5182-Article Text-9953-1-10-20210109
5182-Article Text-9953-1-10-20210109
5182-Article Text-9953-1-10-20210109
E, 17 (6) (2020)
1
S. Salmi, 2 A.A. Nuraini
1
Department of Mechanical and Manufacturing, Universiti Putra Malaysia, Serdang, Selangor,
2
Department of Mechanical and Manufacturing, Universiti Putra Malaysia, Serdang, Selangor
Email: 1 nasmiesan@gmail.com, 2 nuraini@upm.edu.my
S. Salmi, A.A. Nuraini: Effect of Coal with High Moisture Content on Boiler Operation
Parameters at Thermal Coal Fired Power Plant -- Palarch’s Journal Of Archaeology Of
Egypt/Egyptology 17(9). ISSN 1567-214x
Keywords: Coal, Thermal Coal Plant, Boiler Operation, Pulveriser.
ABSTRACT
Focus on developing county, the electricity industry plays important roles. In fact, energy
drives the national growth in supporting the other industries. Most developing country produce
electrical energy through thermal coal plant and is recorded above 70 percent of total Asian
capacity. Coal is still a choice as the main fuel in thermal coal plant due to cheaper price
compared to another type of fuel, distillate or gas. However, coal performance is uncertain due to
the different characteristics and coal types. Coal must be tested and analyzed before fired into the
boiler. Problematic coal may cause issued to the boiler furnace such as ash slagging and fouling,
ash corrosion, tube leak, and consequently impacts to the boiler efficiency. Therefore, this study
purposely to investigate the effects of sticky coal on the boiler operation parameters. The study
found boiler pressure deviation was fluctuated badly to minus 25bar, coal flowrate was decreased
to minus 5 tonnes per hour during firing coal with high moisture content. By looking at
pulverizer parameters, mill different pressure at bowl was decreasing, mill motor current was
increased about 5 Amps and primary air to carry the pulverized fuel increased accordingly. From
this study, the main factor of sticky coal is due to high moisture contents. Hence, to minimize the
high moisture contents, coal not recommended to remain in the yard for a long time.
1. Introduction
Thermal energy in Asia remains a major electricity source, with coal-fired
power plants in China alone generating almost 75 percent of electricity.
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
condition for combustion to take place in the boiler combustion chamber [4]
[21]. Therefore, heat energy is released to convert the boiler water into
superheated steam for electricity generation [11].
thermal Coal fired power plant
The power plant designed to produced 700MWn, installed with boilers are of
sub-critical pressure, single reheat and controlled circulation type [9]. This
boiler is fired with pulverised coal to produce steam for the continuous
generation of 700 megawatts (MW). The boilers are designed to fire coals
within the bituminous rank. The combustion circuit consists of a single furnace,
with direct tangential firing and a balanced draught system [4] [17].
The firing equipment consists of four elevations with 16 burners, remote-
controlled fuel oil burners equipped with high energy ignitors, used to start-up
the boiler and to support combustion of the pulverised coal at low firing rates.
Boiler Maximum Continuous Rate (BMCR) was designed 40 percent of an oil
burner, seven elevations of pulveriser with a total of 28 coal burners located
just above or below a fuel oil burner [4], [15]. The capacity of coal burners is
100% BMCR when firing coal within the design range. All the burners are
located in the furnace corners with designed as tangential firing. Figure 1
shows the two-pass drum types opposed-fired boiler with a single back pass
thermal coal plant.
Fig I: Two pass drum types opposed-fired boiler with single back pass
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
10 percent. At full capacity of the BMCR, the total combustion air flow for this
power plant is 2120kNm3/hrs and total primary airflow required for mill to
transport the pulveriser fuel is about 570kNm3/hrs [16].
For this coal plant, was installed with 7 vertical bowl pulveriser or called as
mills [4]. The firing equipment consists of seven elevations with 28 coal
burners located just above or below a fuel oil burner. The capacity of coal
burners is 100 % BMCR when firing coal within the design range. The
pulverizes and burners system provides pulverized coal to the boiler as primary
fuel. Coal enters the plant from the coal handling system where it has been
crushed to consistent sizes where it can be handled by the pulverizes [8], [22].
It is delivered to the coal bunkers which are located directly above their
respective pulverizes, also called mills. Hot and cold primary air is used to
maintain the pulverized coal temperature. The air enters the pulveriser through
nozzles in the air pot ring, which surrounds the grinding table to dry and
transport.
2. PROBLEM STATMENT
Industries are going to face critical demand when there are restrictions on coal
stock, limited coal with good quality. Hence, as a preparation for future needs,
the firing of distinct types of coal need to be studied as it will give an impact on
the boiler parameters. It is crucial to conduct the study especially when the coal
is not meet the designed boiler operation in the thermal plant. This is because
the effect on boiler performance will give an impact on boiler performance
efficiency.
3. METHADOLOGY
Coal specification, 2 types of coal with different characteristic was used for this
study. Coal types A is a preferred coal which means coal was fired during
commissioning of this plant. During commissioning period, the boiler
operation parameters was recorded as benchmarked and operated to meet the
coal specification and characteristic [7], [11]. Coal types B, alternative coal
with different coal specification was introduced to this power plant. Alternative
coal was fired for 5 days as trial burn period to measure and indicate the
impacts at the boiler operation parameters.
Table I: Sub bituminous coal specification for coal type A and coal type B
Coal Unit Coal Coal
Specification Type A Type B
Calorific value kcal/kg 4852 5113
Carbon % 74.30 74.13
Hydrogen % 4.97 5.42
Nitrogen % 0.91 1.49
Oxygen % 19.67 18.33
Ash % 2.50 6.20
Moisture % 28.4 23.4
Sulphur % 0.10 0.45
HGI Number 47 43
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
The coal analysis was carried out at the coal supplier laboratory. For the coal
quality, the measurement was carried out through proximate analysis and
ultimate analysis [4], [6]. During the trial burn period, boiler is fired with the
same coal for 3 days continuously without any interruption. Data were
collected using the numerical plant performance data. Average of the
parameters was firmly keep recorded.
During unloading coal process, visual inspection was carried out at coal yard.
Coal was unloading from shipment to coal stock yard. Before transport to the
coal bunker for firing, sample of coal was taken to verify the coal characteristic
[10], [11]. Analysis of coal was performing and compared with the existing
Coal of Analysis (COA) delivered from the supplier. There is no issues and
problem accrued during handling coal types A. From visual observation at coal
yard for coal types B, there is no significant issues on handling this types of
coal as well. Indeed, coal handles properly and there are no incidents of belt
skewing due to coal sticking to the belts. Several incidences of self-heating
were observed and no significant slumping observed. However, there were 2
incident of mill chute block was reported. Figure II shows the stacker and
reclaimer at coal stock yard attached at this plant. Figure III shows the coal at
conveyor line transport from the coal yard to the coal bunker.
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
Table II: Boiler operation parameters recorded during trial burn period for coal
type A and coal type B.
Operatio Un Coal Type Coal Type
n it A B
Paramet Da 1 2 3 4 5 6
ers y
Measure Me 7 7 7 7 7 7
d MW ga 3 3 3 3 3 3
(gross) wat 7 7 7 3 4 3
t . . . . . .
2 3 1 1 2 4
Measure Me 6 6 6 6 6 6
d MW ga 8 8 8 8 8 8
(net) wat 5 5 5 1 1 1
t . . . . . .
5 8 9 7 4 2
Boiler Bar 1 1 1 1 1 1
actual 8 8 8 8 8 8
pressure 5 6 6 8 7 8
Boiler Bar 1 1 1 1 1 1
sliding 8 8 8 8 8 8
pressure 6 6 7 5 5 5
Boiler Bar 0 0 0 - - -
pressure . . . 3 2 2
deviatio 1 2 2 . . .
n 1 6 8
Steam ˚C 5 5 5 5 5 5
superhea 4 4 4 3 3 4
ted 0 0 0 8 9 3
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
temperat . . . . . .
ure 7 2 2 4 4 1
Reheater ˚C 5 5 5 5 5 5
steam 4 3 4 3 3 4
temperat 0 9 0 8 9 3
ure . . . . . .
5 0 3 7 5 9
Superhe To 5 6 6 1 1 1
ated nne 0 5 5 1 3 2
spray /hr . . . 9 0 5
water s 1 5 9 . . .
flow 1 1 1
Reheater To 0 0 0 0 1 1
spray nne . . . . . .
water /hr 3 1 2 9 6 0
flow s
Furnace ˚C 7 7 7 7 7 7
rear path 4 4 3 8 8 6
temperat 3 1 4 1 5 1
ure . . . . . .
2 0 5 0 8 8
Flue gas ˚C 1 1 1 1 1 1
temperat 6 6 6 7 8 7
ure 5 6 9 4 0 2
. . . . . .
1 8 1 6 9 5
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
pulveriser parameters including motor amps, coal flow, and PA flow was
shows in Table III.
Table III: Average mill operating parameters with mill 10 in standby mode
Parameter Unit Coal Type A Coal Type B
Duration Day 1 2 3 4 5 6
Coal mill KW 457.1 454.8 439.0 428.6 426.2 421.0
motor
power
Mill motor Amps 86.6 92.6 89.7 84.7 84.0 82.4
current
Feeder coal Tonne/hrs 54.2 53.5 54.1 57.4 57.6 58.3
flow
Mill PA kNm3/h 101.5 101.3 101.4 106.5 109.6 107.3
corrected
inlet flow
Mill PA ˚C 273.7 265.9 255.9 289.2 305.3 286.3
inlet
temperature
During boiler operation, observed the load was disturbance between range 5-6
MW which is due to pressure deviation. Reheater temperature inlet and outlet
not meet the set target value 540 ˚C. Reheater temperature is between 520 ˚C to
530 ˚C and cause efficiency decrease. Mill coal flow about 56-58 ton/hrs which
is slightly different compared to previous coal type A about 55-53 t/hrs. Mill
motor current shows minimum impacts on motor amps but not significantly
affects to the pulverize performance in total. Figure IV shows the pulverizes
performance for the power plant on generating at steady load, 700MW.
Nominal designs for pulveriser equipment require coals with moisture content
between 8 percent and 12 percent. Each two percent of moisture increase will
reduce output by approximately 5 percent to 6 percent, up to hot air flow limit.
Once hot air capacity is reached, each two percent of moisture would result in
approximately 15 percent fall in output. Increase in the moisture content of the
fuel will cause a fall in the mill outlet temperature, which in turn will demand
that the mill inlet temperature should rise. Consequently, the hot air density is
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
reduced, and since the air/fuel ratio is a function of mass flow, the net result is
a fall in the mill output capacity.
Figure V shows some typical effects of increasing moisture on mill output
performance. The percentage of the moisture will influence the percentage of
the mill performance because of the need of more air inlet to the mill system.
More air will be required to dry the moisture content of the coal before it enters
the boiler for combustion. In fact, coal with high moisture content will give
significant impact to the combustion process.
Some Ball Tube type mills however have a “Boost Gas” arrangement, which
allows furnace bottom gas to enter the mill system in order to boost this
temperature and thus aid the drying process [2]. This type of mill has a much
greater mass of metal necessary to dissipate the heat and prevent the mixture
temperature from rising to abnormal levels, while limiting oxygen content in
the atmosphere. Therefore, the risk of spontaneous ignition is greatly reduced.
Similarly, other systems use steam, CO2 or nitrogen as inerting media, but
these are systems provided for the safety of the plant and are not to be used for
general operation of the plant. Indeed, use of these systems to control the plant
have resulted in catastrophic and dangerous mill system fires [5], [6].
Further investigation was carried out; the boiler furnace was fluctuating
between -1.0 to – 2.5 mbar. This is due to melt coal was fall down at furnace
area. Induced drought (ID) fan was responding accordingly to ensure boiler
furnace pressure at optimum level, setting at – 1 mbar. In facts, when
the pressure in combustion area of the boiler is less than atmospheric pressure
[4] [11]. This is achieved in balanced draft boilers by using Forced draft fans to
force air into boiler (pressuring it) and Induced draft fans to remove air from
the boilers to create negative pressure. Observation during firing coal type B
during trial burn period as shows in Figure VI.
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
Figure VII shows the boiler furnace rear path temperature fluctuated during
firing wet coal. Furnace rear path increase up to 780℃ compared to normal
operation value between 700-760℃. Increasing of rear path temperature
impacts to the heat transfer process at the back path of the boiler, consequently
cause high temperature at the boiler tube surface.
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Effect of Coal with High Moisture Content on Boiler Operation Parameters at Thermal Coal Fired Power Plant PJAEE, 17 (6) (2020)
The results show coal type B has high moisture content which is 32.4 percent.
The moisture value given for a proximate analysis is the moisture measured as
mass lost from a sample under specified conditions after heating in
a moisture oven to 104 to 110°C (ASTM method D3173-11 [2], [17].
Moisture absorbs heat, so high moisture content in coal reduces the relative
efficiency of heating when a coal is combusted [14]. The coal calorific value
and carbon content for coal type A and coal type B almost similar. More
volume tonnage of coal is requiring to produce full capacity of BMCR of the
boiler.
4. Conclusion
The critical moisture content at which the coal is most highly prone for
spontaneous combustion was also obtained. It was found that different ranks of
coal have different critical moisture contents [2], [19]. For lignite and
anthracite, the critical moisture content was 25% and 20%, respectively. It was
found that, for different ranks of coal, the effect of the moisture content can be
quite different and for the same rank of coal, different moisture contents will
affect the coal's performance in very different ways.
Moisture absorbs heat, so high moisture content in coal reduces the relative
efficiency of heating when coal is combusted [20], [21]. This is why low-rank,
high-moisture coals have lower calorific values (Btu/lb) than high-rank, low-
moisture coals [2]. Moisture adds weight to coal, and also contributes to
spontaneous combustion in low-rank coals. Therefore, the coal with high
moisture content impacts the boiler performance parameters and pulveriser
system as well.
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