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Vibration - Case Study On Resolving Bearing Oil Whirl

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CASE STUDY ON RESOLVING

OIL WHIRL ISSUES


ON GAS COMPRESSOR

John J. Yu, Ph.D.


Nicolas Péton
Sergey Drygin, Ph.D.

GE Oil & Gas

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May 23, 2017
Abstract

• This case is a site vibration issue on a Gas compressor module.


When machine was running at partial load condition, vibration at
compressor DE and NDE bearings suddenly increased and tripped
the machine.
• This case study outlines how the high vibration issue was
successfully diagnosed using shaft relative vibration data.
• The high vibration of 346 um pp (14 mil pp), higher than nominal
bearing clearances, was due to subsynchronous 0.37X component
forward precession. Significant shaft centerline thermal influence
was detected.
• Oil Whirl condition, was diagnosed at compressor bearings.
• Bearing modification was suggested to the OEM. Length/Diameter
bearings ratio was decreased by pads machining from both sides.
Follow-up tests after bearing modification confirmed no vibration
issue afterwards at any load condition.

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May 23, 2017
Machine Information
Machine Overview

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May 23, 2017
Machine Information
Compressor Mechanical Data
Motor Speed : 1497 rpm
Compressor Speed : 5877 rpm
Compressor 1st Lateral Critical Speed : 2786 rpm
Compressor 2nd Lateral Critical Speed : 9042 rpm
Rotating Direction View from Drive End : Clockwise
Shaft Seal Type : Labyrinth
DE Bearing Clearance : 0.250-0.293 mm
NDE Bearing Clearance : 0.190-0.233 mm
Compressor Bearing Type : Plane Sleeve
Balance Piston Seal Clearance : 0.85-1.07 mm
Design Operating Condition:
Flow Rate : 168685 m3/h (224144 kg/h)
Suction Pressure : 0.99 Bar abs.
Suction Temperature : 35 deg C
Discharge Pressure : 3.063 Bar abs
Discharge Temperature : 169 deg C
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May 23, 2017
Design Operating Curve

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May 23, 2017
Problem Description
Machine Trend Diagram

Air
Compressor

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May 23, 2017
Background
When machine was running at partial load condition,
vibration at compressor DE and NDE suddenly increased
and tripped machine.

Example condition before the first tripped on 29th Dec 2015


• Discharge pressure : 0.86 Barg
• Air Flow Rate : about 182000 kg/hour
• Discharge Temperature : about 125 deg C
• Suction Temperature : about 33 deg C

Example condition before the first tripped on 15th January 2016


(after realignment)
• Discharge pressure : 1.14 Barg
• Air Flow Rate : about 287000 kg/hour
• Discharge Temperature : about 152 deg C
• Suction Temperature : about 33 deg C

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May 23, 2017
Process condition during trip events
Machine tripped at different operating conditions.

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May 23, 2017
Shaft Speed Trend

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May 23, 2017
Compressor Overall Vibration (Abnormal)

4 Diagnosis Fixed
1
3 5
2

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May 23, 2017
Gearbox Overall Vibration (Normal)

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May 23, 2017
Data Analysis
Overview

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May 23, 2017
Shaft Speed vs. Vibration Amplitude Trends: Vibration suddenly increased

Shaft Speed

Overall Vibration Amplitude


Vibration suddenly
increase and trip the
machine

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May 23, 2017
Vibration Amplitude: Higher than bearing Clearance (>293 um)

346 um pp
5th December 2015

Bearing
Clearance
= 293 um pp

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May 23, 2017
Vibration Spectrum: 0.371X Dominant

Forward 0.371X
2175 cpm

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May 23, 2017
Dynamic Shaft Movement (Orbit): Big, Elliptic, Forward Precession

Non Drive End Bearing

Drive End Bearing

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May 23, 2017
DE and NDE orbits: In-Phase

DE

NDE

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May 23, 2017
Average Shaft Centerline : Significantly Different btw Cold and Hot Condition

Startup from 233 rpm Coast down to 233 rpm

Cold Condition

Hot Condition

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May 23, 2017
X probe
Y probe

Air Temperature
increased (load up) Lube oil temperature
increased

Tripped

Run-up

Coast down

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May 23, 2017
Diagnostics Summary
Vibration Information Summary

Amplitude : More than Bearing Clearance (293 um)


Dominant Frequency : 0.37X (2175 cpm) (< 1st Res Freq.)
nX Vector : 0.37X, DE and NDE are in-Phase.
Shaft Position : Near Bearing Center
Orbit Shape : Slightly Elliptical Shape, Forward Precession

Fluid Induce Instability – Whirl


(most likely at DE bearing)

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May 23, 2017
Fluid Whirl/Whip

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May 23, 2017
Immediate Recommendations

1. Inspect Bearing and Seal Components

2. Check piping support, if any restriction.

3. Confirm Alignment / Correction

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May 23, 2017
First Inspection

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May 23, 2017
Piping Support inspection

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May 23, 2017
Alignment Confirmation

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May 23, 2017
Bearing Inspection

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May 23, 2017
What else to fix the problem?

Excessive Bearing Coupling Misalignment Bearing design issue


Clearance
-0.42
(-0.40)
(-0.30)

-0.33
(-0.33, fix)
+0.33 ?
DE: 0.29-0.30 mm +0.40 Needs to consult
NDE: 0.18-0.19 mm with the OEM

NO NO
After adjust
alignment, problem
still existed. 31 /
GE /
May 23, 2017
Corrective Action

A. Adjust External Alignment (btw Coupling): This would help if problem is


not severe. >> Already tried, but not successful.

B. Change Lube Oil Temperature: not permanent solution. >> system could
not further decrease oil temperature.

C. Decrease Lube Oil Flow Rate: Risk to damage other bearings.

D. Bearing Modification: must be designed and approved by machine


manufacturer.

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May 23, 2017
Bearing Design to break Circumferential
Oil Flow Pattern

Two Axial-Groove Three-Lobe Elliptical


Pad
Center

Offset Cylindrical Tilting Pad Pressure Dam


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May 23, 2017
Solution
Bearing modification (suggested by OEM)

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May 23, 2017
After bearing modification
Speed Trend

Normal shutdown
Startup
then Re-startup

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May 23, 2017
After bearing modification (Cont.)
Vibration Amplitude, 25 um pp (1 mil pp)

25 um pp maximum at NDE bearing

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May 23, 2017
After bearing modification (Cont.)
Frequency, 1X dominant (normal)

5887 CPM (= 1X)

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May 23, 2017
After bearing modification (Cont.)
Orbit plots shows normal dynamic shaft movement

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May 23, 2017
After bearing modification (Cont.)

Shaft Cold Startup


Centerline
Hot Shutdown

Warm Startup

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May 23, 2017
Discussions
• Oil whirl frequency tracks with speed, usually at < 0.5X (<50%
running speed frequency). If the frequency is exactly ½ X, the
instability is not oil whirl, instead it is parametric excitation
(rub contact or bearing looseness).

• Oil whip frequency locks into one of the natural frequencies of


rotor-bearing system, usually the lowest . As speed goes up,
the frequency remains unchanged.

• Subsynchronous vibration could also be caused by


aerodynamic instability such as stall or surge in compressors.

• Oil whirl/whip is affected by speed, bearing types and design,


lube oil temperature and supply pressure, while aerodynamic
instability in compressors is affected by flow condition.
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May 23, 2017
The End

Thank You

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May 23, 2017

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