pump efficiency, instrumentation error, and mass flow precision), th_
efficiency data point scatter in Fig. 143 and 144 can be readily understood.
A comparison of turbopump test results with turbine calibration data shows that
the turbine efficiency is scattered about the turbine calibration data, thereby
indicating some substantiation. It should be noted that calibration data were
obtained under conditions more suitable to higher precision and, therefore, the
turbine efficiency obtained from the callbration tests should be considered most I
t
229
1.587 --_.
0.54 -
0._ 0.50 -
o
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1.746
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TEST 24-1
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INLET
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i.l I
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I i ! I
Several tests were terminated by the vibration sensor device monitoring the out-
put of the accelerometers attached to the turbopump housing. This was caused
by a combination of several factors. Normally on a new turbopump several tests
are required to establish its vibration signature and thus set the cutoff point
at the appropriate levels. It appears that with the Mark 48-0 turbopump, this
level is in the 20 to 25 g rms range in conjunction with a 2K Hz low-pass filter.
Some of the early runs were terminated because the cutoff redline was set too
low. In addition, the manual GN 2 feed coatrol system employed on the first seven
runs frequently resulted in slow transition through critical speed zones, with
attendant buildup in vibration levels.
Bently data and accelerometer data obtained from high-frequency tapes showed
increased synchronous activity at 4115, 5026, and 5528 rad/s (39,300, 48,000, and
52,800 rpm). These compared favorable with the analytically predicted critical
speeds of 4723 and 5482 rad/s (45,108 and 52,363 rpm), respectively. No evidence
of subsynchronous vibration was present in the data.
The measured seal drain pressures, temperatures, and flowrates were, in general,
in good agreement with predicted values, indicating proper functioning of the
shaft seals. During chilldown of the pump on the LN2 tests, it was noted that
the secondary hot-gas drain line frosted ever. This could occur as a result of
heat transfer through conduction, but possibly also as a result of the pump fluid
from the primary L02 seal drain cavity leaking across the intermediate seal. To
prevent a potentially hazardou§ condition, the purge pressure level in the inter-
mediate seal was raised to 138 N/cm 2 (200 psig). No problem was experienced at
: this pressure level with mixing of incompatible fluids. It is quite possible
that the originally planned purge pressure of 41 N/cm 2 (60 psig) would be
adequate. This could be established on future tests by sampling and analyzing
the drain fluids during chilldown.
The turbopump was disassembled after the test series to permit visual inspection
of the components. Figure 147show the condition of the more significant parts.
The condition of most of the components was excellent; only two discrepancies
were apparent: The pump-end bearings showed evidence of overheating, and the
chrome plating on the rotor under the primary hot-gas seal ring flaked off.
Figurel48 shows the condition of the inducer and impeller: neither part had any
adverse after effects from the testing. As experienced, superficial rubbing
contact took place at the tips of the inducer vanes and at the impeller front
shroud labyrinths. In Fig.149the impeller and the diffuser are included to
232
ORIGINALPAGI_IS
OF POOR QUALITY 233
.
: ' I I
ORIGINALPAGBl_ 235
_IV'POOR QUAIa_
I.
illustrate the condition of the balance piston low-pressure orifice elements as
well as the stationary land of the hlgh-pressure orifice. There was no sign of
contact at either orifice.
Components of the rotating assembly and the shaft dynamic seals are shown in
Fig. 150 and 151, respectively. The only discrepancy noted on the seals was a
slight roughness on the inner diameter of the turblne-slde ring of the primary
hot-gas seal, under which the chrome plate flaking occurred. Figure 152 illustrates
the appearance of the sealing surfaces on the rotor. The surfaces under the
primary LO 2 seal and intermediate seal rings are in excellent condition. On the
other hand, some of the chrome plating flaked off under the primary hot-gas seal
rings. Difficulty has been experienced during fabrication of the rotor in obtain-
ing a sound plating in this area, but it is anticipated that, with more stringent
quality control and engineering surveillance over the process, a satisfactory
i plating can be achieved.
The turblne-end and pump-end bearings are shown in Fig. 153 and 154, respectively.
The condition of the turblne-end bearings was excellent. There was no evidence
of overheating or excessive loading. In contrast, the balls of the pump-end
bearings were discolored and a piece spalled from one of the balls. The cage
pocket which contained the spalled ball was worn. Wear tracks on the races indi-
cated high and varying load levels. _,e overheating is attributed to insufficient
coolant flow caused by high resistance in the balance piston return flow passages.
(See discussion under Pump Hydrodynamic Performance).
The remaining components, including the pump and turbine housings and supports,
were in excellent condition. There was no sign of structural failure, excessive
deflection, or other deterioration.
236
/ ORIGINA_ PAGE IS
'- OF POOR QUALITY
I
_ I
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, i
!"............
F...........T f i '
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J _ _ 1 . I t i I
ORI(_INAI;PAeg IS
; 2_0 OE 900R QUALITY
i
APPENDIX A
DESIGN GROUND
RULES
ii
i
/
APPENDIXA
DESIGN GROUNDRULES
Fe
Allowable Alternating
Fe _ • Stress Line
• .
¢#'j ""_-.._.... f _."
Lower/f Ftu
or 1.1
243
APPENDIXA (CO_T'D)
/
!mpcller
Impeller burst speed shall be at least 20_ above the maximum oper-
ating speed.
Disk burst speed shall be at least 20Z above the maximum operstin$
speed.
"_ 244
J i t
L I I i :¢. I } i J
_ APPENDIXA (CONT'D)
- 4
.!
| Disk maximum ef[ective stress at 5_ above the maximum operating
i speed shall not exceed the allowable .2% yield stress. (Does not
apply to areas in which local yielding is permitted).
"! Beartn_
Material:
Seals
LO___2 H2+I{2_____O
Critical Spegd
Rotor bending frequency shall be at least 25% above the rotor maximum
operating speed.
245
r
APPENDIX B
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I f
ab.
APPENDIX D
;- REFERENCES
I
REFERENCES
5. Cordes, G. : Fluid Mechanics of the Axial Flow Gas Turbine, With Special
Consld_ratlon of the Jet Engine Turbine, Springer-Veriag, Berlin, 1963.
6. Horlock, J. H.: Axial Flow Turbines, Butterworth & Co., Ltd. ¢London), 1966.
279
I
1 _, _ I_ I
/
APPENDIX E
DISTRIBUTION LIST