Report On Oil Ingress Problem in Generator
Report On Oil Ingress Problem in Generator
Report On Oil Ingress Problem in Generator
Fig-01
13. Slope of H2 side oil drain line from generator TE and EE pre chamber to IOT was found
more than sufficient. As per drawing it should be 40 mm per meter.
14. The line size of H2 side oil drain line from pre chamber to U-loop was found NB 50
which is as per drawing no. 0-150-00-01648 (sheet1/5) and also as per BOM (TGE-3256,
Rev 02 dtd 04.05.2015) the material supplied is of size NB 50 and after U-loop to IOT the
line size was found NB 80.
On enquiry for the line size of H2 drain line from Generator pre chamber to U-loop
with same rating set like Lalitpur and Bara, it was found that their having H2 drain
line size NB 80 and our H2 side drain line size NB50,which was found different.
Therefore it was concluded that due to H2 side drain line size NB 50 oil got ingress
in Generator as DC SOP also got picked up due to malfunction of VOT level switch
and due to running of both AC & DC SOP seal oil flow got high as seal oil DP
maintained high which could not be accommodated in H2 side drain line size NB 50
causing oil ingress in generator.
As Generator TE H2 side drain line length up to U-loop was much more than that of
EE as compared therefore LLDR first alarm triggered in TE during oil ingress and
then EE.
Action taken:
1. Problem reported to the Hardwar unit for their concurrence for modification of TE
and EE H2 side drain lines up to U-loop. Unit has given concurrence for the same.
After obtaining concurrence from Unit both TE and EE H2 side drain line size from
generator pre chamber to U-loop has been modified from NB 50 to NB 80.
2. Both generator TE and EE H2 side modified drain lines from pre chamber to U-loop,
cleaning was done by air blowing/blasting method as flushing was not possible.
3. VOT make up float valve stuck problem was attended by increasing the length of
guide sleeve by 30 mm (Fig02). Make up float valve re-assembled after its siting
surface proper cleaning/servicing and kerosene test. After re-assembly of float valve
checked for its operation by charging oil to VOT. Afterwards no oil passing was
observed in VOT through float valve and also oil level in VOT gets maintained at 160
mm.
Fig02
4. All the 04 nos. metal type flow-meters installed in seal oil skid rack for measuring
seal oil flow to Generator in TE and EE lines were serviced and calibrated.
5. A temporary mesh put in H2 side drain to IOT inlet line near IOT, to arrest any
foreign particles during initial operation of seal oil system and to be remove before
system put in regular operation.
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