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The Southern African Institute of Mining and Metallurgy

6th Southern African Base Metals Conference 2011


R Hawker and D O’Connor

KEEPING OPEN OF UNDERGROUND BLAST HOLES

R Hawker
Minova Australia

D O’Connor
Minova RSA

Abstract

Underground mining of base metals like copper often uses massive mining methods
such as sublevel open stoping. A feature of these mining operations is the drilling of
“rings” of blastholes, typically 60 – 120 mm in diameter and often over 15 m long. For
convenience of equipment and personnel utilisation it is common practice for a number
of “rings” to be drilled in a campaign, a long time in advance of their planned use – 12
months is not uncommon. Unfortunately in the time between drilling and charging, the
holes may be become distorted by changing stress fields or be blocked by dislodged
rocks, both potentially preventing the hole from being charged with explosives. The
blocked holes must be re-drilled at high cost and safety risk, or are abandoned, causing
poor blasting results.

Recently a system has been developed to reinforce the holes after drilling so that they
are less prone to blockage in the time before charging. The reinforcement consists of a
thin lining of tough resin that holds loosened rock fragments in place and reduces
deterioration of the hole wall. The resin is a fast-setting, two component silicate. The
two components are pumped at the required ratio to a mixer and innovative head that is
inserted in the hole and withdrawn at a controlled rate, while spraying the mixed resin
onto the rock. It sets quickly to a form a thin membrane that is strong enough to
withstand deformation and spalling of the rock.

The system has been under test on an Australian nickel mine for over year, with results
that indicate that the system is rugged, cost effective and suitable for the hole diameters
and lengths covering all those commonly found in this industry. It will soon be made
available to other users in Australia and later, in Africa.

Introduction

Many base metal mines worldwide work massive or steeply dipping orebodies that are
mined by sub-level caving, sub-level open stoping or block caving. A common feature
of these mining methods is the drilling of patterns of blastholes (schematically shown in
Figure 1), usually with diameters in the range 60 - 120 mm. The equipment to drill
holes with these diameters is large and heavy so it is preferable to drill the holes for
many successive blasts in one campaign, before the drilling equipment is moved to
another working place. As a result, holes may stand open for as long as 12 months until
they are charged with explosives. During the interim period holes fret and close or
become blocked (Figure 2) so that they cannot be charged until they are cleared.
Clearing of blocked holes is labour intensive, time consuming and dangerous so mine

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6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

operators have looked for solutions. This paper describes the development of one
method of alleviating the problem. It is currently (2011) under trial on mines in
Australia; a number of mines in Africa have expressed interest in the system.

Figure 1. Sub-level stoping mining scheme

Figure 2. Mechanisms of hole blocking

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

The problem

While newly drilled blast holes are generally strong because of their circular shape,
over time some holes partially collapse and can become blocked (Figure 3) to the
explosives charging hoses. This is exacerbated by unfavourable geology, stress and
vibration from adjacent blasting which leads to fretting of blast holes and displacement
of wedges of rock, blocking the hole. Ring drilling is more susceptible to blocking than
other blasting patterns such as benching, as off-vertical holes have a greater tendency to
become blocked. In some instances the blockages can be quickly removed by using
compressed air/water but this not always effective and usually only a little effort is
expended prior to re-drilling or abandonment of the blast holes.

Figure 3. Borehole camera view of blocked hole

In either case, abandonment or re-drill, these instances will result in significant


additional cost for the mine, due to disruption to normal production drilling, loss of
drilling capacity or poor fragmentation and secondary blasting, in each case resulting in
loss of production capacity of the mine. The clearing and-re-drilling of holes is also a
strenuous operation and known to carry an increased risk of injury to workers.

The industry analysis presented below is from the Australian mining experience
(Hawker 2009). The problem of closing holes is principally where mining takes place in
weak or highly stressed ground and where blast causes damage. Block caving, in
particular, is usually conducted in relatively weak ground, and all the undercut holes are
vulnerable to damage. Undercutting is a part of mine development and not directly
linked to ongoing mine production, so the problem affects relatively brief periods in the
life of a mine. In the case of sub-level caving (SLC) operations, both blast damage and

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

stress result in very high re-drill rates. Re-drilling was estimated at around 30%
(Hawker 2009), and continues at that rate for life of mine. It is thus directly influential
on both production output and productivity. Additionally, many underground mines
could benefit from blast-hole preservation techniques from time to time, as they mine
through weak or highly stressed ground. In these cases, re-drill rate is estimated at
between 5 – 15 % of originally drilled metres.

Typical drilling costs for 89 and 102 mm holes are A$25/metre and A$30/metre
respectively.

The Australian underground hard-rock mining industry produces approximately 70


million tonnes of rock per year and drills approximately 7 million metres of ring holes
to achieve that output. A 2009 survey of the top 18 producing mines, representing 65%
of total output, gave an estimate of linear metres drilled per year of 4.6 million.
Excluding the block cave mines because of their episodic drilling operations left 4.4
million metres per year being drilled in SLC and open stoping perations. Conservatively
applying a factor of only 15% of primary holes being re-drilled at a cost of A$25 per
metre, the estimated cost to the Australian hard-rock mining industry from blocked
blast holes is A$16.5 million (R115 million). It can be expected that countries such as
Canada, with similar orebodies and mining practices, will be experiencing losses of
similar magnitude.

Apart from direct costs of re-drilling, blocked or collapsed blast holes are the indirect
cause of other cost increases, including:
• Deviations from the designed blasting pattern and powder factor, causing under-
or over-break, loss of reserves or dilution, over- or under fragmentation and
secondary blasting;
• Increase in labour complement, to undertake the largely manual clearing of
blocked holes. On fly-in/fly-out mines, where the mine operator bears all living
and transport cost, this is a material cost.
• Increase in investment in drilling equipment, to handle the re-drilling required.
Industry approaches to dealing with the problem

The most common approach to alleviating the problem is adoption of a “just in time”
drilling strategy. Holes are drilled for one blast only, then fired within a few days.
Although this almost eliminates the need for re-drilling, it results in decreased
flexibility in operational scheduling as drilling must be closely synchronised with
blasting. The drilling equipment must be more frequently trammed between working
places, causing reduced availability for actual drilling – and so an increase in inventory
of drilling equipment.

Mines have attempted to keep drilled holes open during the drilling process by using
cement slurries or additives that mix and set with the drill cuttings to bind the borehole
walls but these technologies are only beneficial for down-holes and do not contribute to
support of the blast hole that is often needed during the production blasting where
significant vibrations lead to un-ravelling of the rock wall.

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6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

Strengthening of the hole was also recognised as a potential solution. Junction mine in
Western Australia (now closed) forced slotted PVC pipes into their blastholes. This was
effective in keeping the holes open. Although the cost was high, the benefits of reduced

re-drilling outweighed them and the system was applied over many years; it has not
found wide application however.

More recently a spray-on coating has been developed that holds the promise of offering
a cost-effective, widely applicable system that is compatible with mechanised
explosives loading systems.

Spray-on rock reinforcement systems

Since the late 1990’s, thin sprayed liners (TSL’s) have been increasingly used in the
mining and tunnelling industries for protection and stability enhancement of rock
surfaces (Potvin, 2002). Usually the TSL’s are applied by hand-held nozzle or robotic
arm, similar to shotcreting practice. Harrison (Harrison, 2003) described remote
spraying of a TSL to stabilise the rock surface of 1.5 m and 3.2 m diameter raise-bored
return-air raises in the norite country rock surrounding the Cullinan Diamond Mine.
Their apparatus used a rotating disk to distribute a TSL being pumped onto its
periphery. An essential feature of that application was close coordination between the
rates of TSL pumping and movement of the spray-disk along the length of the bore, to
ensure that the desired thickness of coating was obtained. The project was successful.
Remotely-applied spray linings are also used in the micro-tunnel and pipe repair
industries (Trenchless World, 2011).

Minova Australia is a supplier of rock support systems (including TSL’s); it is a


subsidiary of Orica Limited, a major explosives supplier to the Australian mining
industry. A significant portion of explosives consumption is supplied fully pumped into
the holes and Orica was therefore daily exposed to the problem of blocked holes.
Recognising that the problem was one of uncontrolled rock deformation, Orica
approached Minova to analyse the problem and propose a solution. The proposed
solution drew on mining TSL and explosives pumping technologies: it is a “reactive”
TSL (as defined by Spearing, 2002) sprayed onto the inside of the hole just after
drilling. The TSL forms a tough structural membrane 2-3 mm thick that resists spalling
and deterioration of the rock surface.

The Liner System

Prior to selection of the resin system that would be used for development work the
performance criteria were defined.

The resin needed to:


- Set quickly, with an ideal set time of a 1-3 minutes post mixing.
- Gel quickly to eliminate resin loss in up-hole applications.
- Have high bond strengths to rock, generally exceeding 1 MPa in bond.
- Provide a support lining that would offer confinement to the rock surface but not
be too brittle.

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6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

- Not pose significant OH&S issues for handling.


- Work in humid and wet conditions.
- Have low viscosity to enable ease of pumping, with an ideal range of 200-
500mPas.
- Be compatible with a range of explosive systems available on the market.

Various resin systems were considered for use, such as Polyureas, Polyesters, Epoxies
but these often matched some of the criteria but not all. The Minova range of organo-
silicate resin systems was then explored as a possibility and a suitable resin system
selected for initial testing. This silicate resin matched the criteria in nearly all areas and
in particular it was a resin that would quickly gel, increasing from individual viscosities
of 300-400 mPas to a mixed viscosity of over 90000 mPas once combined. It is a two-
component resin (named Components “A” and “B”) in which the components are
mixed at the spray nozzle and react rapidly to immediately form a cross-linked polymer
layer.

Other properties of this resin system are shown in the table below:

Tests performed at 22oC

Ratio A:B
Component Component
2:1 1.5:1 1:1 Standard
A B
Punched 3 mins 5 8 5 Density DIN
1445±50 1150±25
Shear
5 mins 14 12 6 Kg/m2 12791
Strength
(MPa) 1 hour 25 20 9 Dark
Light
Colour brown/red -
Gel Time (secs) 10 3 3 brown
tinge
Cure time: DIN
Flash
Penetrometer 33 26 24 - > 140
point oC 53213
hardness test (secs)
1 hour 70 Viscosity
UCS ISO
@ 25oC 320-420 250-350
(MPa) 24 hours 75 3219
mPas
2 mins 42
Shore D 5 mins 55
Hardness 10 mins 62
30 mins 70

The advantage of the active TSL over conventional “non-reactive” TSL’s is that mixing
only takes place near the nozzle so small quantities may be dispensed without material
starting to set in mixers, hoses and the spray nozzle; also hardening is almost
immediate.

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

Following the verification that the material properties would be suitable, confirmation
was also required that the cured material would not react with explosive systems. A
range of tests was performed on both gassed and un-gassed emulsion and also ANFO to
conclude no reactivity existed between the cured resin system and these materials.
(See Figures 4 and 5)

Figure 4. Compatibilty with ungassed emulsion

Figure 5. Compatibility with gassed emulsion

Components and operation

The development of equipment for the blast hole lining process concentrated on two
key areas of a dual component pump and a spray head. Whilst a hose feeding system
was also critical to the application it was anticipated that existing hose feeding systems
available on the market, in particular the hose feeding systems for blast hole charging,
would meet the needs of the project,

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

Equipment consists of:

A two-component pump (Figure 6) that delivers the two chemical components of the
resin in a fixed ratio, to the delivery pipes. The pumping rate must match the retraction
rate of the spray head to ensure a full coating of the blast hole wall and achieve a 2-
3mm nominal thickness. Product consumption of one litre per blast hole metre was
calculated and thus a pump with output range of 10-15 litres per minute that could
deliver over 10 MPa pressure was required. The final criterion for the equipment was
dual action from the pistons to ensure consistent product feed to the spray head. Trials
had demonstrated that pulsing of the product feed rate would lead to gaps and
inconsistency in the final liner coating. The pump is a modified version of the standard
pump used for injection of resin to stabilise broken rock.

Figure 6. Two-component pump

Spray delivery system. The spray head needed to firstly accommodate two product
lines to fit into its base but also needed to fit inside blast holes of diameters as low as 89
mm. The spray head also needed to be low weight to ensure it could easily be pushed to
the back of up-holes that maybe up to 40m in length. The spray head incorporates a
static mixer that mixes the product correctly in a short distance to ensure the length of
the spray head was short as possible. Finally the spray tip was selected to best match the
desired coating. A full fan spray tip that delivered at an angle of 120 degrees was
selected. Figures 7 and 8 show the spray head assembly.

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

Figure 7. Spray head assembly

Figure 8. Spray head and nozzles

Surface trials

Following the selection of the required product and equipment, a series of spray trials
were conducted on surface to prove the concept and that ensure a full coating at the
required thickness could be achieved. A number of 90 mm PVC pipes of 25m length
were installed vertically. Following this the capacity of the pump to deliver a full spray
fan at 25 m height was checked then a series of trial sprayings conducted to check the
spray pattern inside the pipes at various heights. During the testing it was discovered
that a hole-centralizer would be of value to ensure the spray tip stayed approximately
central during the spray retraction process. It was also discovered that multiple coats
could be achieved to increase the liner thickness if required and that increasing the
retraction speed would enable a thinner coating of approx 1 mm. Several blockages of
the pipe also occurred during testing when the retraction was stopped, thus suggesting
that any delay of the spray head retraction during the lining operation may cause hole
blockages. An example of the spray result can be seen in Figure 9.

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

Figure 9. Inside coated test pipe

Mine site trials

Following completion of the surface trials and demonstration of the system to the mine
customer a series of mine trials commenced. The first of these trials was the lining of 9
production holes of length 20-25 m and diameter 102 mm. Several of the lined holes
would be used for visual surveying after lining to check for hole collapse whilst two
holes would be used to check EP VE explosives retention. These initial trials used a
nylon adaptor to connect the spray tip. This was prone to damage during the
installation, which caused several spray tips to come off during trial. In the second
series of mine site trials a steel adaptor was used.

The second round of trials involved the lining of 60 production up-holes again of length
20-25 m and diameter 102 mm. During these trials several other issues were noted.
Firstly the use of the Orica 25mm powerhose hose pusher proved inconsistent when
trying to push the spray head and product lines to 25m height. An average height of
15m was all that could be achieved. Further testing noted that the use of a larger
diameter powerhose overcame the limited height and a height of 25m could be reached.
The second issue was the use of a nylon body for the spray head. Although this item
assisted with keeping the spray head weight low, spray pressure above 1500PSI caused
leaks in the spray head and resulted in inconsistent spray coverage in several blast
holes. An aluminium spray head has now been developed which enables greater
working pressures to be reached. The series of photos (Figures 10, 11 and 12) show
details of these spray trials.

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

Figure 10. Inserting the spray head

Figure 11: Lined hole

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

Figure 12. Borehole camera view of hole lining

Monitoring and Results

Following completion of the initial trial it was evident from camera survey work that a
full coating of resin could be achieved to the blast hole (See Figure 12). EP VE
emulsion explosive retention in lined holes was not impacted and thus the 60 hole
campaign was approved.

Completion of the 60 hole campaign took several days with 22 holes being lined in one
10 hour shift when there were no interruptions. Lining of one blast hole was estimated
to average 5 minutes.

Monitoring of the 60 holes was initially completed with a borehole camera survey. This
survey discovered some unlined sections of the borehole which were later discovered to
be due to nylon spray head body pressure limit. Holes could only be lined to average
height of 15m due to the limitations of the pipe pusher system.

Lined holes were gradually mined through over a 12 month period due to various
production delays. Some blockages of lined holes were noted and are thought to be due
to inconsistent lining in these holes. Most of the lined holes remained open and these
are attributed to full coating at nominal thickness of 2 mm. Without the coating, all
holes on the mine were usually closed within 6 weeks.

Trials indicated that development of an independent hose pusher and mobile vehicle
would be required for full industrialisation of system; standard hose pushing equipment
can be utilized if the feeder hose is of sufficient strength.

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

Conclusions

Initial mine site trials have demonstrated that a blast hole can be supported for a long
term using a reactive resin lining post-applied to the drilled hole. To ensure ease of blast
hole coating and prevent hole collapse prior to lining it is suggested that lining of the
blast holes is best carried out as soon as possible after drilling. Damage of the lining
was noted when inconsistent coating was applied, with a majority of this damage
caused by blast vibration. Further mine trials are being planned by Minova to further
develop this application technology.

Acknowledgements

The authors would like to acknowledge the financial support of Minova International
and Orica Mining Services and in particular the efforts of Chris Fox, Minova Australia
Technical Officer and Steve Thomson, Orica Mining Services for their ongoing work.

The image used in Figure 1 is by permission of Atlas Copco MCT AB, taken from the
publication “Guide to underground mining methods and applications”, 1980

References

Thomson, S. Concept paper Blast hole preservation, Orica Mining Services Australia
internal report, Internal report, 2009

POTVIN, Y., Towards a common understanding of TSL applications in mines,


SAIMM, International Seminar on Surface Support Liners, Johannesburg, 2002.

SPEARING, A.J.S and GELSON, J. Developments and the future of thin reactive liners
since the previous conference in Australia (August 2001), SAIMM, International
Seminar on Surface Support Liners, Johannesburg, 2002.

HARRISON, A.”Spinnekop Project”, presented at SANIRE Coalfields Branch


Meeting, November 2003.

TRENCHLESS WORLD, Magazine published by Aspermont UK, March 2011

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The Southern African Institute of Mining and Metallurgy
6th Southern African Base Metals Conference 2011
R Hawker and D O’Connor

The Authors

Robert Hawker – BSc. (Chemistry and Geology) 1997 – University of Wollongong


Technology Manager, Minova Australia, Nowra, Australia

Rob joined Minova Australia, previously Fosroc Mining Australia in December 1997 as
Product Development Engineer. Minova Rob has been involved with a variety of
projects dealing with cementitious, polyurethane and flexible membrane systems for
both the metalliferous and coal mining industries. Rob spent eight years as Product
Manager for the flexible membranes and injections resins product range and has been
leading the Minova Australia technology team for the past 2 years.

Donald O’Connor, Director, Minova RSA

Worked from 1978 - 1981in the SA gold mining industry in rock engineering and mine
seismicity research. Since 1982 has been involved in the development, manufacture and
application of explosives and rock support systems, covering resin and cement grouts,
cavity filling and backfill, thin spray liners and drilling equipment.

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