Advanced Gasturbine (Agt) Technology Development Project: DOE/NASA/0167-12 Nasa CR-180891 Garrett NO. 31-3725
Advanced Gasturbine (Agt) Technology Development Project: DOE/NASA/0167-12 Nasa CR-180891 Garrett NO. 31-3725
Advanced Gasturbine (Agt) Technology Development Project: DOE/NASA/0167-12 Nasa CR-180891 Garrett NO. 31-3725
NASA CR-180891
GARRETT NO. 31-3725(12)
ADVANCED
GASTURBINE(AGT)
TECHNOLOGY
DEVELOPMENTPROJECT
FINAL REPORT
Engineering Staff of
Garrett Auxiliary Power Division
A Unit of Allied-Signal Aerospace Company
March 1988
Prepared for
NATIONAL AERONAUTICS AND SPACE ADMINISTRATION
Lewis Research Center
Cleveland, Ohio 44135
Under Contract DEN3-167
for
U.S. DEPARTMENTOF ENERGY
Office of TransportationSystems
Heat Engine PropulsionDivision
WashingtonD.C. 20585
TABLE OF CONTENTS
Pa e
1.0 SUMMARY
2.0 INTRODUCTION
i
TABLE OF CONTENTS (Contd)
Pa e
Combustor Design 88
Combustor Development 90
££
TABLE OF CONTENTS (Contd)
Page
6.3 Ceramic Struetures 207
APPENDIX E REFERENCES
iii
LIST OF FIGURES
F eure Title
21 AGTI01 S/N 001 Build 21 Fluid Film Thrust Bearing (Test 4-19-84) 23
iv
LIST OF FIGURES (Contd)
Title
V
LIST OF FIGURES (Contd)
Title
vi
LIST OF FIGURES (Contd)
Title
70 Compressor Rig 54
vii
LIST OF FIGURES (Contd)
vi re Title Page
93 Compressor Test Rig with Slip Ring Assembly Installedin Test Cell 64
108 Turbine Inlet Strut Sections [Modified NACA 16-201 (tlc = 0.30)] 71
109 Turbine Inlet Hub and Tip Velocity Distribution for Baseline
Configuration 71
viii
LIST OF FIGURES (Contd)
Title Page
113 Ceramic Turbine Stator Velocity Distribution (Linear Pressure
Surface, 19 Vanes) 72
121 Baseline Ceramic Cold Turbine Rig Test Results, System Efficiency
Versus Pressure Ratio 78
122 Baseline Ceramic Cold Turbine Rig Test Results, System Efficiency
Versus Engine Speed 78
124 AGT101 Metal Dual Alloy Wheel - 13 Blades, Conical Astroloy Hub 79
l
131 As-Cast AGT101 Bladed Rings and Machined Dual Alloy Wheel
Assemblies 83
133 Microetched Cross Section of AGTI01 Dual Alloy Wheel Test Specimen 84
ix
LIST OF FIGURES (Contd)
Title Page
150 93
AGT101 "Regenerator System" Componenls
q
154 Static Seal Leakage Comparison for Seal Design Phases I00
X
LIST OF FIGURES (Contd)
Title page
157 Regenerator Seal Coating Wear Test Rig 103
x£
LIST OF FIGURES (Contd)
Title
180 Measured HP AP Data From Regenerator Cold Rig with Bonnet 129
184 Capacity Rate Ratio and Integrated Mass Flux Versus Radial Position 132
194 Phase V Regenerator Seal Drive Torque Versus Seal Pressure 139
xii
LIST OF FIGURES (Contd)
Title ea e
201 Engine Electronic Control Unit (ECU) 143
xiii
LIST OF FIGURES (Contd)
TitIe
2O5 Interface Conditions for 871, 1149, 1371C (1600, 2100, 2500F)
TIT Engines 170
208 Static Coefficients of Friction Versus a Normal Load for RBSN and
SASC at Room Temperature 173
209 Friction Versus Relative Motion for Bare SASC and RBSN Under the
Point Contact Condition With a Normal Load of 25 Pounds 173
212 Friction Versus Relative Motion for Bare SASC and RBSN Under the
Line Contact Condition With a Normal Load of 25 Pounds 175
213 Room Temperature Strength RBSN and SASC After Line and Point
Contact Tests 175
xiv
LIST OF FIGURES (Contd)
Title Page
215 RCG Coated and Machined HTP Insulation from Lockheed 180
217 Maximum Power and Idle Condition of Lockheed HTP-16 Insulation 181
222 Rotor S/N 256 Failed During Spin Test in Mode Similar to
Previous Engine Failure 186
225 Initial Attachment Method Involved Solid Stub Shaft Rotor 189
229 Typical 3-D Views of the Finite Element Blade Vibration Model 191
XV
LIST OF FIGURES (Contd)
Figure Title
243 Principal Stresses for Room Temperature 115,000 RPM Proof Test
Predicted from No-Fillet Model 202
247 Rotor Failure Probability for Partial Power Operating Conditions 205
248 Rotor Failure Probability for Maximum Power Operating Condition 205
xvi
LIST OF FIGURES (Contd)
Title
261 Turbine Shroud Critical Stress Areas (Shroud Screening Rig Model) 217
266 Turbine Shroud/Outer Diffuser Critical Stress Areas (Engine Model) 223
xvii
LIST OF FIGURES (Contd)
Title
281 The Original and Strutted RBSN Flow Separator Housing FEMS 238
xviii
u
LIST OF FIGURES (Contd)
Title Page
295 Typical Correlation Between Test and Analytical Turbine Stator
Thermal Response 246
298 Original Turbine Stator MPS Distribution 20 Seconds After Light-Off 247
299 Cutback Turbine Stator MPS Distribution 20 Seconds After Light-Off 247
303 Combustor Assembly Steady-State 1371C (2500F) Max Power MPS 249
xix
LIST OF FIGURES (Contd)
Figure Title
318 Strain Gaged Regenerator Shield and Mechanical Screening Rig 259
321 Standard Oil SASC Stator Vanes in the Thermal Shock Test Rig 261
323 Transition Duct and Baffle Screening Rig with Original (top)
and Final (bottom) Configurations 262
324 Turbine Shroud Screening Rig Original (top) and Final (bottom)
Configuration 263
325 Static Structure Rig Original (top) and Final (bottom) Configurations 265
326 1371C (2500F) Static Turbine Rig Original (top) and Final (bottom) 267
XX
LIST OF FIGURES (Contd)
344 Plaster Base and Mylar Ring for Casting Solid Ingot 297
355 Single Dip Wax, Plaster Base and Steel Retaining Ring 309
356 Rotor Pore Size Versus Spin Test Rotor Speed 317
xxi
LIST OF FIGURES (Contd)
Title Pa e
366 Short Hot FillPattern When Using Single Point Gate 331
367 Full Shots Using Point Gate Material Pull-Out in Gate Area (a)
and Solid Shroud Cracks (b) 331
xxii
LIST OF FIGURES (Contd)
Figure Title
379 Ceramic Flow Separator Housing Showing Strain Gages in Place 343
381 Ceramic Flow Separator Housing with Double Wall Bulkhead 345
xxiii
LIST OF TABLES
Table Title Pa e
1 Comparison of Foil Bearing Designs 16
9 Impeller Properties 57
12 Turbine Design Point Cycle Conditions Sea Level, 29C (85F) Day,
Maximum Power 70
16 Combustor Data 92
xxiv
LIST OF TABLES (Contd)
Table Title
27 Fast Fracture and Stress Rupture Data was Measured for Many
Advanced Si3N 4 and SiC Materials 149
30 Flexure Strength and Fracture Origins of Laser Marked Test Bars 178
xxv
LIST OF TABLES (Contd)
52 Test Cycle for Initial 1371C (2500F) Testing in the Stator/Shroud 276
Screening Rig
xxvi
LIST OF TABLES (Contd)
xxvii
This Page Intentionally Left Blank
xxviii
1.0 SUMMARY
The design of the AGT101 is based upon 1.2 Power Section Development
the use of high technology structural ceramics
Engine Mechanical Development
in the hot gas flowpath. Symmetry of the
ceramic structures was a primary design con- The gas lubricated foil bearing is located
sideration, as it provided more uniform at the hot end of the turbine rotor, between
stresses throughout each part and eased the the compressor and the turbine wheel. The
fabrication of components. It also made anal-
self-generated gas film requires no external
ysis by finite element methods a much simpler pressurization, and the bearing is tolerant of
task, as most work could be done using two- high temperatures as well as a degree of rotor
dimensional models.
misalignment and distortion. Once developed
for stability and load capacity, foil bearing
A continously variable transmission (CVT)
temperature capability and material compati-
with high reduction was required for use with bilty were developed. The bearing configura-
a single shaft turbine engine in an automotive tion in use at the end of the AGTI01 program
application. Power transmission is through a employed gold coated foils running against a
VSTC coupled with a high reduction planetary sintered silicon nitride (SSN) journal (the rotor
gearbox. This assembly is bolted direct to a shaft). This configuration offers excellent
Ford four-speed AOD transmission. Offsetting load capacity (24 ib at 75,000 rpm) as well as a
speed changes in the transmission and the low wear rate.
planetary gearbox produce a continuously vari-
able drive. The VSTC was tested early in the The rotating group support system also
program to generate a performance map, and employs a circular thrust runner, added to the
gearbox differential ratios were selected to engine configuration to increase damping and
operate the VSTC in the most efficient areas. control subsynchronous rotor whirl. This
Activities related to the development of the thrust runner is part of a pressurized oil-
power transmission portion of the powertrain lubricated thrust bearing. The compressor end
were deferred for industry sponsorship when of the rotating group is supported by a high
project funding levels were reduced and the speed ball bearing, and sealed by floating ring
project was redirected. Note that the com- seals.
i
Operational clearances were measured combustor performance, flowpath leakage, and
during metallic engine operation, and then regenerator durability.
corrected to determine ceramic engine clear-
ances. While some performance data was obtained
at 1149C (2100F) using the metallic (dual
Engine Rotor Dynamic Development alloy) turbine rotor, performance testing of
the all-ceramic configuration was limited by
During the course of the engine develop- the material properties of the rotor. The
ment, dynamic instabilities in the rotating performance data taken was used primarily to
group were addressed by isolating the rotor assist in seals development.
from gearbox excitations, inserting an oil film
thrust bearing into the design, and by making One seal area recognized as critical was
the tieshaft integral with the gearbox input that between the turbine shroud, flow separa-
quill shaft. These modifications allowed con- tor housing, and transition duct. The high
sistent operation to full speed of 100 krpm. temperatures in this area dictate the use of a
ceramic sealing element. The initial concept
Engine Development Evaluations for this area, which employed two seals sepa-
rated by a ceramic wave spring, was even-
The AGT101 test bed was developed in tually modified to three sealing elements with
three consecutive configurations. The first an increased axial load.
was metallic, with only the regenerator core
and regenerator seals employing ceramics. 1.3 Component/Subsystem Development
This configuration was used early in the pro-
gram for system development to 1600F Tur- Activities centered around the develop-
bine Inlet Temperature (TIT), and for rotor ment of the following major components and
dynamics, controls development, heat transfer subsystems: compressor, turbine, combustor,
coefficient determinations, rotor system eval- and regenerator.
uations, and regenerator development. This
configuration was also used to test a ceramic The compressor system consists of a single
turbine wheel to 97 krpm, and was employed stage backward swept wheel with 12 full and
as a proof test of ceramic turbine wheels prior 12 splitter blades, a three stage radial dif-
to their installation in the all-ceramic engine. fuser, and a set of 17 variable inlet guide
vanes (VIGVs). One design iteration from the
An intermediate configuration incorpo- original design yielded a compressor with the
rated ceramic structures in the hot gas flow- required ratio and flow, diffuser performance
path, but retained the metal turbine wheel and close to predictions, and a desirable efficiency
used a metal combustor with a thermal barrier envelope for the automotive application.
coating. This configuration was used to verify Although considerable work was done with
the design of the ceramic structures, and to Alcoa on the development of a forged powder
obtain performance data at 2100F. A success- metal aluminum compressor wheel, the backup
ful 100-hour endurance test was also run with titanium impeller was used for engine testing,
this configuration. due primarily to time constraints.
The third major_ iteration featured a ce- The AGTI01 turbine wheel is a single stage
ramic combustor and turbine rotor as well as radial inflow design, specifically for ceramic
ceramic structures. Operation during the materials. The turbine wheels used inthe 871C
AGTI01 program was limited to 1204C (1600F) and I149C (2100F) configurations
(2200F), due to material limitations of the utilized the ceramic design, but these metals
turbine rotor. Long term steady-state opera- wheels were cut back at the inducer tips to
tion at 2200F was demonstrated, although fur- reduce stress. Turbine stators were made in
ther development was indicated in the areas of two basic configurations, with an integral ring
2
fabricated of metal used successfully in the Testing was also done in a hot rig to
lower temperature 871C (1600F) configura- measure leakages in the regenerator system,
tion, while 19 individual segments were determine matrix effectiveness, measure core
required to make the higher temperture drive torques, and measure the cavity pressure
ceramic stators survive. at the core ID to determine the bleed orifice
size. It was seen during this testing that while
For the 1149C (2100F)design, a dual alloy the effect of core clearance on leakage at low
turbine wheel of MAR-M 247 and Astroloy was pressures was small, at higher pressures the
employed, although its use was discontinued leakage was very sensitive to clearance.
after a reliability proglem with the bond joint
betweenhub and blade ring was identified. 1.4 Ceramic Materials and Component
Development
The ceramic rotor was redesigned during
the course of the project to improve fabri- Ceramic Materials Testing- In the last two
cability. The changesmadeto the blade shape years of the AGT program, significant testing
did not significantly affect the efficiency of was done to characterize the advanced sin-
the design. tered silicon nitride and silicon carbide mate-
Combustor development looked at both rials. The high temperature properties of
variable and fixed geometries as a means of several candidate rotor materials were deter-
achieving the requirements of low emissions, mined to be inadequate to meet the rotor
multi-fuel capability, and good fuel economy. requirements. Data from as-fabricated test
The fixed geometry was determined to be bars showed adequate properties in four mate-
more feasible, for its lack of moving parts, rials: SN-82 and SN-84 from NGK-Locke, and
and at program's end, a redesign incorporation SN 250M and SN 270M from Kyocera. The
SN-82 and SN 270M materials could not be
a larger primary burn zone was favorably
evaluated. Nozzle development emphasized formed into the complex rotor shape, and
good atomization and reduced heat load, with testing of the material properties of the SN
a simplex design incorporating air cooling, air 250M rotors revealed significantly lower ma-
assist, and a center-body ignitor as the terial properties than indicated by the initial
favored arrangement at the close of the pro- test bar data. Similar testing of SN-84 rotors
ject. also showed lower properties than test bars,
but the reduction in properties was not as
Regenerator development was carried out significant, and so the SN-84 material appears
at Ford motor Company and at Garrett. The to be suitable for 1371C (2500F) engine test-
regenerator cores, supplied by Corning and by ing.
NGK-Locke, exhibited performance approach-
ing RPD goals. Critical to the successful Although large improvements have been
development of the regenerator system is the made during the AGT program, additional
design of regenerator seals. The performance work needs to be done to achieve better ele-
of these seals has been improved on a static vated temperature properties, fracture tough-
basis over the course of the program, ness, and shape capability.
approaching AGT goals, but performance and
durability have been hampered by distortions Ceramic Compatibility Testing-Stress and
at engine operating temperatures. Further temperature conditions at various engine
development of these seals if required before interfaces were identified, and a series of
RPD goals can be successfully met. tests was performed using test bars to evalu-
ate the sticking characteristic at these inter-
Activities at Garrett included studies to faces. In those cases where sticking was
determine the pressure profiles of the system, observed, retest showed that no sticking
evaluate means of controlling flow, and occurred when flame-sprayed mullite coating
predict effectiveness. was used at the interface.
Other testing was performed to investigate yses using a finer substructure model mesh
the effects of line contact and point contact were performed.
at component interfaces and to evaluate coef-
ficients of friction for reaction bonded silicon Stresses were analyzed for 3 modes of
nitride (RBSN) and sintered alpha silicon car- loading encountered during normal engine
bide (SASC). Also, a study was performed to operation; one pressure (full power) and 2
determine causes for spalling in RBSN, and thermal (steady-state and lightoff transient).
fabrication techniques were successfully Shutdown transient conditions were initially
modified to reduce the occurrence of spalling. considered but were insignificant due to core
thermal inertia.
Identification of components by laser
marking of serial numbers was introduced fol- Rig Design/Development
lowing a study which showed little or no
strength degradation in most materials. Only Major structural components, such as re-
lithium-aluminum-silicate (LAS) was unsuited generator shield, flow separator housing, tur-
due to excessive damage to a legibly marked bine shroud and rocker assembly components,
surface. are first tested in mechanical rigs to simulate
the pressure and contact loading encountered
Ceramic Structures in engine operation. These tests then are
followed by a proof test in thermal screening
Initial design criteria for AGT101 compo- rigs to simulate the maximum principal
nents were established empirically, with com- stresses encountered in engine operation. The
ponent testing providing feedback to the thermal cycles for the screening rigs are de-
analytical process and material selection. fined so as to simulate stresses which exceed
Component symmetry was pursued in the basic predicted engine stresses under normal start
design to eliminate circumferential element by 25 percent.
analysis. This reduced cost, and allowed for
rapid analysis and extensive design iterations. Screening tests are intended to eliminate
The only exception is the flow separator components with gross internal defects and/or
housing, whose function required an asym- smaller defects lo_ated in regions of high
metrical design. stress. Lower quality components will frac-
ture during screening, allowing only the high-
To eliminate extensive design optimization est quality parts to continue through qual-
on each material/component combination an ification and engine test. Results of these
evaluation was performed on the preliminary tests can also feed back into the empirical
configuration for each component to identify design loop. Significant examples of this are:
primary and alternate materials. Subse- the inner diffuser housing, which was rede-
quently, design optimization was performed signed from a shape similar to a birdbath to a
using a prime material candidate for each shape more like a dinner plate following fail-
component. After design optimization was ures in the screening rigs; the elimination of
achieved, alternate candidate materials again slots from the turbine shroud flange following
were evaluated. mechanical screening tests in which failures of
RBSN shrouds initiated at those slots; and the
Because of the lack of ductility in redesign of the turbine shroud to reduce a
ceramics, localized stress concentrations can- stress concentration in the seal fillet radius
not plastically redistribute stresses. Conse- following repeated thermal screening failures
quently, known stress concentrations must be with origins in that radius.
reduced or eliminated from the design wher-
ever possible. When component analysis The static structures rig test utilizes all of
revealed significant tensile stresses near the ceramic components in an assembly of the
known stress concentrations, additional anal- engine structure, without the rotor, and
checks the mechanical functioning of the developed and used for long-term at 1371C
assembly. Further, the static structures rig (2500F) to investigate high temperature ef-
evaluates the sealing capability, component fects on ceramics. To date, limited sticking
capability, axial and radial pilots, contact at 1371C (2500F) has been seen, and no failure
loading, and stresses at elevated tempera- has occurred due to sticking. Some interfacial
tures. The maximum operating condition for distress was seen between the transition duct
this rig was set at I093C (2000F), which and combustor baffle, but this can be elimi-
corresponds to the maximum operating tem- nated by using an alternating material stack in
perature of the turbine exhaust. Sufficient this area.
confidence was eventually gained in the
thermal and mechanical screening rigs that
A cold seal leakage rig was also developed
use of the static structures rig was discon-
in which the performance of three ceramic
tinued as a qualification rig.
sealing areas could be evauated: turbine
To evaluate ceramic components upstream shroud/flow separator (piston rings), regen-
of the turbine exhaust, another rig, capable of erator shield/flow separator (butt joint), and
operation of 1371C (2500F), was required. The regenerator shield/exhaust housing (piston
initial 1371C (2500F) milestone was achieved rings). The cold leakage data allowed a com-
twice in the stator/shroud screening rig in the parison of seal concepts, and measured the
spring of 1984, for short durations. A separate effects of load, concentricity, and pressure
rig, the 1371C (2500F) static rig, was later distortion on these sealing interfaces.
5
2.0 INTRODUCTION
This report is the final in a series of o Emissions less than federal standards
Technical Summary Reports for the Advanced
Gas Turbine (AGT) Technology Development o Ability to use a variety of fuels
Project, authorized under NASA Contract
The Garrett/Ford automotive Advanced
DEN3-167 and sponsored by the DOE. This
Gas Turbine has been designated the AGT101.
report has been prepared by the Garrett Tur-
The AGT101 nominally is a 74.5 kw (100 shp}
bine Engine Company (hereinafter referred to
as Garrett), and includes information provided engine, capable of speeds to 100,000 rpm and
operating at turbine inlet temperatures (TIT)
by the Ford Motor Company hereinafter
referred to as Ford), Standard Oil Engineered to 1370C (2500F) with a specific fuel con-
sumption level of 0.18 kg/kw-hr (0.3 pounds/
Materials Company (Standard Oil), and
horsepower-hour) over most of the operating
AiResearch Casting Company (ACC). The
project was administered by Mr. Thomas range.
Strom, Project Manager, NASA-Lewis The program was initiated in October 1979
Research Center, Cleveland, Ohio. This
and was to entail 68 months. Two phases were
report summarizes plans and progress from planned; Phase I was 45 months long and
October 1979 through June 1987. involved most of the component/ceramic tech-
nology effort and the early engine and vehicle
testing. The 23-month Phase II was scheduled
Project effort conducted under this con- to include completion of the all-ceramic
tract is part of the DOE Gas Turbine Highway
engine effort plus the vehicle deliveries and
Vehicle System Program. This program is evaluation.
oriented at providing the United States auto-
motive industry the high-risk,long-range tech- Budget reductions in mid-FY81 resulted in
nology necessary to produce gas turbine a re-orientation of the program. The vehicle,
engines for automobiles that will have reduced transmission and engine gearbox/transmission
fuel consumption and reduced environmental efforts were deleted. The program was then
impact. The intent is that technology result- oriented toward developing the long-range
ing from this program be capable of reaching high-risk technology of the AGT101 gas tur-
the marketplace by the 1990s. bine such that the auto industry can carry that
technology forward to production in the
1990's. Emphasis was placed on ceramics, gas
The advanced gas turbine, when installed in bearings, low emission combustion and im-
a Ford vehicle with a 1364 kg (3000 lbs) inertia proved component performance. The AGT101
weight would provide: gas turbine was envisioned as a test bed in
which to develop these technologies.
A combined federal driving cycle (CFDC) The program schedule with milestones is
fuel economy of 5.5 L/100 km (42.8 miles shown in Figure 1. Key milestones accom-
per gallon) based on Environmental Protec- plished include completion of the design
tion Agency (EPA) test procedures using review in January 1980, the first set of
DF-2. The AGT-powered vehicle shall give ceramic structures passing rig test to 1093C
substantially the same overall vehicle (2000F) in August 1983, ceramic structures
driveability and performance as a compar- engine test to 1149C (2100F) in February 1984,
able production vehicle powered by a con- first ceramic structure rig test to 1370C
ventional spark-ignition powertrain system (2500F) in May 1984, first all ceramic engine
6
test in January 1986, and completion of an 85- This final report summarizes the power-
hour all ceramic engine test to 1204C (2200F) train design, power section development, and
in October 1986. While the feasibility of component/ceramic technology development.
applying ceramics to a gas turbine was demon- Appendices include reports of progress from
strated, further improvements in the ceramic Ford, ACC, and Pure Carbon. Work performed
turbine rotor material properties were needed by Standard Oil is published in NASA topical
for further testing. report CR-180871.
=ISCAL YEAR
GOVERNMENT MILESTONES
CERAMIC DEVELOPMENT
STRUCTURES
TURBINE
REGENERATOR DEVELOPMENT
COMPONENT DEVELOPMENT
POWER SECTION DEVELOPMENT
7
3.0 REFERENCE POWERTRAIN DESIGN
This reference powertrain design (RPD) is pressure side of the ceramic rotary regener-
comprised of the AGT101 power section, split- ator. This feature provides increased thermal
path variable stator torque converter (VSTC) efficiency by minimizing heat loss. The par-
gearbox and Ford automatic overdrive (AOD) tially heated air passes through the regener-
transmission as depicted in Figure 2. The RPD ator core where it is further heated to approx-
is to be installed in a 1364 kg (3,000 Ibs) imately I060C (1940F) temperature (at idle),
inertia weight vehicle. and then to the combustor.
The AGT101 engine, shown in Figure 3 is The combustion system features a fixed
flat rated at 74.57 kw (100 hp) with a mini-
geometry, lean-burn, low-emission combustor.
mum SFC of 0.18 kg/kw-hr (0.3 Ib/hp-hr). The
Combustor air temperature increases to a
single-shaft rotating group is composed of a maximum of 1370C (2500F) with the addition
radial turbine, centrifugal compressor, and of fuel, is ducted to the ceramic stator, and
output gear supported by an air-lubricated
then expanded across the radial turbine rotor.
foil-journal bearing and an oil lubricated ball Turbine exhaust gases 1093C (2000F) maxi-
bearing. The maximum (steady state) engine mum temperature at idle) are ducted through
speed is 100,000 rpm, and idle speed is approx- the low pressure side of the rotary regenerator
imately 50,000 rpm. and out the engine exhaust at a maximum
temperature of 266C (510F) at maximum
Ambient air enters the engine through
power.
variable inlet guide vanes and passes through
the single-stage compressor. The compressed
air, at approximately 185C (365F), is routed All ceramic hot section structural compo-
around the full engine perimeter to the high nents are symmetrical except for one housing
687_TB-tM
8
while the second path passes through the
planetary ring gear to a VSTC utilized as a
speed changing device. The variable output
speed of the VSTC is connected to the carrier
via a clutch that is open during vehicle idle
and closed during normal driving modes.
Speed ratio modulation across the VSTC
results in a variable output speed of the plane-
tary carrier, which in turn is geared directly
to the AOD transmission. Step ratio changes
in the AOD are phased with offsetting speed
ratio changes in the variable speed gearbox.
This produces a continuously variable drive"
line system which allows the engine to operate
at optimum speeds to deliver high efficiency
cruise power, acceleration power, or engine
braking power.
9
KEY
Op:DIAM.RAL
PITCR ___ ACCESSORY
OH_VE
N = RPM RANGE T
T: GEAR
TEETH
INUMDERI
AOD = AUTOMATIC OVERDRIVE "aTr_+64T ,= 2.?. ,6,3
i 31T OVERRUNNINGCLUTCH
PLANETARY --: _ N = 1716 - 3684
N =0- 65 8
, ,p..%"_l'lL,..j]___....
N1 : 55K-
I)p lOOK 35T MAIN OIL
REARAXLE RATIO
/
10
_F POOR QUALITY.
687_7_150
ll
LIFO0 km IMPGI ILB/HP-HR
0.70.
44
5.4 Ko/kW-HR
0.40" 065
5.5
43 0._'
0.35-
0._'
5.6
0.30 • 0._"
_ 5.7
0.43.
41 _ 0.25-
0.8
0._'
5.9
IFTi
020-
0.35"
0._-
\
0.15- 0.25
!
0 40 80 I00 120 KW
OUTPUT SHAFT POWER
!o -_
_ 3 G6/-O78.T62A
4 I I ! I
46 48 50 52 54
IOLE SPEEO,KRPM
12
4.0 POWER SECTION DEVELOPMENT
Power section development on the AGT101 the design of the ceramic structures, and to
concentrated on several key areas: gas foil obtain performance data at 1149C (2100F). A
bearing development, engine rotor dynamic successful 100-hour endurance test was also
development, and engine development evalua- run with this configuration.
tions. Development of the major components
of the power section is discussed in Section 5.0 4.1 Enffine Mechanical Development
- Component and Subsystem Development.
4.1.1 Foil Bearing
Experimentation with several different
foil, coating, and backing spring materials and The AGTI01 foil bearing design was re-
configurations eventually yielded a successful, quired to meet the following operating condi-
robust design in which gold coated foils run tions:
directly against a sintered silicon nitride jour-
nal (the rotor shaft). Operating speed 50,000 to i00,000 rpm
Maximum load 6 g for 0.2 seconds
Dynamic instabilities in the rotating group Maximum temperature 649C (1200F)
also required considerable effort to overcome.
In order to dampen the system and help to The operating range shown above repre-
control subsynchronous rotor whirl, the system sents the actual engine operating range, how-
as finally developed employs a circular thrust ever during engine starts and stops, the engine
runner as part of a pressurized oil-lubricated must operate at speeds of less than 50,000 rpm
thrust bearing. This and other modifications, and pass through 2 rigid body rotor critical
including the integration of the rotor tieshaft speeds. Additionally, the bearing breakaway
and the gearbox input quill shaft, finally al- torque must be below the engine starter stall
lowed consistent operation to full speed of 100 torque.
krpm.
In addition to the above, this application
The AGT101 test bed was developed in has imposed additional requirements on the
three consecutive configurations. The first foil bearing which are unique relative to other
was metallic, with only the regenerator core foil bearing applications developed at Garrett:
and regenerator seals employing ceramics.
This configuration was used early in program High unit loading at 1-g load. This bearing
for system development to 871C (1600F) tur- has a 30 kPa (4.3 psi) unit loading with a
bine inlet temperature (TIT), and for rotor ceramic turbine rotor or 39 kPa (5.6 psi)
dynamics, controls development, heat transfer with metal rotor. Previous high tempera-
coefficient determinations, rotor system eval- ture foil bearings were subjected to unit
uations, and regenerator development, this loads in the 7.5 to 14.5 kPa (I.I to 2.1 psi)
configuration was also used to test a ceramic range.
turbine wheel to 97 krpm, and was employed
as a proof test of ceramic turbine wheels prior Rotor excursions can exceed the calculated
to their installation in the all-ceramic engine. bearing sway space. The bearing may not
be hydrodynamic when the first critical
An intermediate configuration incorpo- rotor speed occurs.
rated ceramic structures in the hot gas flow-
path, but retained the metal turbine wheel and The AGT101 foil bearing was first devel-
used a metal combustor with a thermal barrier oped for stability and load capacity. This
coating. This configuration was used to verify work was performed through a combination of
13
analysis and testing in the single bearing rig. using the strain energy approach. The gas film
Bearing stiffness and damping were evaluated pressure distribution is then calculated based
during rotor dynamic development when minor on the deflected profile of the foils and shaft
changes in the bearing geometry were ef- speed. Convergence is achieved when the gas
letted to optimize these characteristics. film thickness matches the deflected foil pro-
Temperature capability and material compati- file for the same pressure distribution.
bility were developed once the basic geometry
was established. This work utilized the foil Figure 10 shows the model output for the
coating wear rig as well as the single bearing deflected height for the baseline bearing
rig to evaluate potential foil coatings. lightly loaded at i00,000 rpm. Take note that
Number of foils 7
Foil thickness 0.15 mm (0.006 inch)
Foil arc length 29.2 mm (1.150 ihch)
Foil axial length 26.5 mm (1.045 inch)
Foil preform radius 29.2 mm (1.150 inch)
Foil material Inco X750
Backing spring web 0.14 mm (0.0055 inch)
thickness
Backing spring arc 13.3 mm (0.525 inch) FOIL
length
Backing spring 27.9 mm (I.I00 inch)
RACKING SPRING
preform radius
Backing spring Inco X750
material
BASIC OEARtNG CONFIGURATION
Bearing sway space 0.15 - 0.25 mm
6|7-0711-183
0.006-0.010" inch
Foil coating Au-Ni or Au-Co Figure 9. Basic Bearing Configuration.
Journal surface Sintered Silicon
Nitride 28 ¸
Journal diameter 34.3 mm (1.350 inch)
24
*Diametral clearance between the journal and
aE 20
foils with the foils and springs making all i,,,,,-
14
most of the bearing deflection is taken in the ing torque is measured via a torque arm and
curvature of the foils and not in the backing load cell attached to the test bearing housing.
spring. This is because the backing spring is
used to help the bearing sustain high loads and Compatibility of the foil bearing with the
the model only simulates a lightly loaded con- rest of the rotor system was evaluated in the
dition. Figure 11 shows the pressure dis- rotor dynamics rig and in the engine test beds.
tribution for that bearing at operating speed. This work is discussed in the rotor dynamics
This model proved useful for establishing an discussion in Section 4.2.1.
initial bearing configuration and for screening
proposed bearing geometries before fabrica- Table 1 shows the progressive development
tion and testing. of the foil bearing geometry through the pres-
ent.
i .28
The "P" type foil is compared with the
1.24 reference bearing in Figure 12. This bearing
featured a redesigned backing spring and foil.
,.,.+1.20
The polyimide foil coating on the P type
1.1e bearing provided temperature capability up to
343C (650F), which was a 38C (100F) improve-
,_ !.12 ment over the temperature capability of the
I,,4,4
I',,I Teflon S coating used in the reference foil.
-" 1.08
15
Table 1. Comparison of Foil Bearing Designs.
Foil Thiek, mm (inch) 0.15 (0.006) 0.15 (0.006) 0.178 (0.007) 0.178 (0.007) 0.15 (0.006)
Foil Length, mm (inch) 30.2 (I. 19) 30.2 (1.19) 30.2 (1.19) 30.2 (1.19) 26.4 (1.040)
Foil Radius, mm (Inch) 21.0 (o.85) 21.6 (0.85) 21.6 (0.85) 27.9 (1.100) 29.2 (1.150)
Spring Web, mm (inch) 0.127 (0.005) 0.15 (0.006) 0.15 (0.006) 0.15 (0.006) 0.14 (0.0055)
Spring Radius, mm (Inch) 17.78 (0.70) 20.3 (0.80) 20.3 (0.80) 22.9 (0.90) 27.9 (1.10)
Journal Coating METCO 443 METCO 443 ME?CO 443 ME?CO 443 TiN or SSN
Sway Space, mm (inch) 0.279 (0.011) 0.259 (0.0102) 0.259 (0.0102) 0.203 (0.008) 0.203 (0.008)
Load Capaeity, N (It)) 53.4 (12) at 88.9 (20) at 88.9 (20) at 88.9 (20) at 106.7 (24) at
100,000 rpm 100,000 rpm 100,000 rpm 100,000 rpm 75,000 rpm
Turbine Vibration, mm (mil) 0.076 (3) at 0.038 (1.5) at 0.02 (0.8) at 0.02 (0.8) at 0.013 (0.5) at
100,000 rpm 100,000 rpm 100,000 rpm 100,000 rpm lO0,OOO rpm
,Nco
x.,50
5U,3THATE ,'7, ,
_MATEH,AL
iM,L I I' [ /
TH,HNER JVPol (I'I'_ _/t'_1
FOIL I COATING:
LARGER PREFORM HI HER
:::_S
RAOmUS __/ ON 30_
TEFLON SS
COATING _ _--_j ,.
'_/_,
POLYIMIOE IIOOF SUBSTRATE
| TEMPERATURELIMITI ,,,. _ _-_._---r-_._,,_j \ i\ '___,,,,p / D-TYPE
l , LASER WELDED _ I I -- \
'NCO 719 MATERIAL _ _ .- -- ".,,. _,_1,_,. , _ j,.
TALLER, THINNER RIBS • \_ _" --\ [ _ I / I _ /
THINNER. WIDER WEBS _ J _ . I I • _ l_ I [•1 l
OETWEEN
SPR,NOS ,,8s " \ ix. I.L /
mAROER RADIUS
PREFORM j ....__ _ _ I _ I ,'1_ ",'f I / ",. /
50 PERCENT GREATER ,," /'_.,_,,_ % %J ' I- I_ } _ TACK WELD -- "'" -- I"
TOTAL THICKNESS %., _ -... _ \ / , _ _ ........
302 SS/
GeZ-OTS-ie7 MATERIAL
16
OBJECTIVE:SURFACECOATINGSANO DISK ALSO TRANSLATES AXIALLY ON
MATERIALS FOR BEARINGS AXIS OF REVOLUTION. AMOUNT OF FORCE
TO 1200F
AT CONTACT SURFACE IS CONTROLLED. FLAT ROTATING OISK
_ t "JOURNAL" COATING APPLIED
[ CANDIDATECOATINGS] ONTACT SlOE
1 } 538C IIOOOFi
STEP I 427C
649C {{120OFi
80OF)
(
"FOIL" SPECIMEN SUPPORTED _ ,, ...... _... -
ON AIR BEARING AND
.'_R!N.-__N_-'- rLA, ",O,L" SPECIMEN
TOROUZ TO COONI[IIAC! _ _'I_TH C_]_'_'NG APPLIED
BOTATION MEASURED
start/stop durability. Once coating systems The test procedure for single bearing rig
passed the single bearing rig evaluation, they evaluation of the candidate foil bearing sys-
were evaluated in an actual rotor system, tems was as follows:
either in the rotor dynamics rig or in an
engine. The dynamic properties wear rig tests Ten no load starts to 50,000 rpm. Measure
simulate the non-hydrodynamic operation of a bearing static friction before and after
foil bearing during starts and stops with cold starts
17
Table 2. Dynamic Properties Rig Test Results.
Foil Coatings
Yttria
IN?18 Stabilized Titanium Chromium
Journal Coatings Gold (Au) Boronized Zireonia (YSZ) Carbide (TIC) Oxide
Sintered SUieon Good atall Not tested Excessive abra- Not tested Not tested
Nitride (SSN) temperature sion at ambient
Titanium Nitride Good atall Not tested Not tested Not tested Not tested
(TIN) temperatures
1090 Chrome Coating failure Not tested Not tested Not tested Not tested
at 1000F
Karamite Good at all Not tested Not tested Not tested Not tested
temperatures
Yttria Stabilized Not tested Exeessive Not tested Not tested Not tested
Zireonia (YSZ) abrasion
at
ambient
Kaman SCA Not tested Not tested Not tested Good at all Coating
temperatures failure
O Ten l-g load starts to 50,000 rpm. Mea- perties rig testing. Table 3 summarizes the
sure bearing static friction before and resultsof this testing.
after starts
The initial testing with the METCO 105
O Remove bearing and visually examine for (plasma sprayed Alumina) and METCO 202
damage. If there is no damage, reinstall (plasma sprayed Yttria Stabilized Zirconia)
the bearing and measure static friction coated shafts with the soft and then with the
hard gold coatings gave a lead that the hard-
o Measure power consumption at loads from ened gold foil coating might be compatible
l-g to the maximum load attainable for 2 with the high density silicon nitride ceramic
seconds or more shaft. Subsequent testing in the dynamic
properties rig and then in the single bearing
o Remove bearing and examine rig proved this combination to be the optimum
system.
Replace bearing foils and shaft if neces-
sary. Measure static friction. Run 1000 1- The rig testing of the SCA/TiC coating
g load starts. Measure static friction,then system required some manipulation of the foil
examine bearing. bearing geometry to achieve the 85.3N (19.2
lb) load capacity. Initial bearing geometry
Single bearing rig testing was used to eval- was the same as the "P" type bearing de-
uate surviving candidates from dynamic pro- scribed in Table 1, however the load capacity
18
C,,,_:}E,:A:b P,'_'-, ,,
19
TIME--
I SEC 2 SEC 3 SEC 4 SEC
.._...._.__ _ . .
2000
; : ; i : : ! ] : i !"
O. .... " : ' ' ' : i _ I ' '_ ...... ' i t"
w,J
mL
[ ' ii :." _ : [:::'I -;b: :,. t .-.:':-'t-" :_::-::.::_= ,::::_.'-t:'l_.: .," "t',: "['-=,: :-.-:'T'-:_-:"V'-I
1.0
I
! : ! ,"!: :".-]-_BREAKAWAYAND:.:;_::--
i ! :_ TRANSiTiON
TO _-]:_:-
r.
W,.
Z
RESIOUAL
TORQUE-4
IOOESNOTAFFECT_
....... _-_'-' _:-'1",- _--_ _i ABSOLUTE TORQUE_
M.#
:
.
;
: "
t -I..#.:::t,:-44;-I:I-jLE:=I:-=4_OYNAMIC:_-"
:." ?" :flT':._--:|::..'f_"_ to:_T':.: |:¢DIPTIflW:T'___---
-: -::I VALUES_L
__._
_4:'-_-'-,-----.-[-- ..!'_
0 --,
; 1 I i I ' ', I I I I _ F _
617-070-171
Table 3.. Single Bearing Rig Evaluation of High Temperature Bearing Coatings
SCA eoated shaft, TiC sputter Heavy wear and high friction 85N (19.2) lbs for
eoated foils after 263 starts !2 see at 75,000 rpm
Sintered silicon nitride shaft, Unmeasurable wear after 1000 10?N (24) lbs for
>200 KNOOP gold eoated foils starts, rig failed after 2934 30 see at ?5,000 rpm
starts due to shaft failure
20
OIL SUPPLY PASSAGE
SECTIONA-A
THRUST WASHER
TYP 6 PLACES
THRUST RUNNER
THRUST WASHER
!
Figure 17. AGT101 Hydrodynamic
Thrust Bearing Configuration.
plate assembly are made spherical. This con- Metering orifice design 448 kPa (65 psig)
figuration will permit the thrust washer to pressure
align exactly flush with the mating thrust
Design inlet temperature 82 C (180F)
surface of the thrust rotor. This arrangement
also will sustain the alignment through small Maximum oil discharge 121C (250F)
displacements of the housing or the shaft temperature
during thermal excursions in engine operation.
Oil flow (Thrust bearing 4.16 L/rain
only) (1.1 gpm)
The thrust bearing is designed to utilize
Total oil flow (Thrust 5.3 L/min
ATF-Dextron II lubricant which conforms to
bearing plus hydraulic (1.4 gpm)
SAE Specification SAE-J-311B. The oil supply
mount)
is fed through the same drilled passages used
in the original AGTI01 configuration. From In the static condition the thrust runner is set
the main supply duct, oil is metered through a up with axial clearance between both forward
2 mm (0.080 inch) orifice to the bearing and reverse thrust washers. As the engine
through six holes in the thrust washer. The accelerates during a start and forward thrust
hydraulic mount is also fed from the main builds, the rotor assembly moves forward,
supply duct in parallel to the thrust bearing. compressing the spring which preloads the ball
Oil supply parameters are shown below: bearing. The oii film thrust bearing is not
21
{HPI
actually loaded until forward rotor movement KW
7.
decreases the forward bearing clearance suf- 5-
ficiently to develop the supporting oil film.
The curve in Figure 19 shows the rotor thrust 6 o
MIN AXIALCLEARANCE
: _504 iN 5"
200"
FLUIDFILM
150" 4"
ffi
_50-
50.000 lO0.OOO
RPM 3"
0 __,,._._//////////////////////_ 2-
_50 BALL
REAHING
RANOLES
I. HALL
GEARING
AND
FLU'O
FILM
GEAR'N8
_!
FORWARD THRUST | SHARE FORWARD THRUST - 2-
NOTES:
I-
I. AXIAL CLEARANCE ' 0.004 IN
2. SPRING
RATE6250 LD/IN
GI/_T_It4
SPEEO, KRPM
4.1.2.2 Thrust Bearing Power Consumption
GOT.G78-175
Evaluation
Figure 20. Total Analytical Heat
Theoretical bearing power consumption is Generation for AGT101 Fluid Film
shown in Figure 20. An engine test was Thrust Bearing Cavity.
performed to evaluate this power consumption
and determine whether bearing scavenging was supporting evidence for the theory that exces-
sufficient. These test results,shown in Figure sive oil in the bearing cavity produced insuffi-
21 indicate that the apparent penalty due to cient scavenging and caused oilchurning.
the thrust bearing is much higher than pre-
dicted. It is believed that the higher test 4.1.3 Ball Bearing and Compressor Seal
results are an indication of insufficientscav- Desi
enging and the resulting churning that is 4.1.3.1 High Speed Ball Bearing Design
taking place.
The AGT101 ball bearing is a 15 mm 202
Another test was performed to evaluate series ball bearing designed to carry a maxi-
the effect of reduced oil flow on thrust bear- mum predicted radial load of 182N (41 lbs) and
ing power consumption. This test was con- a thrust load of approximately 1335N (300 lbs)
ducted at 70,000 rpm and the oilsupply to the at I00,000 rpm.
thrust bearing was separated from the hy-
The bearing was designed to meet the
draulic mount so that reduced thrust bearing
following conditions:
supply pressures would not affect the hydrau-
lic mount damping or stiffness. The results of
Speed 55,000 to I00,000 rpm
this test,shown in Figure 22, indicated that at
partial speed, the power consumption reduced Radial loads 42.3 to 182 N
substantially with reduced oil flow. This was (9.5 to 41 Ibs)
22
(HPI
KW
Thrust loads 311 to 1335N
3.0"
(70 to 300 lbs) 2.2,
2.9"
2.4"
1.8-
Lubricant Automotive transmis-
2.3-
sion fluid 1.7- ENGINE SPEED: 70.000 RPM
!
L/MIN
When the hydrodynamic thrust bearing was 2 3' 4' '5
OIL FLOW
added to the system midway through the pro- G|7_TLIT7
OUTER SHELL
RETAINING RING
2_
MATING RING 1410/ (43,401
i I I I I
1440C1
"_f "__', _
5O 60 70 80 90 1O0
SPEEO, KRPM
G87_7_tT8
23
durability standpoint. Rotor clearances as- hub, and static structures. At a constant idle
sembled into the engine will vary depending on speed where pressure effects are minimal, the
the effects of thermal and pressure distortion turbine clearance decreased by as much as
on the rotor support structure and on the rotor 0.46 mm (0.018 inch).
shrouds. These effects were measured during
actual engine testing in the metal engine test Once thermally stabilized, the turbine
bed using capacitance probes mounted in the clearance changed very little as a function of
rotor shrouds with metallic rotors. speed. The curve in Figure 25 shows the
variation of axial turbine and compressor
4.1.4.1 Metallic Engine Clearance Testing clearance as a function of speed. The com-
pressor axial clearance decreased by 0.30 mm
Running clearances were measured on the (0.012 inch) as a function of engine speed.
compressor and turbine rotor during metallic Half of this change was attributed to "flower-
engine operation. These data included clear- ing" of the compressor rotor due to centrifugal
ance changes during low speed operation due effects and the other half was due to pres-
to light-off thermals and clearance changes as sure/thermal distortion of the adjacent struc-
a function of engine speed under essentially tures.
isothermal operation at 871C (1600F). The
engine build clearance is established when the Based on these test results, the build clear-
engine centerline is vertical and the support
ances for the compressor on the metal and
bearings have no radial static load. When the
ceramic engines was established on a go for-
engine running clearances are measured the ward basis. The rationale for establishing the
engine centerline is oriented horizontally, and
compressor clearance is shown below:
the rotor supports are radially loaded by the
weight of the rotor assembly.
Compressor Axial Clearance
START TO OSITE
5O.OOO RPM, 871C [1600F)
OATAI
-15"
-0.38t - 4.1.4.2 Ceramic Turbine Clearance
-2'0 ' Analysis
24
desired operating condition. Further correc- The ceramic turbine build clearance was
tions were made for pressure induced struc- calculated based on the start effect noted
tural deflections resulting from differing during metallic turbine testing, plus similar
speedconditions. Table 4 showsthese correc- allowances used for establishing compressor
tions. build clearance. This information is sum-
marized in Table 5.
[MILS)
_' -0381 -15- STEADY STATE AT 871C (1600F)TIT. The analysis summarized above is con-
MAX TDT servative since it does not reduce rotor droop
E
-0.508 -20-
of the ceramic turbine rotor.
TIT = 1371C
TIT = 1174C TIT = 1281C (2500F)
(2146F) Idle (2337F) Cruise Maximum Power
Parameter Evaluated 50 krpm 65 krpm 100 krpm
25
Symmetrical design philosophy was used engine structural assembly. The other compo-
throughout the engine, and low cost, highly nents, the compressor housing, exhaust housing
producible materials were used for the metal- and inlet housing, are the main structures in
lie components where possible. the engine. These structures contain the pres-
surized gases within the engine, provide burst
The engine cross section in Figure 26 indi- containment for the rotating components, sup-
cates the metallic engine components in the port the engine at the mounting interfaces and
provide a reacting load path for the pressure
Table 5. Ceramic Engine Turbine loads generated within the engine.
Axial Build Clearance.
The design of the compressor housing and
exhaust housing was augmented by finite ele-
mm [ (inch) ment analysis to provide a stable support for
the engine ceramic and rotating components.
Thermal/Centrifugal/ 0.036 (0.015) Section stiffeners and gussets were designed
Rotor Droop into these components to minimize pressure
induced deflections.
Worst Speed Transient 0.0762 (0.003)
Worst Excursion 0.127 (0.005) 4.2 Engine Rotor Dynamic Development
Build Tolerance 0.051 (0.002) 4.2.1 AGT101 Rotor Dynamic History
Minimum Running 0.127 (o.oo5)
The initial AGT101 rotor system was sup-
Clearance
ported by an oil mounted ball bearing and a
Minimum Axial Turbine 0.762 (0.030) foilbearing. This initialrotor system configu-
Clearance ration, which includes a metal turbine for
26
COMBUSTOR SEPARATOR
HOUSING
TURBINE
DIFFUSERS
RBINESTATORS
ROTOR
INLETHOUSING
COMPRESSOR
HOUSING
GB7-O78-181A TURBINE
SHROUD
development purposes, is shown in View A of the frequency caused by rotor unbalance) and
Figure 27. The operational rotor system con- increased as the engine was loaded.
figurations with metal and ceramic turbines
are respectively shown in Views B and C of A waterfall plot of engine vibration during
Figure 27. acceleration, shown in Figure 28 clearly shows
the existence of gearbox excitation frequen-
Rotor thrust loads were transmitted to the cies.
support structure through the oil mounted ball
bearing. Rotor torque was transmitted to the A design was then introduced to isolate the
drive train through a sun gear mounted on the gearbox from the AGT101 rotor in order to
rotor shaft. The sun gear meshes with 3 eliminate gearbox excitation frequencies that
planet gears on a compound planetary gearbox may be causing rotor instability. To accom-
to provide a speed reduction of 37.143 to 1. plish this, the gearbox was separated from the
rotor by a splined quillshaft with the sun gear
Alignment and timing of the rotor mounted mounted on itsown bearings.
sun gear to the gearbox planet gears was found
to be important. Misalignment and mistiming Subsequent testing showed the near elimi-
contributed to the inability to repeat early nation of gearbox excitation frequencies.
successful engine testing. However, a subsynchronous frequency of large,
pulsating amplitude was present. As the rotor
Engine testing of the initial AGT101 rotor system speed increased, the amplitude of this
system showed that full speed operation could subsysnchronous frequency increased, causing
not be achieved because of high amplitude foil bearing failure consistently between
motion at the foil bearing that caused the 75,000 and 85,000 rpm.
rotor system to go unstable. This high ampli-
tude motion was subsynchronous in nature The cause of the detrimental subsynchro-
(meaning that its frequency was lower than nous rotor system excitation was identified
27
through a series of engine motoring tests. The placed by dummy components systematically.
engine was powered externally using a high F_gure 29 shows the sequence of rotor systems
speed air turbine starter so that the engine evaluated. As each of the aerodynamic corn-
bladed aerodynamic components could be re- ponents were replaced, the rotor instability
VIEW A
O.,_L
s.-- o,_.o..tEo / I _/ t
VIEW B
........ -
"_ COUPLIN6
uletl-zl VIEW C
28
PLANET 2 X PLANET GEAR UNBALANCE
RING GEAR GEARS RESPONSE
RESPONSE RESPONSE
RESPONSE
i
2OO0
O FREQUENCY.HZ
697-078-189 A
th{'eshold speed increased. This trend is shown foil sway space, foil materials and foil coat-
in the curve in Figure 30. The conclusion ings were varied. Impact testing was also
drawn from these engine motoring tests is that conducted to determine the foil bearing damp-
detrimental rotor system excitation was aero- ing at operating speed.
dynamically induced.
Impact testing consists of striking the
Since aerodynamic excitation will always rotor system in the radial direction while it is
be present, an investigation was made of ways rotating, as shown in Figure 31. The rotor
to improve the stability of the rotor system. responds primarily in free vibration of the
first mode. The decay rate of rotor subsyn-
Testing indicated that rotor system motion ehronous whirl is an indication of the damping
during unstable operation was conical whirl in the rotor supports. The results of the
with motion at the foil bearing. A detailed impact testing showed that the foil bearing
investigation of the foil bearing was under- has a relatively low viscous damping coef-
taken to determine if the stiffness and the ficient of approximately 2.0 Ibf-sec/in.
damping of the foil bearing, which affect rotor
stability, could be significantly improved. By extending the length of the foil bearing
and reducing the sway space, the instability
Tests were conducted in which foil bearing threshold speed was increased by I0 percent.
length, foil thickness, backing spring stiffness, However, foil bearing stiffness and damping
29
o.. 0.0500- 2.00-1
o,.
E ,_: BUILD 45 !
could not be significantly improved while
. ,.oo.-,RL
RASELINEABEoRB
° o:o°,,o
E
0.0375-
maintaining an acceptable foil bearing thermal
environment. Therefore, a more stable rotor
1.2 T_
system would have to be obtained by improve- _ 0.0250-
ments in other areas. i "_'_ E>: BUILD 45C I
,_ j_._,_o BOMM,
,UBB,NE
The stability of the rotor system was im-
_ 0.0125. "_MMY COMPBE
'- 0.111111. ".®_ , ,_ ,_----?,
proved by changing the rotor support con- 60 85 70 75 DO85 _o 95 ,oo
figuration. The ball bearing was moved for-
ENGINE SPEED, RPM x 1000
617.078-191
ACCELEROMETER
0iLLMOEUANT
_D OEFORILN
G l I
IIII?-OTO-ZTA "_
Figure 29. AGT101 Engine Motoring Testing showed that this new configuration
Rotating Group Configurations Tested. was sensitive to gearbox-to-engine alignment,
30
but that careful assembly yielded consistent, 4.2.3 Rotor System Test Results
stable operation. The resulting operational
rotor system configuration is shown in Fig- The current rotor system configuration
ure 32. with the ceramic turbine has been tested
through the entire operating speed range and
4.2.2 Current Rotor System Configuration its rotor dynamic behavior recorded.
The current rotor system configuration is The ist critical speed occurs at approxi-
similar to the operational rotor system con- mately 12,000 rpm and the 2nd critical speed
figuration with the metal turbine except that is not seen because it is highly damped. A 3rd
it has a ceramic turbine with a collet attach- critical speed exists at approximately 82,000
ment. To simplify assembly, the plated rpm. This 3rd critical was seen in the test
splined quillshaft was removed and the tie- data between 70,000 and 90,000 rpm. Testing
shaft extended into the gearbox as shown in has demonstrated that these critical speeds
Figure 33. The extended tieshaft has the same are of no concern to the operation of the
stabilizing effect as did the plated splined AGTI01 current rotor system configuration.
quillshaft. The 3rd mode in the current rotor system
ORIGINAL, PACF, IS
DE POOR QUALITY
THRUST REARING
31
/
THRUST BEARING
\
\
SHAFT EXTENSION
GB7-078-193
configuration is caused by the relatively low the bending critical speed would occur near
rotational stiffness of the toilet which has 82,000 rpm, which is the bending critical speed
axial slots cut in it for assembly. Also, the seen in current engine testing.
3rd mode rotor response at the foil bearing is
different in the horizontal and vertical direc- 4.2.5 Rotor System Analysis
tions indicating that the rotor system is whirl-
ing in an elliptical orbit. A rotor dynamic analysis was performed in
order to analyze the rotor system critical
4.2.4 Rotor Static Modal Determination speeds and the response of the rotor system to
Testing unbalance.
Static modal tests were performed on the The rotor dynamics model used in anal-
current rotor system configuration to verify yzing the current rotor system is shown in
analytical prediction and to correlate with Figures 34 and 35. The relatively low rota-
engine test results. tional stiffness of the collet is due to the axial
slots in this part and was calculated from
Static modal testing showed that a bending simple beam bending theory. The rotational
critical speed does exist in the operating speed stiffness near the curvic coupling was specifi-
range. If gyroscopic stiffening were addedp cally chosen such that the predicted bending
32
COMPRESSOR TURBINE
MASS: 0.0423 KG-SEC2/m t0.00237 LB/SEC2/INJ MASS: 0.0704 KG-SEC2/m _J0.00304 LO/SEC2/IN)
Ip: 0.000031 m-KG-SEC [0.0027 IN-LB-SEC ) Ip: 0.000041 m-KG-SEC 10,00354 IN-LB-SEC J
ID: 0.000026 m-KG-SEC2 [0.0225 IN-LB-SEC2) In: 0.000071 rn-KG-SEC
2 10.0_12 IN-LB-SEC2)
ECC: 0.0127 turn I0.0005 iN) ECC: 0.0127 mm (0.0005 IN)
A: 00EGREES /"'T'N
A: 180 DEGREES _
MASS MOOEL
r----f
r"----'--T-1 ' I
STIFFNESS MOOEL
STATION
NUMBERS
f J I I I I [ 1 I I
INCH -1.00 0.28 1.57 2.85 4.14 5.42 6.71 7.99 9.27 10.56
cm .2.54 0.04 3.98 7.24 10.52 13.77 17.04 20.29 23.55 26.82
AXIAL POSITION
TERMINOLOGY
critical speed matched the observed bending 4.2.6 Rotor Stability Analysis
critical speed of 82,000 rpm.
The dynamic characteristic of a stable
The rotor system mode shapes were deter-
rotor is to have low amplitude subsynchronous
mined by an undamped critical speed analysis
motion and the rotor supports are able to
and can been seen in Figure 36. The ist mode
positively dampen subsynchronous motion.
is conical whirl at the foil bearing and the 2nd
Improved stability usually occurs when there is
mode is whirl with more motion at the oil film
an increase in the forward mode log decre-
thrust bearing than at the foil bearing. The
ment, which is a calculated value from the
3rd mode shows the rotor flexing near the
rotor dynamic analysis. In the case of the
curvic coupling because of a relatively soft
AGTI01 with a ceramic turbine and collet
collet rotational stiffness.
attachment, the Ist and 3rd forward mode log
Unbalance response plots of rotor deflec- decrements are important.
tion and bearing loads are shown in Figures 37
and 38 and a whirl speed map is shown in The stability analysis of the rotor system
Figure 39 for reference purposes. Predicted shows that the difference between a stable
rotor displacements at the first and third and unstable AGT101 rotor system configura-
critical speeds are similar to measured rotor tion is predicted by a relatively small log
displacements. Although relatively large dis- decrement.
placements were predicted at the 2nd critical
speed, engine tests did not show large dis- Log decrement values for the Ist and 3rd
placements because the engine accelerated forward whirl modes have been plotted and are
rapidly through this critical and this mode was shown in Figure 40. Damping is present when
highly damped. the log decrement is greater than zero. The
33
TIESHAFT
(lOO.OOOLB/IN]_____ .
.....................
II OOO000 LB/INI _ L_
. < 1
I • .
000
IN-LB/RAOJ
<:_(1.000.000 LB/IN) COMPRE3SOR"'
'S,,N, ' O
ROTOR C)27
_ I, ,,_ IJ3Om-N/RAD
OIL MOUNT _ _ L,,_ 10.000 IN-LB/RAO
'_ I / OILFILM TUR ,NE
NON-REAM MAS.RL-__ 7-)7- THRUST 8EARING
current AGT101 rotor system configuration gas flow paths, structural support systems, and
has demonstrated consistent stable operation rotor configurations were also similar, though
to I00,000 rpm. differing according to the specific require-
ments of ceramic and metallic components.
4.3 Engine Development Evaluations
The metallic configuration engine was the
AGT101 engine development testing aug- first operational AGT engine. Featuring all
mented the engine design effort through ver- metal structural and rotating components, this
ification of engine design. This program uti- engine was limited to 871C (1600F) maximum
lized three basic test bed configurations shown turbine inlet temperature. The metallic
in Figure 41, each representing different engine was used principally for system devel-
stages of ceramic engine development. These opment prior to ceramic engine testing. This
test beds were used toward the development engine was used for rotor dynamic develop-
of a high temperature engine configuration ment, engine controls development, heat
capable of achieving the reference powertrain transfer coefficient determination, rotor sys-
design goals. tem evaluation, and low temperature regen-
erator development.
All three engine test bed configurations
were similar in design and function, and all The ceramic/metallic engine was a hybrid
required the same facilitiesand energies for engine with a combination of ceramic and
testing. These test beds shared the same rotor metallic components in the hot power section.
bearing system and regenerator system. The This engine, was an intermediate step in the
34
ceramic engine evolution, featuring ceramic The all ceramic engine featured ceramic
engine structures, metallic combustor and a structures, ceramic combustor, and ceramic
metallic dual alloy turbine rotor. The devel- turbine rotor. The operating temperature of
opment of ceramic structures as part of the this engine was limited by the stress-rupture
engine system was performed in this engine. properties of the turbine rotor material.
TOTAL _ ]
n_ 20 PERCENT COMPRESSOR
_i
--- -2.00
/
-0.72 0_14
SE. 4.42
_ 5.71 6.99 8.27 9.50
o_T,ESRAFT
10.84
]
79 PERCENT STRAIN ENERGY {S.E.JIN FOIL BEARINGSUPPORT
,oo _ I
/_ I _ -_ o_T,ESRAFT
-+.o.5o
1 ,.,,_
| 46 PERCENT
| 26 PERCENT S.E. IN THRUST BEARINGSUPPORT S.E,
t II PERCENT S.E. IN FOIL BEARINGSUPPORT ROTOR
0.00
't
,_ -+.,2 0:5_ ,:B5 s ,AL
pO4SI_S'2' " "
THRUST BEARING
-0.50 COMPRESSOR
GOl-O76-31A
Figure 36. AGT101 Engine Critical Speed Mode Shapes.
35
ROTORSUPPORTS
I
I
I
I
.... I- .................
I
I
I
I
% .... T ........ _
-
I
-{ ......... { .....
I I
I I
l I
I I
F_ .J ........
-t- ........ L_ ........
I
I
I
I I
I
0 { i { I {
0 20 40 60 80 IOO 120 140
Turbine inlet temperatures of 1204C (2200F) operation, fuel control operation, and rotor
were achieved. This engine was used to eval- dynamic development.
uate the characteristics of all ceramic engine
operation.
Because the ceramic and metallic engines
shared similar operating systems, the metallic
4.3.1 Metallic Engine Testing
engines provided a low risk test bed to evalu-
ate new design features before they were used
The AGT101 metallic engine saw extensive
in the ceramic engine. Examples of this work
use during the first five years of the program.
were the testing of new ECU software, light-
these engines compiled a total of 270 hours
off evaluations of new cornbustor configura-
and 720 starts. This experience was accumu-
tions, the evaluation of a new regenerator
lated during two types of evaluations, for
drive control, and evaluations of a new engine
engine mechanical development, and for ce-
air starter system.
ramic engine development. Basle mechanical
system development include the following ac-
tivities, engine operating procedure develop- Because the metallic and ceramic gas flow
ment, engine control unit (ECU) operation, foil paths were similar, metallic engine testing
bearing operation, regeherator drive system was used to improve the analytical methods
36
ROTOR SUPPORTS
266.89- 60-
222.41 - 50 ..................
---1 ........................
,,0
133.45- 30 ......... 1- ........ J- ........
88.96- ......... I-
I
I
44.48 -
O-
employed in the design of ceramic compo- rotors have been pretested to high speeds and
nents. Thermocouples were installed in the 871C (1600F) in a metallic engine before test-
metallic engine flow path to collect data on ing in a ceramic structured engine.
the heat transfer characteristics of the engine
flow path. This information was used to Significant in the development work per-
calculate heat transfer coefficients along the formed in the metallic engine were rotor dy-
flow path. Extrapolations were made based on namic engine testing and ceramic turbine
these data to simulate the ceramic engine blade vibration evaluations. Engine rotor
condition for improved analysis of ceramic dynamic development was discussed in Section
components. 4.2.1, ceramic turbine blade vibration evalua-
tions are discussed below.
Ceramic turbine rotors were evaluated in
the metallic structured engine. Ceramic tur- Turbine Blade Vibration
bine blade vibration was noted as a potential
problem when a ceramic rotor failed during As a result of early ceramic turbine rotor
testing in a metallic engine. Turbine blade tests performed in a metallic structured en-
variation was evaluated by testing an instru- gine, turbine blade vibration was identified as
mented rotor in a metallic engine. Ceramic a potential rotor failure mode.
37
(9 IST BACKWARD 0 1ST FORWARO _ 2NO BACKWARD [] 2NO FORWARO
40"
/
In those tests of S/N 001 engine, early vibration tests were conducted. In the first
generation sintered silicon nitrlde ceramic test, cold strain gages were located at the
turbine rotors were evaluated. These rotors point of peak stress for the fundamental vibra-
contained several defects which were removed tion modes, on the inducer and exducer por-
through extensive blade shroudline and back- tions of the ceramic blades as shown on Figure
face recontouring, and hand finishing. Con- 43. Then the rotor was installed on a mag-
sequently, the rotors did not conform to print netostrictive shaker and vibrated at the blade
dimensions. The first rotor was installed in natural frequencies to determine strain-to-
S/N 001 engine and operated to 97,300 rpm at failure.
871C (1600F) turbine inlet temperature before
a failure occurred. The second rotor, shown in Following this test, a similar straln-ffaged
Figure 42, failed at 62,000 rpm. Analysis of rotor was installed in a metallic structured
the rotor excursions during the failures indi- engine. This engine was then motored, forcing
cated that a sudden imbalance was imposed on ambient temperature air through the turbine
the turbine rotors which caused them to de- section, powering the engine through the blade
part from a previously stable orbit, in the resonant speed range.
second test the rotor failed at a speed known
to excite blade resonance. The results of this test, reported more
fully in Section 6.2, indicate that these newer
A test plan was developed to evaluate the generation turbine rotors have the room tem-
blade vibration problem. Two different blade perature strength and toughness to withstand
3B
0 1ST FORWARD • 3RD FORWARO
0.6-
0.6-
0.4
\
\ \
02'
i,----(9
blade vibration induced by the passing of the operation with 1149C (2100F) turbine inlet
blades through the stator wake. Analysis temperatures.
indicates that the cold condition is much more
severe with larger driving forces; however this Principal evaluations with this engine ad-
can be avoided in engine testing by limiting dressed the design verification of the ceramic
the speed of the engine without a flame in the structures, and for transient thermal strength
combustor. during starting. In addition, this engine was
used to induce the maximum pressure loads on
4.3.2 Ceramic Structure/Metallic Turbine the ceramic structures through operation at
Engine Development maximum speed and the collection of 1149C
(210OF) engine performance data.
The ceramic structure/metallic turbine
engine configuration was an intermediate step Analysis indicated that the highest stresses
in the evolution of the AGT101 engine. All of occurred in the ceramic structural components
the ceramic structures had been developed to during the few minutes immediately following
the engine test stage in the ceramic structures engine start. During early testing, precise
rig, however the ceramic turbine and ceramic control was exercised over the engine thermal
combustor were not yet ready for engine test- conditions and extended thermal transient
ing. A dual alloy turbine rotor and the metal- schedules were used during the start to mini-
lic diffusion flame combustor, slightly modi- mize the thermal shock to the ceramic com-
fied and incorporating a thermal barrier coat- ponents. The start transient for the first
ing, were used on an interim basis to achieve 1149C (2100F) engine test took 52 minutes to
39
CERAMIC PARTS
4o
ORIGINAL PA'CE IS
0t_ P.OOR QUAL/T'E
DRIGD, rAU PXCg Ig
DE _OOR QUALIT._
INOUCER
STRAIN GAGE
EXDUCER
STRAIN GAGE
GB7-078-184 97095-4
the remaining 20 hours of testing was per- ing this series of tests, improvements in inter-
formed on the engine. nal engine and regenerator seals were also
evaluated. The ceramic components endured
The ceramic engine components were in the full pressure conditions without failure.
Problems were encountered concerning the
very good condition after the completion of
the test. These parts are shown in the photo- durability of the metallic components oper-
graph in Figure 46. Neither excessive oxida- ating at the elevated temperature and high
speeds.
tion nor sticking at the ceramic component
interfaces were noted. The regenerator seals
4.3.2.2 Dual Alloy Rotor Integrity
did show significant distress though the core
and drive components were in good condition.
The dual alloy turbine rotor was designed
for short term operation at 1149C (2100F)
The successful completion of this test indi- turbine inlet temperature and was utilized to
cated that the ceramic structural engine as- enable ceramic engine development on an
sembly could endure the rigors of engine oper- interim basis until a ceramic turbine rotor was
ating conditions for extended periods. Con- available. The rotor was designed with a
fidence was gained to proceed with engine forged powder metal Astroloy hub hot-
testing to high speeds where component pres- isostatic-press (HIP) bonded to a directionally
sure loading and interface stresses were at solidified cast MAR-M 247 blade ring. Shown
their maximum level. in Figure 47, this rotor had provisions to cool
the bore of the rotor with air bled from the
Several full and near full speed tests were compressor seal, enabling operation at 1149C
conducted in the 1149C (2100F) engine. Dur- (2100F).
41
c IF)
1200
"70
2O0O
60O
1000 {
-30 --
D 400_ _..
- 20
500-
200m
I0
PREHEAT -
0 I I I I I I i I I I I I I I
O 5 10 15 20 25 30 35 40 45 50 55 60 65 70
TIMEIMINUTES)
Figure 44. S/N 002C - T4 Schedule for the First Ceramie Engine Test.
These rotors were used in all 1149C Both ultrasonic inspection techniques and vis-
(2100F) engine testing, including the 100-hour ual methods were used to examine the rotor
endurance test and the various runs to maxi- bond joints. These inspections indicated that
mum speed. During the course of this testing, most of the rotors had detectable bond joint
two dual alloy rotors failed. These rotors had defects, though whether these defects could
a predicted stress rupture life of 500 hours at cause a rotor failure was not known. More-
100,000 rpm with 1149C (2100F) turbine inlet over, the review disclosed that there was no
temperature. The first rotor failed due to effective proof test or NDE technique that
stress rupture of the east blade ring after 100 could positively weed out defective rotors
hours of testing at 67,000 rpm, and a short from the good rotors. As a result, the use of
time at 95,000 rpm. This failure was an dual alloy rotors was discontinued in future
indication that the blade crystal geometry was engine testing due to the uncertainty of their
less than optimum, resulting in a less than integrity.
predicted stress rupture life. The second dual
alloy rotor failure occurred during engine test- 4.3.3 Ceramic Engine Development
ing at 68,000 rpm and 982C (1800F). This
rotor experienced a separation of the blade The ceramic engine configuration incor-
ring from the hub. An examination of the porated an entirely ceramic hot power section,
rotor remnants revealed that the HIP bond including ceramic engine structures, ceramic
joint was discontinuous in several areas. combustor, and ceramic turbine rotor. The
evolution of this engine was the progression
This experience caused a review of the from the ceramic structure/metallic turbine
other dual alloy rotors in the AGT inventory. configuration as the ceramic turbine rotor and
42
Evaluation of the ceramic engine configu-
KEY MATERIAL SOURCE ration was initiallyapproached from a durabil-
I MAS -- MAGNESIUM ALUMIMUM NGK-LOCKEE ity standpoint. Engine performance was re-
SILICATE garded as secondary to insuring that the
2 LAS -- LITHIUM ALUMIMUM CORNING GLASS
ceramic structures were sound, that the
SILICATE WORKS
3 ROSN -- REACTION BONDED AIRESEARCH
ceramic turbine had sufficient life at temper-
SILICON NITRIDE CASTING CO ature, and that this system would operate as a
4 SAME AS 3 ABOVE
5 SN-50 SILICON NITRIDE NGK-LOCKE
i_, "=. . _; _ j
43
unit. The development of performance en- the ceramic component interfaces was not a
hancing components such as interpath seals problem. These structural components were
and the regenerator system, was performed in reused on a subsequent test.
their individual rigs until basic enginedurabil-
ity was established. This engine was rebuilt incorporating sev-
eral improvements in the combustor fuel noz-
Ceramic enginedurability testing was per- zle and regenerator system. The combustor
formed to identify the weak areas in ceramic fuel nozzle was thoroughly flow checked and
engine design and to demonstrate the capabil- tested in the combustor rig for carbon forming
ity of the ceramic engine system. To this end, tendencies. The regenerator core was fabrica-
the ceramic engine was tested steady state at ted from an improved MAS material with
1204C (2200F) and 60,000 rpm for 85 hours reduced thermal expansion. In addition the
until a failure of the ceramic turbine rotor inner regenerator seal was modified to relieve
stopped the test. The results of this test potential thermal interference at the cross-
provided much valuable information on the arm to outer peripheral interface. The test
durability of the ceramic components used in cycle was similar to the 85-hour test except
the engine. that a periodic shut down would be made to
pull and inspect the fuel nozzle for plugging.
The cause of the engine failure was traced
to partial plugging of the air assist ports in the After 12 hours of testing, another failure
fuel nozzle. The plugged ports allowed two occurred. This time the turbine rotor experi-
unatomized fuel streams to impinge with the enced a hub burst, most probably as a result of
wall of the pilot combustor, forming deposits premature stress rupture. The stress rupture
of hard carbon. When the carbon deposits properties of specimens cut from similar
broke loose from the combustor wall, they rotors were inconsistent and lower by orders
traveled down the gas path and impacted the of magnitude than the stress rupture proper-
turbine rotor inducer blade tips causing dam- ties of test bars of the same material. Fur-
age to the turbine and subsequent engine fail- ther rotor material development is required to
ure. resolve this problem.
The engine regenerator system showed The regenerator system fared much better
severe thermal distress. The magnesium during the 12-hour test. The regenerator core
aluminum silicate (MAS) regenerator core had showed minimal distress and thermal stress
indications of high thermal stress with thermal cracking was not significant. The regenerator
cracks emanating from the outer rim toward seals, however were again distorted. Follow-
the center. The regenerator seal wearface up work at Ford was performed to resolve the
coating on the hot side seal had delaminated seal distortion problem. This subject is dis-
about the inner periphery and the shape of the cussed more thoroughly in Section 5.4.1.
seal crossarm was significantly distorted. This
damage occurred during the course of the test Ceramic combustor light-off performance
and was not a result of the failure. has been marginal. During steady state oper-
ation at high temperatures, this combustor has
Follow-up testing in the combustor rig had provided consistent, reliable, stable operation.
indicated that the key to preventing fuel noz- However further development is required to
zle fouling was to maintain proper nozzle face improve the combustor system start and low
temperatures. Indications were that excessive temperature performance.
temperatures in the air-assist passages of the
nozzle caused fuel in those passages to coke The design deficiencies of this combustor
and plug the passage. have been identified and design improvements
have been made. This modified combustor
The ceramic structures survived the test design, reported in Section 5.3, has been fabri-
intact. Oxidation was minimal and sticking at cated in metal, tested in the combustor rig,
44
and tested in the metallic structured engine. 8RA_
r_ SPZEO
° ,oo._RPM
Engine testing of the enlarged bore combustor oYNo
_ ' lc°.
M_ESs°R 4TURBINE
has shown dramatic improvements in start and
low temperature performance.
_,L. '_ T3.6 I
4.3.4 Engine Performance Testing ,b "1 J TURBINEPISTONRING (7.86%)
I _.......................... "I"1 [--I= ,TERATIVE
tions less severe than the RPD, for the pur- DYNOPOWER 22.42 kW [30.07 HP] 22.43 kW (30.08 HP)
pose of seal development. SHAFTPOWER 32.4 kW (43.4 HPI
the engine performance model to establish the T3.R 7,5QC{13B3F) 762C (1404F]
overall leakage of the engine and determine 1170C (2139F) 1170C 12139F)
T4.1
the equivalent engine performance at sea level
T5.1 860C (1597F]
standard conditions. Using the measured data
TB.O 36QCI680FI 347C 1058F)
as a starting point in the engine performance
model, the internal leakages are varied until a7.0711.194
45
DUAL FLOW SEPARATOR SEALS WiTH
LP
TORGINE SHROUO SEAL
HP
HP
_v
ilTiT_IN
46
5.0 COMPONENT/SUBSYSTEM DEVELOPMENT
o Mass Flow at 29C (85F) 0.388 kg/sec 5.1.2.1 Compressor Aerodynamic Design
sea level (0.8542 lb/sec)
The aerodynamic and geometric impeller
o Stage Pressure Ratio 5 design summary is shown in Tables 7 and 8.
47
Table 8. AGT101 Impeller DesignGeometric DesignSummary.
Exit RakeAngle 0
48
10
65
i i I i
18 -- AIR ANGLE
/ 60
\ .... 9LAOE ANGLE
i°\ / \
/
/
,I
/
/ i \ \
\
_J
/ -__ 4o \ _MI __._
EAN
_'"
/
"/,, '
/
O
0 2O 40 60 60 100 \
\
/,i
RUB SHROUD _f
PERCENT FLOW
3O
6117.07666196 •
0 20 4O 60 60 IO(_
49
MM {INCNI
1O
f - /°°5-
•_o.8 \ HUB
i 1.0
''l1 0.04-
o.o+- f
_ 0.6
,,,, o.J=:
O.OI-- SHROUD
MEAN _
0.4 + O.O0 I I I l I
0 20 40 60 80 I00 O 20 40 60 80 I00
PERCENTMERIDIONAL
DISTANCE PERCENTMERIDIONAL
DISTANCE
601.OIE-_ GII7-078-205
Figure 56. Compressor Impeller Blade Figure 59. Impeller Normal Thickness
Surface Maeh No. Distribution- Mean. Distribution.
0.8
63.98 OEG
f
• / VM = 188
i551
HIS
Ipsl
f_ 1319 fpsl
f
W T = 344 M/S (1229 fPsl WT = 160 M/S
HUB
O.2
51.45 OEG
O 20 40 60 80 I00
6il7-07i1-203
PERCENTMERIOIONAL
DISTANCE VM : 110
(362
M/S
fPsl
5,.DE,
Figure 57. Compressor Impeller Blade
W T = 170 M/S W T = IN M/S
Surface Maeh No. Distribution - Hub. i55G Ipsl 1522 fPsi
II07-07&3_
/|" geomimass
= 1.086
Impeller splitter aerodynamic and stress
i avg
analyses were completed. To reduce a locally
1.1-
high splitter leading edge stress, the hub lead-
ing edge was moved axially forward from the
original position to make the edge more radial
(Figure 61). The circumferential position of
the splitter leading edge then was shifted to
1.0
I I I I | match the 50-percent mass flow streamline
20 40 50 80 100
across the entire blade height. This meanline
PERCENTMASSFLOW
shift was accomplished as shown in Figure 62
Gii7-076-204
for each streamline calculation. The reposi-
Figure 58. AGTI01 Impeller Design tioning was performed to eliminate a potential
Minimum s/a'geom. loss penalty associated with a non-uniform
50
CM (INCH)
Diffuser Design
|.8-
4.8- Based on the reference study and sub-
sequent design analyses, the radial diffuser
1.4- SHIFTED SPLITTER LE_ design consists of three vane rows. The first
row is a standard 2-D vane islanddiffuser with
a converging end wall followed by a cascade of
I°2_
two deswirl vane rows. During the analysis, a
tradeoff was made between the first stage
1.0-- (vane island) diffuser area ratio and the tan-
dem deswirl vane diffusion factors. The ef-
2.0 4
0.8--
0.6
1 0.2
I
ORIGINAL SPLITTER LE fect of varying the first deswirl vane exit
angle on the diffusion factor of each row is
shown in Figure 63. The firstdeswirl vane row
o ,o 2]o s_o
AXIAL DIMENSION. CM
o.82
GB7-078-207 z
== 1.5
CURVE EVEBYWHE
NORMAL TO MAiN \ _-"_\\\\\",_ i.o
GLAGEMEAR',NE
\ E 1.0
ROW 1
_-'_ _ ,'_'-[ FMEAN TANGENTIAL o.e
_.<_-\\\'_. _" I \ POSITION BETWEEN .- ROW 2
0.4
, I\ I"';-_;DE,'BEO
S,L,TTEB 0.2
ON STATION _
LINE_ J 0.8
• I_l .......... -_ n ISATISFIES
I',\--5G-50 MASS _ .MAIN BLADE 0.7
0.8
Ii\ ,uc,
ONSOB,ACE 0.5
'_ 0,4
0.3
51
inlet Mach Number was 0.225, a value pro- CM ilNI
5.0-
viding the vane island diffuser with an area
12.0.
ratio of 2.59 which is consistent with Garrett
4.5. R : ]1.163 CM 14,397INI
experience.
R 9.911CM 13.902INI
I0.0. 4.0.
Further design iterations resulted in a dif-
fusion system having a convergence over the I 3.5-
R = 6,712 CM 13.233INi
radial vane island of 0.05 cm (0.020 inch) from
&0-
the leading to trailing edge, and a trailing 3.0.
0.376CM [0.146INi OIA
edge thickness of +the vane island of 0.178 cm R : 5.860 CM
12.307
(0.070 inch) and 34 vanes. An axial projection 2.5-
8.0-
of the diffuser-system is shown in Figure 64 34 VANES
_.0,
and meridional flowpath in Figure 65. Dif- |
O0 1.0 2.0 3.0 40
fuser vector diagrams are shown in Figure 66. X -- AXIS.EN
o_0 71o ,'.o o_o 8_o ,o'o
5.1.2.2 High Flow Modification X-AXIS. CM
GlT,O7|.210
(INCHI
2ND DESWIRL VANE EXIT
n = 11,17 CM (4.397 INI
4.6-
.p--.-- FLOW ANGLE = 00EGREES
MACH NO = 0.105
CM 68 VANES
4.2
1ST DEGWlRL VANE EXIT
I0.0" R = 0.91 CM 13.901 INJ
FLOW ANGLE = 32.58 DEGREES
3.8-
MACH NO = 0.141
34 VANES_
3.4-
DIFFUSER EXIT
O.O ¸ R = 8.21 CM 13.233 IN)
FLOW ANGLE = 47.03 OEGDESS
3.0-
MACH NO = 0.225
34 VANES_,__
2.6"
DIFFUSER INLET
2.2- R = 5.86 CM 12,307 INI
", FLOW ANGLE = 72.8 DEGREES
\ MACH NO = 0.853
1.8-
', iMPELLER EXIT
R = 5.45 CM (2.145 IN]
4.0"
1.4"
2.0
0.6
1o o ,io 3o
i
-2.0
IINCHi
GB7_7_211
Figure 65. AGT101 Diffuser Meridional Flowpath.
52
72,81 BEG
1.2"i_/I
I.I -_
VR = 107.3 M/S
(351.9 fpsl
.=.
54.07 OE6
_ 0.6
• _ ,4 (151.8 Ipsl
IST OESWIRL VANE 2ND DESWIRL VANE 2NO OESWIRL _ELLER iMOOELEO FROM TEST 1 OATAi
LEAOIN6 EDGE LEAOINGEOGE VANE EXIT 0.2
O 10 20 30 40 50 60 TO nO gO 100
iilT-OTO-2]
2
PERCENT MERIOIONAL OISTANCE
667.076.213
Figure 66. AGT101 Diffuser Vector Diagrams.
Figure 67. AGT101 Modified Impeller
design levels, an analysis was conducted to Blade Loading's--Tip.
evaluate several exclusive and related modifi-
cations. Working within available hardware
constraints, modifications that added 0.02 cm
(0.052 inch) to the impeller tip radius, 0.019
cm (0.048 inch) to the inducer shroud line and 0.6
0.007 cm (0.018 inch) to the exit blade height
0.5
were analyzed to increase flow capacity and
work. A comparison of the modified impeller
blade loadings and loadings based on Test 1
(reference paragraph 5.1.2.3) data is shown in
Figures 67 and 68 for the shroud and hub
0.2
respectively. The loadings shown for this Test
i
1 impeller were modeled using tested losses
O. ------ MOOIFIEO IMPELLER INIOH FLOWEO AND TIP EXTENOEDI
and deviation. Figure 69 shows the modified "_ BASELINE iMPELLER [MOOELEO FROM TEST t OATA)
impeller geometry. I I I I I I I I l I
0 10 20 30 40 50 60 70 80 90 150
Based on the modified impeller geometries,
the stationary shroud and diffuser also were PERCENT MERIDIONAL DISiANCE
007-076.214
modified. Since Test I data indicated that the
diffuser minimum loss occurred at design inci- Figure 68. AGT101 Modified Impeller
dence, the original diffuser design criteria was Blade Loadings--Hub.
retained. In addition, since the match ob-
tained between vane rows I, 2, and 3 showed
good performance, a decision was made to 5.1.2.3 Aerodynamic Testing
modify only the Ist vane row to accommodate
the larger impeller and retain the 2nd and 3rd Compressor development testing was con-
vane geometries as designed and tested. To ducted on test rigs suitable to aerodynamically
accomplish this, vane row I was increased in and mechanically evaluate the impeller, dif-
height, and the vane height was linearly con- fuser, VIGVs, inlet plenum and compressor
verged to match vane row 2. discharge airflow path.
53
lINCH]
2.3,
MODIFICATIONS i_
2.1 DIFFUSER
CM _'__! , DRIVE TURBINE
1.3 "
I BASELINE /
1.1-
G87,078-216
54
can be achieved. Instrumentation is of a size 0,60-
measured.
w N 0.65-
I
Two compressor stage tests were con- 0.65" w_mTEST 1
ducted on the AGT101 compressor. During
0.65 --TEST 2A
Test 1, compressor flow and pressure ratio
were below design intent. Based on Test 1 3,50"
0,80
0.50
,-,I
0.70
] 0.70 " " '_ ""
_--- _ TEST I
0,60 Z
0"65t
_ 0.55 0.75.
0.50
TEST 2A
0.65
70 - - ,_,_,,
-
2.50.
_ 3.00
I,- ,,_
2.50
1.5050.-..,---.._,,,_,,
-,,_
2.50'
'_ 1.50
1.50
"'150
50
ILBM/SEC]
0.10 0,30 0.50 0.70 0.90
GII7-0711-217 STAT,ON
RAT,NO CORRECTEO
_NLET _'OW
607..076-219
Figure 71. Full Stage Compressor Data, Figure 73. Full Stage Compressor Data,
lGVs Open. IGVs = 70 Degrees.
55
0.102 mm (0.003 to 0.004 inch) as designed. STATIONARY
STRUT
Test data indicates the following:
X I =0 X=O
o Design pressure ratio and flow were
achieved / r P,VOTPOINT
Development testing on compressor stage This problem was resolved, based on prior
hardware encompassed inlet guide vane (IGV) Garrett experience, by introducing a minimal
acoustic evaluation. The IGV test rig is shown disturbance in the flow field. Flow tabs, as
in Figure 75. shown in Figure 76, were installed on the fixed
56
t30 [ I !
FLOW RATE = 0.131 LS/SEC I
IGV ANGLE = 65 OEGREES
110- _-
- t20_,
tOO-
--JTNOUT
F=W
TABS
gO'v--WITH FLOW TABS
GD7_7_223
GB7-078222 4
P72492-8 Figure 77. Inlet Guide Vane Test Results.
57
217.2 MPa 191.7 MPa
(31°5 KSII 127.8 KSI]
10
G87-078-224
blade/hub interface. Calculated blade fre- A 3-D elastic stress and vibration analysis
quencies are shown in Figure 79 and the first was performed on the final splitter configura-
four mode shapes in Figure 80. The first tion. Results are provided in Figures 81 and
vibratory mode is at 3.5E (where E represents 82. The splitter stress levels are similar to
the rotational speed) at 100-percent speed. the levels in the main blade. Frequency
Experience has shown that impeller blades are analysis of the impeller splitter blades shows
relatively insensitive 1_o distortion related potential interferences of the first and second
excitations when the first mode frequency is vibratory modes with the IGV excitation. This
above 3E. The first three blade modes will not analysis also shows physical location on the
have interferences with 17E IGV wakes in the airfoil where the maximum vibratory strain
operating range. With the relatively long flow would occur for each of these modes. Since
space between the IGVs and blades, higher these modes occur at part speed, the blade
mode excitation is not expected. steady-stress level and metal temperatures
will be significantly lower than the levels that
Exducer region stress levels have to be exist at the 100-percent speed mechanical
controlled to provide adequate rupture life. design point. Using the stress and tempera-
The combination of 614 m/sec (1872 ft/sec) tip ture values that exist at the peak vibratory
speed and 50-degree backward curvature re- strain location for the predicted speeds of the
sults in a maximum elastic stress at the exit interferences, the analysis shows that the al-
of 214 MPa (31 ksi) and an adiabatic wall lowable vibratory stresses of the first and
temperature of 190C (374F). second modes respectively are 51.7 and 69.0
58
17E INLET
GUIDEVANES R
30-
L__x /
25"
IOE
_20-
4E
1ST MODE
5
2E
IE
O
0 25 50 75 100 125
SPEED,PERCENT
667_7&225
!
VIEWJ
isotherms for the 29.4C (85F) day design point.
These stress levels are consistent with Garrett SE:200 / I SF = 2.00
RPM = 100,000
experience on similar aluminum impeller de- R RPM=,OO.OOO
/ /
signs. A life summary is presented in Table
I0.
An aluminum (2219-T6) and titanium (Ti-6- Figure 81. AGTI01 3-D SplitterElastic
4) impeller were mechanically evaluated to Stress at I00,000 rpm.
59
173.9C
I
5TH MOOE
4TH MOOE
t
i
I
3ROMOOE l
2NO MOOE (INLET6UIOEVANES(
I
1ST MOOE 8E
8E
4E
2E
25 50 75 100 125
SPEEO.PERCENT
137.8C
116C 1280F)
Figure 82. AGT101 Impeller Splitter 1240FI
Campbell Diagram.
15
687-078-230
6o
Table 10. AGT101 Impeller Life Summary (-30
Material Properties).
BR - 0.85 (UTS-3a)
aAve Tan
•--"-] I
-.-- {0.0056INI
0.,4M. j/ // /1
,//"
2 10,340 10,427 10,411
3 12,341 13,108 13,138
4 15,172 16,858 17,127
5
J. ,
17,194 18,467 18,681
6 18,201 22,256
7 22,174 24,877 25,277
61
MODE1 FREQ[HZ) = 4681
i
R
-- X NORMALMODESHAPE
l NORMALMODESHAPE
Ge7-079-233 "_p _,
Figure 86. AGTI01 ImpeLler Blade
Vibratory Mode 1.
Figure 87. AGT101 Impeller Blade
redesign of the impeller was initiated to im- Vibratory Mode 2.
prove producibility. The efforts regarding
these studies are discussed in the following Results show (Figure 97) that the ductility
paragraphs. improvement goal was successfully met.
Tensile strengths, as predicted, are lower than
5.1.5.1 Material Evaluation - Powder Metal the baseline data but continue to exceed
Aluminum AGTI01 design goals. Properties at elevated
temperatures, particularly above 288C (550F),
Material characterization and evaluation were observed as less sensitive to TMP vari-
of the ALCOA AI-Fe-Ce powder metal (PM) ables, as evidenced by the convergence of
aluminum continued. Baseline screening tests property levels at 343C (650F). Comparing
on sub-size pancake forgings indicated the the tensile strength of PM AI-Fe-Ce with two
material had the capability to exceed the of the high-strength aluminum alloys com-
design goals (Figure 96). Based on these early mercially available (A2219-T6 and A201-T7),
evaluations, component size pancake forgings shows it to be superior even after the 1000-
were procured 11.4 cm (4.5-inches) diameter hour exposed condition (Figure 98). Stress
by 7.6 cm (3 inches) thick. These forgings rupture capability of the alloy also is signifi-
were thermomechanically processed (TMP) cantly better than the two commercial high
specifically to improve alloy ductility. strength alloys(Figure 99).
52
34E
DIFFUSER
48
MODE 15
17E
32
0 o
O 25 5O 75 ! O0 125
SPEEO, PERCENT
63
Figure 91. Strain Gaged Impeller Blade.
GB7-078-239
64
loo.OOO RPM AT TEMP
100 PERCENTRPM = lO0,O00
IKsll
DO
MPa
17E 5O0-
\
AS-FORGED
=
IOE
9E
BE
16
6E
5E
4E
3E
2E
IE IOO'
O.
0 25 5O 75 100 125 10
SPEED, PERCENT
607-078-240
0
75 200 400 5O0 800 1000 IFI
Figure 94. AGTI01 Titanium Impeller
Campbell Diagram Excitation Source.
! I
MEASURED 1DO 50O C
LOCATION BLADE STRAIN (_EI
I 6 229 GB7.078-242
t 8 493
Figure 96. Tensile Properties of Forged
2 3 224
ALCOA PM AI-Fe-Ce.
2 9 291
Ti 111.4±66.9
AL 71.7+_42.1 MPs
MPa |10.4+_6.1
(16.6-+9,7 KSII
KSi} I AL ALUMINUM
Three maximum power design point vector
GB7-078-241 diagrams were evaluated with the engine driv-
Figure 95. Strain Gage Test Results. ing cycle. The three turbine designs were
65
fKSli IKSII
8O 15
MPa
500-
80 i ''%"
70 TM \ 7O
! • MOFIf)IEOTMP
\i
I ' -- 6O
5O
%.
_ %/1
BASELINE
DATA I0
0
• -......t"
_"-_ BASEL
DAT
4O
DESIGN
13O
MODIFIEDTMP
3O
MOOIFIEO
TMP
/\ _2o
2O 2O MODIFIED
TMP- --
i ', I BASEL
I0
I0 10 I DAT
O
o "[ .... "'"lT
0
75 200 4OO 000 80O 1000 IFI 75 200 400 600 8iX) 1000 IF) 75 200 400 600 800 1000IFI
i !
,_o _ c 1Do _ c ,_o _ c
TESTTEMPERATURE TESTTEMPERATURE TESTTEMPERATURE
GD7-07i1-243
[KSII
90
I
MPA
509-
70'
co,! ! [
5O Mra IKSII
698.5 100
ALCOAAI-Fe-Ce
I
4O ALCOAAI-Fe-Ce
[1000-HOUR
EXPOSURE) (FORGEOl
k=-
3O i (FORGED)
A-Z219-TB
69.O 10
\'
20 ¸
_'_ A-2219-T6
100.
•....-"A-2O1-T7 A-2Ol-T7
10
0
T = RUPTURE
LIFE. HOURS
75 200 400 600 800 1000 {FI
! I
16 17 18 19 20 21 22 23 24 25 26 27
100 50O C (T + 4601120 + LOGtJ X 10.3
TESTTEMPERATURE GB7_7&2_
6D7_7&244
66
IKSll
MPA
tOO TENSIO'N/TENSION R = 0 A = I
600.
80
24C 175F1__.
60
=ffi 1,3
Z
0 SLE BLADE
40
Z
1.2
;..,--...
2O 232cf450FI
100- 0 AGT TEST 2A
1.1
0
lo2 io_ Io4 ,o5 I@ Io7 loS
1.0
CYCLES TO FAILURE NF
O.S
687_T&21
0.8
0.6
0.7 O SLE BLADE
- .'._.._
0.5
O,§ _ AGT TEST 2A _T_
0.4
Q 0.3
_. 0.4
• 0.3 G|7_?B-249
67
+ 70_
÷60 0.60
÷ 50
>VIA _ MAX
.40 0.50
= V/Ac_HIGH .J
I.-
+20 o.4o
.J
E uJ
I--
+10
.J
_"
X
Wd
0 o3o
O -10
I.- X)"
wl-
O
_" -20
O I o. o I-
-30 --d i
O
_10:
o._o _
O.O0
0.88
>-
U
Z
uJ
LL
o..6 1HIG
I,I,
LU
.I
<
I-
O 0.84
I-
-<
LU
I-
L4
). 0.82
OPERATING PE RCENT KW
CONDITION P/P)T-SYS N_ I NOMINAL
hp
© MAXIMUM
THROTTLE
CRUISE
1.88
1.78
5,_.0
67.3
I
i
18.0
13.4
_ o.78 15.7
( 4-28 100.0 135.0
I 21.0
J I POWER
MAXIMUM 100.7
0.76 I
1.0 2.0 3.0 4.0
GB7-078-282
68
II,
a = 72 35 . _ = 72.57 ,
"qJ_t_ = " R,:'_ 2.6356 IN /3- 4435
•+. O,oj'Z__,+_ I_,._/3 -15.48 , ._
,,i+++,.3>
"_ - o.+,
_'-.IV"j,,,,+++.;, . _ jW,A,, :o.m
........ I _=r + " +I 32 "qll_/ L"'_ /3 = .60.02
v,,,,%,= ,.,.=:,+, I t. /" • _ I I ____. ,-.. +m.o
o,__ @ -
WU/A'cr - --0.786
+ o,. 73,06
._ 69
Table 12. Turbine Design Point Cycle Conditions Sea Level, 29C (85F) Day, Maximum Power.
Dual Alloy
Ceramic Metallic
APT/PT)Exhaus t, Total Pressure Loss From Rotor Exit-to-Regenerator Inlet 0.0607 0.0312
APT/PT)Inle t, Total Pressure Loss From Turbine Duct Inlet-to-Stator inlet 0.010 0.010
70
0.110
CM IN
5,0 0.1oo
12.0 •
0.090-
I0.0 - 4.0
3 - STRUTS
2.0
0.080
4.0. _ COMBUSTOR
EXIT PLANE U6
I _ 0.050
/
2.0, ----- FINAL MOOiFiCATIOI_
_ O.04O-
O- 0
-2.0 -1.0 0,0 1.0 2.0 3.0 4.0 (INCHESI
0.030-
, i i t
0 50 I00 150 200
MD, mm
GB7-078.289
mm INCHES
SECTtON A-A
Two stator vane profile designs were com-
•_ (T,P
NES,ONI pleted. The baseline design is based on a
o_. o14 016 INCH trailing edge thickness (normal) of 0.508 mm
i
(0.020 in) and a fillet radius of 0.762 mm
0
(0.030 in). The design is consistent with
mm INCHESj previous turbine designs used for the specific
10- o.4-1 speed correlation (i.e., no additional aero-
C = 31.623 mm |1,245 INI
dynamic performance penalty is required).
o2-1 This profile, presented in Figure ii0, was
based on the selected vane number of 19.
Vane suction and pressure surface velocity
O- 0.0 I
distribution is presented in Figure 111 with the
end-wall contour established from the inlet
.o.2-I duct optimization. The second vane profile
i SECTION B-O was designed to facilitate tooling for an injec-
i INUe,EG,ONJ tion molded integral vane ring. Trailing edge
-10" -0.4 !
o o_ O;A O]S 1.4
thickness was increased to 0.762 mm (0.030 in)
INCHES
and the fillet to 1.220 mm (0.050 in). In
0 1IO i
20 !
30 mm
addition, the entire pressure surface and a
6B7-078-2"68 portion of the suction surface were modified
to straight lines, as shown in Figure 112. The
Figure 108. Turbine Inlet Strut effect of a linear pressure surface on the vane
Sections [Modified NACA 16-201 velocity distribution is presented in Figure
(tie = 0.30)]. 113.
71
LINEAR PRESSURE SURFACE
/ _// \ ,= 7o.o,,7.
/_t_. R= 90.6043 mm R= 70.9117 mm
y/OR
I
I /
///
/ I
T_ESS
19 VANES
= 0.508 mm [0.020 'NI \\
_--
/
//I
///
,/_ T.E. NORMAL THICKNESS
: o.761
,. Io.o3o
"-
,N,
\
\ \
\
6D7.076-Z92
GO7 -076-2'D0
Figure 110. Ceramic Turbine Stator Figure 112. Ceramic Turbine Stator
Profile Design. Profile Design.
I i I I I i I I
bINLE T _ 11.684 mm
1 ] n_9o..o_.. \ l R:----,'. 1
o
I.O[ / |3.5671INI I
13.5671INI
_ 10
19 VANES / R 709117 mot INLET FLOW ANGLE = O DEG
/ /Io VANES ' INLET FLOW ANGLE = OEG
J _12.7918IN] I
•-"l F"-o.2s7s
iN _'.'_
5 o.s
_, 0.5
/ _ _--_-O_,G,N_L LOAO,NG
- - _- LINEAR' PRESSURE
G _ "''" "-""
O ! SURFACE
O 10 20 30 40 50 60 70 80 90
0 10 20 30 40 50 80 70 80 90
PERCENT MERIOIONAL OISTANCE
PERCENT MERIOIONAL OISTANCE
mlT471-MI
M7.071i-ZI3
Figure 111. Ceramic Turbine Stator Figure 113. Ceramic Turbine Stator
Velocity Distribution Velocity Distribution (Linear Pressure
(Baseline, 19 Vanes). Surface, 19 Vanes).
72
b
_ b = 6.5405 mm
• _ _ 10.2575 IN] ,,
2.5 ? I / , -.i,,,I _ b = 7.2136 mm
/ I It " z ', ', {0.2840 IN]
aT= 50.9442 mm It lii I \
12.6355 IN) \ J I %
\ nT = 61.1226 rnmi
50 2.0
0 0 / i I I I I I i i I i i
0 0.5 1.0 1.5 2.0 0 0.5 1.0 1.5 2.0
Z. IN Z, IN
I I I l Ij I
0 _ 25 50ram 0 25 50nlm
Z. mm Z. mm
687-078-294
radial turbines are similar. That is, in the hub 5.2.2 Turbine Aerodynamic Performance
region the losses are low (due to lower loading) Testinl_
and progressively increase to about 80-percent
blade height, and then are fairly uniform to The test rig, shown in Figure 119, is a
the tip. Velocity distributions for the rotor double overhung assembly supported by two
are shown in Figure ll7. The velocity distri- angular contact ball bearings. During the
bution for the ceramic and metallic rotors are turbine and rig design effort, an investigation
similar at shroud, mean, and hub streamlines was conducted concerning off-design perfor-
except in the inducer area where the higher mance mapping, particularly accurate perfor-
inducer loading of the metallic rotor is evi- mance measurement at the idle-cruise regime
dent. of the CFDC. A summary of the investigation
and subsequent impact on the cold turbine test
5.2.1.4 Exhaust Diffuser rig design is outlined below.
For the exhaust diffuser, additional calcu- The aerodynamic analysis has shown cold
lation stations were added to the rotor flow turbine rig power requirements at maxi-
solution, since the velocity distribution into mum power of 19.3 to 20.1 kw (26 to 27 hp)
the exhaust diffuser is strongly dependent on with a temperature differential across the
the rotor exit radial swirl and associated loss rig of 98-107C (208-224F). The power
distribution. Both uniform and non-uniform level drops to 0.56-2.38 kw (0.75-3.2 hp) at
inlet conditions were evaluated. The current idle-cruise and the temperature differenti-
configuration is shown in Figure 118 for an al decreases to 3-19C (37-67F) for these
area ratio of 1.75. conditions. The kw/rpm ratio (hp/rpm)
73
b
CERAMIC ROTOR
13 BLAOES.
AXIALLENGTH: 39.370 mm (I.5,5 INI 13 BLADES,
Ut = 701.04 M/SEC 12300 FT/SECI
70 I I -I I i _, TIN = 1371C [2500F}
m" 60 _-SHROUD STREAMLINE- A_IAL LENGTH = 39.370 mm 11.55 IN]
.J f
¢3 50 I MAXIMUM POWER
Z f
<_ 40 /,-
w " 30 METALLIC ROTOR
,< (3 20 IMOO IJ
ma 10 13 BLADES
Ut = 040.08 M/SEC 12100 FT/SECI
% TIN = 1149C (2100F)
AXIAL LENGTH = 39.370 mm (I.55 IN)
7O MAXIMUM POWER
I I I I
60 _ MEAN STREAMLINE --
-i
so l I I SHROUD STREAMLINE
40 f4
1.10 i
_SUCTION
!
uu" 30
1.00
10 -"
0.80
_ 0 _
0.60
7O <
I I I I ' • 0.40
uJ" 60 ----HUB STREAMLINE--
-I LU
50 i >
Z
f F- 0.20 SURFACE _------ J •
<_
_luJ
4o -'>l
w
2O ¢ 0.00
' 0 -0.20
0 10
MEAN STREAMLINE
20 30 40 50 60 70 80 9O lO0 1.00
PERCENT MERIDIONAL DISTANCE o_
I
gi1_178-_6 Lu
m 0.80 I
Figure 115. Turbine Rotor Blade Z 0.60
Z f .._
Angle Distribution. (J
< 0.411
SHROUD 1_
ql uJ
> 0.20
../"
k-
3 0,00
8O
i,r
-0.20 J
<
40 z
_n 0.60 o-
i x
WITHOUT T E % < 0.40
2O "LOCKAC
E w
> 0.20
HUB 0
WITH
BLOCKAGE 'I
T E
_
,
r-
<
BJ 0.00
Figure 116. AGT101 Rotor Radial Figure 117. Turbine Rotor Velocity
Loss Distribution. Distribution.
74
MAXIMUM POWER CONDITION
Z - AXIAL LENGTH• mm
SURFACE MACH NO
50 75
0.56
5.70 I
G"
,* Jl'°'" ,11
•
5.50 _UMP -- .j -
DIFFUSER
0.50 It IIN2I - EXIT "
5.00 125
CM2
10 t _---.._
4.50
-9O
4.00 .I_
DIFFUSER
-8O
3.50 _--AREA RATIO_ --
_ 0.38 /I - 1.75 I 0,
"'..
',..
,," b,_ k /- 75
I- AelAi - 1.75 I
"',',
b
oL' I
Un"
0.,jK
__ UNIFORM
PT.TT
NONUNIFORM
AT RMS
iNLET
RADIUS
INLET
CONOITIONS
_.
N_
I/ L . • l °= I ,; jL
50
"---.,_
CONDITIONS
\
°20 / "5oRs = 11.713 INI
0.16 _..__. _ _ ---I_ _ 25
7,0
0.13 [
0 10 20 30 40 50 80 70 80 90 100 RR = 21.3537 mm'm'm'm'_
°'e° 1.r" 2.0 2.5 3.0 3.3 3.5
10.8407 INI
PERCENT MERIDIONAL DISTANCE Z - AXIAL LENGTHIIN)
697,078-299
ratio varies from 3.728 x 10 -4 (5 x I0 -4) - The high speed, direct-coupled, torque
at maximum power to a low of 2.237 x meter represents the instrumentation
10 -5 (3 x I0 -5) at the idle condition (see with accuracy both for high and low
Table 13) power mapping (mfgr., Torque Meters
Ltd., Northhamption, England)
O Preliminary results of the heat transfer
The platinum resistive temperature
analysis of the cold turbine test rig indi-
sensors provide secondary or backup
cates heat transfer losses could introduce
measurement of performance and pro-
significant errors. Revisions were intro-
vide an important reference for the
duced to the test rig design to provide
temperature surveys at various points
insulation both internal and external to the
in the turbine system.
rig, and to introduce conduction heat
transfer barriers where possible o The combination of direct coupled torque
meter and platinum resistive temperature
O The survey of the industry for precision sensors as backup provided a desirable per-
instrumentation confirmed the availability formance measurement system to assure
of platinum resistive temperature sensors design goals and to properly assess CFDC
and direct-coupled, high speed electronic mileage estimates during the cold turbine
torque meters with the desired accuracy mapping program.
75
COMBUSTOR EXIT TT -6 THERMOCOUPLES
@ - 3 ROSEMONT PROBES
TRANS,T,O,
O°CT PS HUB SHROUO
@TO@
ROTORSRROUO
@,o@
PS HUB L
ROTOR EXIT PS 8 KIEL PROBES
0
@
EXRAUST.O_.FUS_ PS HUB SHROUD
_TO_
O,_F,SER._T
BE_ PS HUB SHROUD
REGENERATORiNET TT 9 THERMOCOUPLES
J
;!: oo,
/
o.,,.,& ....,.o.,o
® -3 ROSEMONTPROBES
"ASSUMED
BEARINGTEMPERATURE.
MECHANICALIN_RUMENTATION
VIBRATION. OIL FLOW.
OIL TEMPERATURE
TORQUE
TORQUEMETE_)
©
GB7-076-299
76
Table 13. AGT101 Cold Turbine Rig Operating Conditions.
4m
Maximum Cruise Cruise Maximum
- Parameter Power No. 1 No. 2 Throttle Idle
Note: Gamma effects not included will alter results by few percent.
transfer effects. Speed then was set based on Figure 120 shows the unit installed in the
inlet temperature, and inlet pressure (for a test facility.
given pressure ratio) was adjusted to obtain
the desired turbine Reynolds number. This A series of cold rig tests were conducted
procedure was followed for all performance to aerodynamically evaluate the baseline
tests and data records obtained after system ceramic configuration (as represented by the
stabilizationfor approximately 10 minutes. Astrology rotor). Baseline ceramic cold rig
77
....... - #,._,_ ,- i_i/
0.00
1985
0.86
0.84
P-
OPERATING
_ o.82
CONDITIONS % N/,yl8
O IDLE I 53.4
__ 0.80
O IDLE 2 58.6
_" 0.78
CRUISE 1 62.4
__ MAX
0.72
POWER___
OESIGNt
0.70
3 4 5
COLD PRESSURERATIO
607-078-303
78
angle in Figure 123. Results of baseline MM liNI
ceramic tests (indicated by square symbols) 75, 3.0
are compared with metallic turbine test data
(circles) and an average curve. The additional
data confirms that the exhaust system loss
2.0
characteristics are low and decrease with in- 50.
r, I.oi ill I
.- ....
ill/ /
n_-_x_ B I
-o-.,,,
I .LJ
CERAM_C_
I --
I I I
Gll7-076-306
IO 20 30 40 50 60 70 80
Figure 124. AGT101 Metal Dual Alloy
a M, DIFFUSERINLET AVERAGESWIRL ANGLE.OEGREES Wheel - 13 Blades, Conical Astroloy Hub.
617-079-305
79
IDLE CONDITION
• N = 55.000 RPM VIBRATION FREQUENCIES
o_ • TIT = 1689C (1993F) 100"/, RPM - 100,000
_: 32
U 9E
I / I /10E
Dual Alloy Turbine Wheel
16 jf'_SE
KSI MPa
I 6E
ilOi 68.947 I 5E
12Oi 137.805
1301 2OO,942
f40i 275.790
(50i 344.737
(68i 413.685
i I I i _ !
i701 482.633
0 25 50 75 100 125
fool 551.550
fOOl 62O,528 SPEED, PERCENT
Gli7471i_10
(IDOl 669.475
(168,51 1.2'99,681
_,,__1_ PLETH INTERVAL =1168; KMIPI' 5.2.3.2 AGT101 (1149C_ 2100F_ Dual Alloy
Turbine Rotor Fabrication
Use of the dual alloy rotors was discon- Rather than compromise the turbine tem-
tinued following a rotor failure. Subsequent perature capability and performance, a mate-
careful inspections of the bond joint between rials mix or dual alloy fabrication concept for
blade ring and hub led to the conclusion that the radial turbine wheel was preferred.
the bond joint was not sufficiently reliable to Materials selected for the dual alloy wheel
continue the test program with the dual alloy fabrication are a cast MAR-M 247 bladed ring
rotor. with directionally solidified (DS) inducer blade
3o
ISOPLETH INTERVAL = 2
RPM = IO0,OOO
I-.-zDELTA[YI Lc OELTAIY)
MODE I FREO = 7679 Hz MODE 2 FREQ = 15448 Hz
l
k
OELTAIY) mL._,z DELTAIYi
MODE 5 FREQ : 25818 Hz MODE 6 FREQ = 31660 Hz
G87-078-311
81
Table 15. Dual Alloy Turbine Wheel Design Parameters.
Number of Blades 13
82
ORIC_N.IL PA-G_ 1_
OF. POOi<. QUALITT_
77848-4
Figure 131. As-Cast AGT101 Bladed Rings and Machined Dual Alloy Wheel Assemblies.
Exposed edges of mated assemblies were Solution I079C (1975F)/4 hrs/rapid argon
brush nickel 0.005-0.010 mm (0.0002-0.0004 cool
inch) plated and all parts were then cleaned plus S71C (1600F)/8 hrs/AC
using Garrett developed procedures. These 972C (1800F)/4 hrs/AC
include a sequence of steps starting with vapor 649C (1200F)/24 hrs/AC
degreasing followed by MEK solvent, HCf solu- 760C (1400F)/8 hrs/AC
tion, distilled water, and Freon rinses. The
mated assemblies were hermetically sealed
using a vacuum brazing technique. Bond Zone Evaluation t
83
Q
5.2.4 Ceramic Turbine Rotor Redesign
Figure 133. Microetched Cross Section Detailed stress analysis of the ceramic
of AGT101 Dual Alloy Wheel Test Specimen. turbine rotor is discussed in paragraph 6.2.?.
• a "°* • e'IP _
" L° "
• q e
" go
BRAZE
• " 2 ..
. . .
.. °, .,.
• .
..
.OF POOR QUALITY
° •
UNETCHEO 50x
Pl LC ASTROLOY
KALLIN(S ETCNANT
GD7-076..317
Figure 134. Braze Closure After HIP Diffusion Bonding (Sample was Subjected
To Yo-Yo Heat Treatment).
85
1
] ASsu
IuAOe
_mLEOv_xa_mORAL
G_MEtRT l j-"]__ """_::: ° '"_":'_ .... /
-I ,..AM j+ SHROUOSTR_
RANSMIT5 INFORMATION
AT CALCULATION 13 BLADES
AXIALLENGTH
STATIONS
= 39.37 mm 11.55 INCH)
._vls[
--
_.;;'o';.......
• nlRTRI|IITtO-
I
|
At¢ALCULATIO.
TRANSMITS INFORMATION
°:
I "
MEAN STREAMLINE
Y
I SLAOE CHANNEL _
I FLOW ANALYSIS I I_ 0
SATISFACTORY _
F--
/
•" 6R-
DISTRIBUTION _-
_- i '?"_R"_+
°'
HUBSTREAMLINE S
._,T,o, j
I,-,._.., I
GITl_ 0
rERCENT
MERIOIONAL
OISTANCE
Figure 135. Radial Turbine Design Flow. 617471-326
2.46- t
MO DIFI EO-,-.,,..,,. I t
BLAME _ I tI
//i
Z.34-
Z22-
Z.lO-
/ 1.0
SHROUDSTREAMLINE
REOESIGNEDROTOR_
t.g-
_ORIGiIIAL
o_ o.e SUCTION SURFACE -j"
.- ._"
,,
.//_'7/j
SLAG[
I1
1Jll-
; O.D;.
m O.l
_+_,+
I %/
1.74-
0.2, _'_/'_
IJIZ -
10 20 30 40 50 60 70 80 90 100
Z. INCR[S
GB7_)78-325
o.a.
REOESIGNEO ROTOR MEAN STREAMLINE f f _"_,_
,," f "
0 I0 20 30 40 50 90 70 80 90 I00
PERCENTMERiDIONALDISTANCE
GB7_78-328
ORIGINALOOTOR
HUB STREAMLINE
_m_ flEOESIGNEO
ROTOR
TE
PRESSURE
0
O I0 20 30 40 50 90 70 90 90 190
PERCENTMERIOIONALDISTANCE
gl7_7_329
87
5.3 Combustor Development
Total Unburned 0.25 gm/km PM/PV LENGTH, CM IINI 1.1-5,1 10.44-2.01 0.36-1.7 (0.14-Q681
88
CONFIGUIqATION NUMBER 1 CONFIGURATION NUMBEq 2
HALF RADIAL
89
5.3.2 Combustor Development
90
nozzle based on this design which would also
be easy to manufacture. One of three nozzles
FUEL NOZZLE __ '_
delivered by Delavan was heavily instrumented
with thermocouples and pressure probes to
AIR COOL _/_ //_PNSULATION I_
assess the potential of coking and fouling
problems. Testing at most severe conditions
showed the nozzle was sufficiently cooled to
prevent coking and led to the selection of the I_ _ _ i I J.i___
Delavan nozzle for all subsequent engine and
rig testing. The current configuration Delavan 1.1 MM ___ ._ii_+ J L"_II - -
nozzle, shown in Figure 147, has been used (O._I4MM, _---_ 3.5 MM __.----'I "_. .........
91
Table 16. Combustor Data.
Configuration Can
Combustor Length cm (In) 30.5 (12.0)
Diameter at Primary Zone em (In) 4.8 (1.9)
Length/P.2. Diameter 2.8 (6.3)
Combustor Airflow kg/s (Ibm/s) 0.729
Combustion Efficiency at Design Point Percent 99.9
Airflow Split
Primary Zone Percent 22.18
Dilution Zone Percent 63.41
Swirler/Injeetor Percent 14.38
Inlet Static Pressure kPa (psia) 394 (57.1)
Combustor Total Pressure Loss Percent 3.6
Inlet Total Temperature C (F) 975 (1787)
Average Total Exit Temperature c (F) 1371 (2500)
Pattern Factor <0.09
Combustor Surface Area cm 2 (in 2) 897 (139.1)
Combustor Volume em 3 (in J) 1627 (99.3)
Liner Wall Material Sintered
Silicon
Nitride
Overall F/A Ratio
Rich Blowout 7.100
Design Point Steady State 0.0118
Lean Blowout at Design Point 0.001
Primary Zone F/A Ratio of Design Point 0.0569
Fuel Injector Type Air Assist
No_ Fuel Injectors 1
Design Point Fuel Flow g/s (Ibm/hr) 3.9 (31.1)
Minimum Fuel Flow for Lightoff at g/s (lbm/hr) 0.34 (3.0)
Start Limit
Maximum Viscosity for L/O at Start Limit eentistoke 12
Turndown Ratio 21
Tolerance to Diffuser Exit Swirl Angle _-degrees 12
Types of Fuel Used DF-2 JP-4
Gasohol
Heat Release Rate at Cruise j/hr-kPA-m 3 (Btu/hr-atm-ft 3) 9.6 x 108
(2.61 x 106)
Aerodynamic Loading at Cruise kg/m3-kPA-sec (Iblft3-see-at m) 7.5 x 10 -5
(0.015)
Reference Flow Area cm 2 (in 2) 67.1 (10.40)
Inlet Math No. 0.06
Primary Zone Reference Velocity m/s (ft/see) 43.2 (141.6)
Residence Time at Cruise ms 5.4
Emissions at Cruise
Nox gm/kg fuel 13.5
CO gm/kg fuel 2.4
HC gm/kg fuel 0.21
Number of Ignitors 1
92
RING
GEAR DRIVE
RING GEAR
SEPARATOR
REGENERATORCORE
ROUSING
MATRIX
IROTI
SEAL
OUTERI
SEAL
G67_78-258
EXHAUST
Figure 149. Enlarged Pilot Zone Combustor. HOUSING
SUPPORT
SUPPORT ROUSING
using both JP-4 and DF-2. It also demon- ROLLERS
strated excellent temperature ramping char- G67_7_3,57
acteristics which easily meet performance
goals. Testing of the metal and ceramic
versions of this configuration will continue to Figure 150. AGT101 nRegenerator System n
characterize its performance. Components.
93
O Flow Separator Housing- A ceramic hous- Hot regenerator rig design/testing/evalua-
ing that divides engine compressed air tion-seal leakage evaluation with helium
from turbine discharge exhaust gas and injection
provides the platform for the inner regen-
erator seal. o Exhaust housing distortion analysis/test
evaluation
0 Exhaust Housing- The metallic housing
that divides engine compressed air from o Drive and support roller bearing/material
turbine discharge exhaust gas and provides tests
the platform for the outer regenerator
seal. 5.4.1 Ford Regenerator Development
O Ring Support Housing- The metallic hous- The primary AGT101 program objectives
ing that provides the platform for the flow for the regenerator system were to obtain an
separator housing. effectiveness of 92.9 percent, a total pressure
loss of less than 7.5 percent at the maximum
Regenerator system development activities power operating condition, and a seal system
were conducted at Ford and at Garrett Tur- capable of operation at 1090C maximum tem-
bine Engine Company (Garrett). Specific com- perature with 3.6 percent leakage. In addi-
ponent development activities to each com- tion, the design and development of a durable
pany are listed below and are discussed in drive and support system was required. This
detail in paragraphs 5.4.1 for Ford Regenera- report summarizes the design and development
tor Development, and 5.4.2 for Garrett Regen- efforts from October 1979 through June 1987
erator Development, respectively. toward achieving the program objectives.
94
ORIVE PINION REGENERATOR
SEAL
/ SPRING ROLLER
ASSEMBLY
spring roller. The development of these com- system durability. These design criteria were
ponents are described in the following para- applied to the following areas of the new AGT
graphs. seal system:
95
also derived from the 707 seal. The inboard Seal Leakage Development
(hot) seal assembly is positioned vertically to
the flow separator housing by means of a Starting with the Ford regenerator seal
retaining rig. Peripheral seal component stiff- technology as a baseline, further reduction of
ness had to exceed the critical buekling seal leakage was a development process in
stresses to prevent radial distortion when the which seal systems were initiallyanalyzed via
limits of constraint (due to thermal growth) computer programs for shoe loadings and dia-
were reached, but also must have sufficient phragm clearance throughout their operating
flexibility to conform to the profile of the range. Seals were then fabricated for evalua-
regenerator core. Wider shoes tend to reduce tion in the static seal leakage fixture at room
leakage by creating a better labyrinth effect. temperature. Concepts that demonstrated
Since low leakage was a prime objective for leakage reduction in the static seal rig were
the AGT regenerator system, the peripheral then tested under hot operating conditions in
shoe width (190 ram) is equivalent to the 707 the regenerator test rig and engine. The rig
system. The crossarm shoe width is 38.0 mm and engine results were used to update the
compared to 41.1 mm for the 707. computer analysis and refine the design of the
next generation of seals. Such an approach
The diaphragm system, which is the com- was successful in the development of seal
pliant member between the shoe and engine systems for other engines at Ford.
structure, was also based on 707 technology.
The diaphragms were formed from foil mater-
ial 0.0762 to 0.203 mm thick. The material A typical regenerator seal cross-section is
that had proven durability, Inconel X750, was illustrated in Figure 152. The seal working
selected for the initial fabrication. height (SWH) represents the total clearance
for the seal assembly resulting from the in-
In order to design a low leakage regenera- stalled clearance minus the axial movement of
tor seal system, the following design consider- the adjacent engine structures and regenerator
ations required investigation" core at specific engine conditions. The dia-
phragm clearance (C) represents the amount
1) Control of engine structures that affect of clearance from the sloid height of the
seal operating clearance. assembly. Regenerator system build clearance
is defined as the total diaphragm clearance
2) Diaphragm design to optimize seal load for (2C) that exists for both seals at engine
minimal leakage without excessive coating assembly. The total above shoe force (FT)
wear and drive torque requirements. imposed on the rubbing shoe, consists of the
mechanical loads from the deflection of the
To assist in the development of a low diaphragm elements in addition to the air
leakage seal systemp the following test rigs pressure force. The combined forces acting
were utilized: above the shoe can be represented equiva-
lently as a force (F T) acting at a specified
I) Static seal leakage rig to monitor design distance (D U) from the inner edge of the
changes. rubbing shoe, as illustrated on Figure 152.
2) Test fixtures to establish seal assembly The primary engine structures that control
mechanical load characteristics. regenerator seal working height are the flow
separator housing and exhaust housing. Axial
3) Hot test rig to evaluate system leakage thermal growth and distortion of these com-
and coating wear characteristics. ponents directly affect the SWH.
96
engine testing, supported by additional loading
and thermal analysis.
T t
c HETAINER __'_
_OIAPHRAGN UPPER In order to analytically determine the dia-
swH I _- _f _ _MiOOLE phragm load and stress as a function of clear-
,, tu
RP LOWE, ance, the diaphragm load characteristics were
_, --RETAtNEH
required input to the "core position" analysis
computer program, which performed a summa-
tion of forces and moments imposed on the
RUBBING SHOE regenerator. Once the operating plane was
I P WEAR FACECOATING determined, the variation in force and stress
distribution for each component of the regen-
erator seal system was defined.
REGENERATORCORE
The main objective for the regenerator
seal system design was to achieve sufficient
contact force (F C) with minimal variance at
EQUIVALENT FORCESYSTEM HP
f 1 each seal component location to provide
effective sealing with coating wear at a uni-
I T i form and an acceptable rate. Contact force
LP r | II
(F C) is defined as the net load resulting from
the above shoe diaphragm mechanical and
pressure forces (F T) that are partially offset
LP_ _ --"- -----,-
..,..,,, ?E U II by the undershoe pressure force distribution
I (F U) that exists between the seal wear face
coating and the regenerator matrix face (Fig-
HP
ure 152). The undershoe pressure distribution
FCONTACT = FC = FT- FU is a function of the labyrinth effect due to
GI7076.'L'_I leakage ch_,racteristics between the shoe and
regenerator core.
97
IXi IP]
PHASE CROSSARM SECTION PHERIPHERALSECTION COMMENTS
X - SAME AS i
P - LOWLiFT OIAPHRAGMS
I I I I PLUS SPRING
I I I I P- SAME AS IV
X - COOLINGLOUVERSAND HOLES
VI BARRIERCOATING ON SHOE
I P - SYMMETRICAL
DIAPHRAGMS UPPER AND LOWER
G|7_7_331
changes and the results were compared on a metric studies in the static leakage rig indi-
relative basis to the baseline regenerator seal cated the need for increased loading of the
system. In this manner, the comparative re- lower sealing diaphragm against the metal seal
sults served as a guideline to provide direction shoe in order to reduce leakage at low pres-
to additional design changes. This procedure sure levels.
was used in previous engines for optimizing
the regenerator seal system design. The Phase III regenerator seal diaphragm
design evolved from parametric studies in the
The initial Phase I seals evaluated in the static seal leakage rig to minimize leakage at
static seal rig at the design clearance ex- low pressures.
hibited leakage slightly above the initial ob-
jective of 7.2 percent of total engine airflow The most significantchange was the addi-
at the maximum power operating condition. tion of a supplementary spring mounted on the
Subsequent testing at Garrett indicated mar- retainer. Engine and rig testing indicated
ginal seal loading and subsequent high leakage substantially improved leakage over Phase I
at part power engine conditions. and II,though seal loading was excessive.
The Phase II seal configuration featured a A parametric test series was conducted on
spring diaphragm inserted between the two the Phase Illconfiguration in parallel with a
sealing diaphragms, and provide the seal load- parametric analysis. This work evaluated the
ing required to reduce seal leakage. Para- effect of seal loading on seal leakage.
98
Through optimization of load distribution, it In addition to these design improvements,
was found that seal loading could be substan- the quality of the prototype hardware was
tially reduced without sacrifice of leakage. improved through the procurement of new
tooling and improved processes.
The main objective for the Phase IV seal
system were to preserve the leakage charac- An interim quality control standard was "
established at that time for the static seal
teristics associated with the Phase Ill design
with a further reduction in mechanical load leakage rig to ensure that low leakage seals
would be sent to Garrett for engine and test
characteristics to reduce drive torque require-
rig evaluation. A 0.006 m3/s static leak test
ments. Additionally, the Phase IV seal in-
requirement per seal (inboard or outboard) at a
corporated cooling passages which used a con-
7.0 mm seal working height (SWH), was estab-
trolled amount of leakage to maintain the
lished. This represented the state-of-the-art
diaphragm temperatures within the limits of
at this time for the Phase V seals. Hot and
diaphragm material capabilities.
cold seals that totaled 0.011 m3/s leakage at
7.0 mm SWH in the Ford static test rig _vere
Through another series of parametric tests
evaluated in the hot regenerator rig at Garrett
and analysis, further improvements in leakage
and mechanical loading were attained. using the helium tracer technique and indi-
cated a leakage of about 5.5 percent.
The mechanical load characteristics for
Additional testing in the static seal rig
each of these seals were measured. The load
with symmetrical upper and lower outer per-
characteristics indicated the Phase IV design
ipheral diaphragms and equal length retainer
was an effective compromise between the
legs demonstrated a potential 20 percent re-
Phase [ and Phase Ill designs. Consequently,
duction in static leakage. This concept was
the actual hardware substantiated the analyti-
adopted as the basis for the next generation
cal predictions.
seal design, which was designated as Phase VI,
as illustrated on Figure 153. In addition, the
Rig and engine testing indicated that in the
Phase Vl design can accommodate more cool-
dynamic thermal environment of a regenerator
ing air for the inboard (hot) crossarm seal
system, drive loads for the regenerator were
compared to Phase V.
higher than the Phase Illdesigns. Leakage was
equivalent to the Phase Ill configuration, Additional features of the Phase Vl seal
though the allowable SWH tolerance was much configuration included a crossarm thermal
more broad with the Phase IV seal. barrier coating for improved seal diaphragm
cooling and bore pressure relief slots in the
Based on the test results for the Phase IV cold seal inner periphery.
seal design, a new design iteration (Phase V)
was initiated. The design objectives for the Phase Vl seals qualified with less than
Phase V seal (Figure 153) configuration were 0.011 m3/s leakage at 7.0 mm seal working
to further decrease the leakage and drive height. These hot seals were also made with
torque requirements. In order to accomplish reprocessed, used shoes. Based on engine
these objectives, the Phase V design featured exhaust flow at full power conditions and
an integrated crossarm diaphragm which corrected for ambient temperature, a static
eliminated the inner secondary diaphragm that seal rig leakage of 0.004 m3/s per seal was
was used in previous designs. Tests in the estimated to be adequate to meet the program
static seal rig indicated a significant portion objective of 3.6 percent for the regenerator
of the total leakage occurred at the inside and system. Therefore, the combination of the
outside corners, in addition, the integrated low leakage Phase VlB cold seal (0.004 m3/s)
crossarm diaphragm had a reduced lift angle, with one of the Phase VIB hot seals (0.005
which would reduce the mechanical load char- m3/s should nearly meet the program objec-
acteristics and drive torque requirements. tive in an engine.
99
b
i00
axial direction in the middle diaphragm, the
flow can be interrupted to prevent boundary
layer build-up and promote localized turbu-
lence, which increases the localized heat
transfer coefficient. In addition, convection
coefficients between the upper diaphragm and
flow separator housing were also estimated
based on leakage.
i01
the circular portion of the crossarm dia-
phragm.
102
coating I-ll2. This was the only Ford proprie- determined. Periodic measurements of sample
tary seal coating that did not have docu- thickness determined the seal coating were
mented durability at the higher AGT crossarm rate.
temperature conditions. In order to establish
the upper temperature limit for the 1-112, an In order to determine the upper tempera-
existing test rig was modified to increase the ture limit of the 1-112 coating to be assured
maximum test temperature from 815 to I090C that it had I090C capability and to be confi-
(Figure 157). The primary modification was dent that its friction and wear characteristics
replacement of the metal test sample holder could be controlled during processing, the fol-
with a ceramic holder. lowing parameters were investigated:
The stationary test sample was loaded 1) Chemical composition and particle size
against the rotating test core by a compres- distribution of the coating powder.
sion spring. A lever arm, which was pinned to
a center shaft, applied the torque reaction 2) Spraying procedure for deposition of the
force against a calibrated load cell. By know- coating powders on the metal substrate.
ing the applied force (P), torque reaction force
(FR) and physical dimensions of the sample, 3) Interface coatings to accommodate the
the sliding coefficient of friction (]_) could be difference in thermal expansion between
the [-112 coating and the metal substrate.
TEST CORE CORE SCREWS ,_ K II Fourteen samples were tested for more
RETAINER \ / [//_\_,J _.L_P:_ than 2000 total hours in order to evaluate the
above parameters.
Figure 157. Regenerator Seal Coating Since the loads in the AGTI01 regenerator
Wear Test Rig. seals were approximately the same as those in
103
the 707 seals, a coefficient of friction less The effectiveness of the deep serrations
than 0.35 and a wear rate of less than 0.020 are clearly illustrated (Table 17). Tempera-
mm/100 hr. should result in acceptable drive ture capability appeared to be increased 55 to
torque and seal life in the AGT engine based 166C compared to a non-serrated sample.
on 707 experience. Tl_ese same criteria were
used, therefore, to establish the acceptability Based on visual observations of hot flow
of the I-i12 coatings that resulted from varia- path components tested in the initial hot
tions in composition, particle size, spraying structures rig and ceramic engine at 1090 to
procedure, etc. I150C turbine inlet temperatures (TIT), the
1-85 coating for the hot seal outer peripheral
For the 14 samples evaluated in the wear shoes appeared to be marginal. Although the
rig, which consisted of the three different copper based 1-85 did not delaminate, soften
batches of powder as well as variations in or experience significant wear, trace amounts
spraying process, the 1-112 coating demon- of copper were found to be the cause of
strated friction and wear characteristics well sticking between other ceramic components.
with the Ford acceptance criteria for exposure In order to increase the upper temperature
up to 1090C and 68.9 kPa maximum load. limit, 1-151 was evaluated as a replacement
for the 1-85 coating on these shoes. Based on
To evaluate the substrate bond coating, wear rig tests at Ford in the early 1970's, the
samples sprayed with commercially available 1-151 (zinc-oxide) had 112C higher tempera-
METCO 443, METCO 447, and GE Superalloy ture capability compared to 1-85 (copper
in place of NiCr were evaluated. In order to base).
evaluate the effectiveness of the deep serra-
tions, additional samples without serrations The initial seals with 1-151 installed in the
were also tested. A summary of the tempera- ceramic engine at Garrett experienced delam-
ture capabilities of the various test combina- ination in the 1-151+I-39 interface bond re-
tions are listed on Table 17. Some improve- gion. An evaluation of the 1-151 coating was
ment was evident with METCO 443 and conducted which established that the coating
METCO 447, which appeared to increase the powder used was not within specification.
temperature capability approximately 28 to Since the coating vendor had difficulty pro-
56C. The GE Superalloy appeared to satisfy ducing this coating, it was decided that the
the I090C objective. 1-151 would not be pursued.
104
As a replacement for 1-151 peripheral seal the 1090F regenerator inlet temperature re-
components, modified versions of 1-85 with quirement, the regenerator matrix must have
improved plasma spray parameters as well as sufficient thermal stress capacity. Durability
1-112 peripheral components were assembled is dependent on matrix material stability at
for engine evaluation at Garrett. Testing seal elevated temperatures for extended time.
assemblies with improved 1-85 or 1-112 in the
ceramic engines did not cause sticking be- During the AGT101 program, regenerator
tween ceramic components. As expected, seal cores have been supplied by Corning Glass
assemblies with 1-112 in place of 1-85 did, Works, and NGK-Locke. The Corning cores
however, have higher drive torque require- are fabricated as a two-sheet wrapping pro-
ments. cess with aluminum-silicate (AS) material.
NGK-Locke utilize the extrusion process with
For the final AGT seal configuration magnesium-aluminum-silicate (MAS) material.
(Phase VIB), the best combination of wear face Geometry and performance for each of these
coatings that would satisfy the 1090F regener- core configurations are compared in Table 18.
ator inlet temperature requirement was as
follows: The Coming aluminum-silicate (AS) wrap-
ped thin-wall sinusoidal matrix satisfied the
1) Hot (inboard) seal: I-ll2 on all compo- pressure drop objective but is 1.0 percent low
nents in effectiveness. Corning was provided addi-
tional funding to fabricate samples of an ex-
2) Cold (outboard) seal: Improved 1-85 on all truded AS matrix with a rectangular cell shape
components except for 1-112 on the cir- and 0.089 mm material wall thickness to meet
cular section of the crossarm. the AGT101 regenerator effectiveness and
pressure drop objectives. The wall thickness
In summary, two of the Ford proprietary wear in the sample provided was thicker than antic-
face coatings (I-85 and 1-112) have been ipated. The estimated performance for this
adapted for the higher temperature require- matrix geometry (Ext. 1) was 0.8 percent
ments associated with the AGT program. Im- lower effectiveness than the original matrix
proved plasma spray parameters have pre- geometry with equivalent pressure drop. Even
vented the 1-85 wear face coating from de- though the extruded rectangular matrix is
laminating at the higher temperature condi- more efficient than the sinusoidal geometry,
tions of the outboard seal assembly. 1-112 the thicker fin wall more than offsets any
combined with GE superalloy bond coating on expected gain in effectiveness. Further devel-
a serrated inboard seal crossarm substrate has opment of the extruded Corning matrix would
satisfied the 1090C temperature requirement. have extended beyond program termination.
105
the fin geometry utilizingshuttle rig test data Corning material. NGK took two approaches
for similar geometries. The predicted per- toward resolving this problem. First, they
formance for the four NGK fin geometries are developed coatings for the inner and outer
listed on Table 18. Estimated performance circumferences, in addition to impregnating
predictions indicated the program perform- the matrix walls. This method was not effec-
ance objectives could be attained with the tive in reducing porosity in the thin wall C0.7
C0.7 fin geometry, provided a more dense or C0.8 matrixes. Then, they fabricated full-
material could be developed to reduce exces- size cores with their dense, less porous revised
sive wall porosity leakage. MAS material designated MAS-A.
Due to the greater wall porosity of the NGK has demonstrated significant im-
original NGK MAS regenerator matrix mater- provements in modifying their standard mag-
ial, core leakage across the crossarm and nesium-aluminum-silicate (MAS) material in
through the inner and outer circumferential order to achieve the porosity leakage objec-
was higher when compared to the more dense tive. The improved MAS-A incorporated in-
Coming:
NGK:
106
creased shrinkage during firing, which reduced
wall porosity from 38 percent to 28 percent.
t" z
Based on static seal leakage data for a full-
size core with the rectangular matrix param-
eter (C0.9), the estimated leakage at full
power conditions was 0.40 percent, which sat-
isfied the porosity leakage requirement. In DISTANCE BETWEEN
addition, the matrix wall thickness was re_ SLOTS = 2G
=i i 7000 1015-580.670725
"li
A three-dimensional thermal stress analy-
\\ NEAR
RDT
COR
,ACE
0O
sis (SAP Ill) was completed (Figure 158) on a 435-
M_S regenerator matrix made by NGK. This
matrix contained a number of tapered slots
extending from the inside diameter of the
rubbing seal shoe on the hot face to the matrix
outside diameter on the cold face. Previous
-J 14,5- I ! ""-
I
|
analysis and experimental work had shown that ,l= , 111 ill= II li lillllil'l=lllll II III1 Ira Ill ' I
these slots were close to the optimum design 5 tO 15 20 25 30 35 40 45
107
matrix is in compression. As the safety factor material has a high thermal stress capacity
increases, the potential for the formation of even though the AS is considerably less stable
rim cracks decrease. Since the safety factor than the MAS materials.
for this NGK core with 28 slots is approxi-
mately 1.0, thermal rim cracking is not ex-
Two full-size cores fabricated with the
pected to be a problem.
new improved MAS-A material were received
from NGK near the end of this program. Ring
The high temperature dimensional stability
gears were bonded to them for engine and test
of the NGK originaland improved MAS mater-
rig evaluation. One of these cores accumu-
ials were evaluated by periodic measurement
lated a total of 96 hours in Ford development
of specimen length change as a function of
test rig,with 53 hours at I090C (1994F) expo-
exposure time at 1000C (1832F) and II00C
sure. This core demonstrated improved
(2012F) for 1008 hours (Table 19). In addition,
thermal stress capacity compared to cores
the thermal expansion behavior between room
fabricated with the original MAS material.
temperature and 1000C (1832F) was deter-
The stress relief slots effectively eliminated
mined for each material before testing and
radial thermal cracks at the outside diameter
after completing the prescribed testing sched-
of the core on the hot face.
ule. As a reference, the Corning AS material
data generated in 1980 is included (Table 19).
Both NGK materials exhibited equivalent sta- In summary, regenerator cores have been
bilitywhen compared to reference data gener- supplied by Coming Glass Works. and NGK-
ated in 1977 for the NGK matrix that demon- Locke. The Corning core, which is fabricated
strated 2500 and 250 hours at 800C and 1000C, as a two-sheet wrap structure with aluminum-
respectively,in the Ford 707 engine. silicate material, is approximately 1 percent
below the effectiveness objective. The most
The significantdecrease in thermal expan- recent NGK extruded core with their improved
sion for the 1986 NGK materials compared to magnesium-aluminum-silicate material is
the 1977 material provides a significant de- approximately 0.7 percent below the effec-
crease in thermal stress, which allows a sub- tiveness objective. Both cores have sufficient
stantialincrease in dimensional stabilitytoler- thermal stress capacity for I090C (1994F) sys-
ance. This is the main reason the Corning AS tem operating temperature.
Coefficient
Dimensional Change of Thermal
(ppm) After 1008 Hr. Exparlsion Thermal Expansion (ppm)
Exposure (X106/C) at 1000C
i|
108
5.4.1.4 Drive and Support System
30
4) Steel backed pinion bearings can be press
fitted without preheating the housing,
which was required for the original design
when the carbon bearing was press fitted
TORQUE: 271 Nm
WT = 9 Kg
FR : GEAR SEPARATING FORCE : 39 KO There are two key areas involved in the
FT : GEAR DRIVING FORCE = 107 elastomer bonded ring gear to regenerator
TI = PHERIPHERALSEAL REACTION FORCE : 36 KO
matrix design for the AGT application that
F2 : CROSSARMSEAL REACTION FORCE : 22.7 KO
FS : SPRING ROLLERFORCE : 23 KO fall within Ford regenerator system experi-
FF : FiXEO ROLLERFORCE : 91 KO ence. These are: elastomer operating tem-
Fp : PINION ROLLER FORCE= 29 KO
perature and compliancy. One of the key
G87-078-338
elements for the elastomer bonded ring gear
Figure 159. Regenerator Support design is to minimize the temperature of the
Roller Locations. elastomer. Utilizing a two-dimension heat
109
transfer program, the results indicated that,
by locating the ring gear near the cold face of
the regenerator, the elastomer temperature
will be comparable to those in the Ford 707 OlAGONALBOND CONFIGURATION
engine (Table 20). Consequently, this elasto-
mer has had no difficulty meeting AGT engine I
cycle conditions. /
Temperatures. @_ ELASTOMER
ELASTOMER
ii0
In summary, the three-point support drive up to 650C (1202F) and durability was evalu-
system for the AGT engine which is a deriva- ated at temperatures up to I090C (1994F).
tive of the Ford 707 system, has not indicated Leakage evaluations were performed in
any significant problems in limited rig and metallic structured rigs with flow paths simi-
engine testing. Attachment of the metal ring lar to the engine configuration. The Garrett
gear to the ceramic regenerator matrix with rig attempted to isolate the regenerator sys-
the diagonal bond configuration, which has a tem from the outer system seals by welding or
high degree of compliance, has minimized the brazing the structural assembly together,
drive system reaction forces imparted on the
eliminating many of the interpath seals. This
core.
rig incorporated a separate flow path for the
high and low pressure sides of the regenerator
5.4.1.5 Regenerator System Development
system. Leakage was measured by seeding the
Rig high pressure inlet gas with helium and sensing
the helium concentrations in the low pressure
AGT101 regenerator system rig testing has
side gas discharge. The Phase V-A configura-
been performed during the AGT101 project at
tion seal was tested in this rig. Leakage was
both Ford and at Garrett. The purpose of this
measured at the 6 percent level at the
testing was to evaluate the regenerator sys-
elevated temperature condition of 650C
tem under controlled conditions for develop-
(1202F). Continued development was con-
ment of the regenerator system components
ducted in the Ford rigs.
and evaluation of the regenerator system op-
erating characteristics. Regenerator system Shown in Figure 162, the Ford rig was
leakage was evaluated at inlet temperatures similar to the Garrett rig, though it could
SEALS
TURBINE
P3.6
COVER_ RINGS
PISTON_
RINGS_
[{]WELOED JOIN1
REGENERATI
SEALS REGENERATOR
CORE
GB7-0711-341
iii
accommodate either metallic or ceramic 2) The entire velocity pressure in each of the
structures. The leakagesfor each of the non- restricting areas is lost.
regenerator system seals were calibrated in
cold, static testing and corrected for high 3) Reynolds Number effects are ignored.
temperature conditions. For measurement of
overall rig leakage at operating temperature, 4) Temperatures at the various points in the
this rig utilized a high temperature orifice flow path were inputted from rig test data.
measuring section between the regenerator
high pressure discharge and rig combustor in- 5) The flow areas used to eliminate the dif-
let. To simulate the pressuredrop across the ferent leaks were determined from mea-
turbine this rig incorporated a valve which surements made in the cold, static rig in
seated on the turbine shroud. The valve the Build-Up Laboratory.
featured a power screw adjustment that
allowed the valve position to be changedin the 6) Other flow areas were estimated from
test cell for precise simulation of engine pressure drop measurements made in the
operating conditions. The operating tempera- dynamic rig.
ture of the rig was limited to 590C due to the
materials used in the orifice section. The 7) All flow areas, except that of the valve,
regenerator leakage was determined by sub- were held constant in all calculations.
tracting the system leakagesfrom the overall•
This model correlated well with the test
Assembled in the ceramic configuration, data taken from the rig at inlet temperatures
this rig was characterized for leakage in cold up to 590C (1094F). The regenerator system
static testing, and overall leakage measured leakage at the hot, cruise condition was pro-
up to the 590C temperature limit of the jected at 4.0 percent using the same model.
metallic interpath orifice section. This data This was close to the program objective of 3.6
was further reduced through analysis to deter- percent• If a Phase VIA hot seal and a low
mine how the regenerator seal leakage com- leakage Corning core had been used, it was
pared to the program goal of 3.6 percent. anticipated that the leakage objective would
have been met.
An analytical model was developed to aid
in understanding the different sources of leak- Durability Testing
age. The flow paths used in this model are
illustrated in Figure 163. All the high pres- After completing the seal leakage evalua-
sure, cold air leaks (P3.0 and PS.I) were tions, elevated temperature testing was con-
consolidated together and simulated by one ducted to evaluate the high temperature dura-
leak, as were the high pressure, hot air leaks bility of the regenerator system. This testing
(P3.6 to P5.1). The unique high pressure, hot was conducted in the ceramic version of the
air leak, (P3.6 to P4.1) which is present in this Ford Regenerator System Rig without the in-
rig but not in an engine, was also included. terpath orifice section installed. This rig was
The components and leak paths _,ere defined capable of operation of regenerator inlet tem-
by a set of flow restrictions, as illustrated in peratures up to the system design goal of
Figure 163. Each restriction is an orifice 1090C (1994F).
having a specified flow area. The computer
model iterates on this network of restrictions During this test program the rig was as-
until it converges on a solution in which the sembled 13 times, accumulating 238 hours of
sum of the pressure drops of the individual testing, including 73 hours at I090C (1994F)
components equals the available pressure drop, regenerator inlet temperature. This testing
P3.0 to P6.0. The following assumptions ap- contributed to the design and development of
ply: the inner regenerator seal cooling configura-
tion and evaluated improved materials and
1) The flow is compressible. designs used in the regenerator core assembly.
112
ANALYTIC MOOEL
P3.6 TO P_ LEAKS
_Y
,,. °.u.,. &Eke- L, ,OE
INLET
ORIFICE
,E...E.,. .C. .C. .,.E.T.
MEASURING
ORIFICE
OOWNSTREAM
AIRFLOW FLOW
INLET HP SlOE MEASURING TURBINE CONTROL LP SlOE
ORIFICE REGENERATOR ORIFICE COMDUSTOR NOZZLES VALVE REGENERATOR
Gil7.078-342
The regenerator seal cooling system was configuration of the regenerator rig. Long
developed through an iterative process. Seal term durability of the seal assemblies were
diaphragms were instrumented with thermo- evaluated in tests planned for 50 and 100
couples and installed in the rig for each test. hours. Significant problems such as regenera-
The resultant temperature data was recorded tor core thermal cracking, seal coating delam-
and evaluated, providing valuable information ination, and shoe distortion were discovered
for seal design improvements such as the ap- and evaluated during extended durability test-
plication of thermal barrier coatings to the ing.
seal shoes, finned support diaphragms etc..
The curves in Figure 164 show typical data The regenerator core thermal cracking
from this testing. problem was related to the thermal expansion
of the MAS regenerator core material and the
Additional information was generated as a strength of t]pe matrix. In cores assembled
result of endurance testing in the ceramic from extruded segments, the strength and
113
C IFI
190( 6"_,
i,,m
%
900. _b• %
IBOO _• •
800.
•i
1400
700" 1300 i , , , ,
NOMINALT5.I = I093C 1200OF)
C 1200 I I I I ' L METALTEMPERATURE
I00O- IFI
1800
1700 <.,),_
", .c o *3.B
1300 'm3
700,_ %% _ 0 1 _- --.0
-,_ THERMOCOUPLE
#1
THERMOCOUPLE
_2
1200 i I _k
NOMINALT5.I = 962C 11800Ei %% O-----C] THERMOCOUPLE
#3
5001 1100 I I I I _ I
C IFI LOCATION
OF
1400 _ _ OIAPHRAGM
SPRING
1200 C_ '._%
"" I I I r',,.
t_O
114
compatibility of the bonding cement was also Subsequent investigation in the regenerator
a significant factor. Small matrix cracks form rig evaluated the coating delamination at tem-
on the outer periphery of the hot face of the peratures up to 1090C (1994F). Seal design
core after several hours of durability testing. modifications were made to remove restric-
In the most severe cases, the cracks would tions to seal thermal growth, however the
propagate with time and temperature across distortion was evident in follow-up testing.
the face of the core to the center, generating
large leaks, and core debris. The problem was Regenerator System Sum mary
solved through proper location of stress relief
slots in the outer rim of the core and the use Based on test data and analysis accumu-
of improved MAS-A material from NGK. lated at both Ford and Garrett, the current
status toward achieving the three main pro-
The distortion of the regenerator seal gram objectives are as follows:
shoes, and delamination of the seal coating
during I090C (1994F) operation are related I) 92.9 percent regenerator core effective-
phenomenon which were discovered during the ness with less than 7.5 percent pressure
last phases of the AGT regenerator seal devel- drop at WOT engine conditions.
opment effort. The photograph in Figure 165
shows the crossarm shoe and how the coating Regenerator cores supplied by Corning
delaminated from the inner periphery of the Glass Works and NGK-Locke, Inc. are ap-
shoe wearface. Inspections of the seal indi- proximately 1.0 percent and 0.7 percent
cated that the circular inner periphery was below the effectiveness objective, respec-
distorted to an oblong shape and that the tively, with a nominal 7.5 percent pressure
coating was lost from the distorted portions of drop. NGK has developed a thinwall isos-
the shoe. Characteristically, the seal shoe celes triangular structure that will exceed
was also bowed axially toward the coated side. the objective provided a more dense mate-
SHOE CROSSARM
I __
115
rial can be developed to have acceptable 5.4.1.6 Non-Diaphragm Seals
wall porosity leakage.
As an alternate approach to cooling the
2) Regenerator System capable of operating inboard (hot) seal crossarm diaphragm, a feas-
at 1090C (1994F) regenerator core inlet ibility study was initiated to eliminate dia-
temperature. phragms from this seal, as shown in Figure
166. The core would run against a wear face
Coming cores fabricated with AS material coating applied directly to the flow separator
and NGK cores extruded with their im- housing (FSH). The key requirements for a
proved MAS-A material have demonstrated successful non-diaphragm seal are low friction
the thermal stress capacity and matrix and wear coatings combined with minimum
thermal stability required for I090C engine leakage gaps resulting from compatible plat-
conditions. form deformations of the core and FSH. The
work plan for this study consisted of the
Ring gear attachment to the regenerator following:
with a compliant elastomer system design
and the associated drive and support sys-
tem has also demonstrated the system CURRENT SYSTEM
temperature objective.
HP
Outboard (cold) seal assemblies with all
1-85 coated substrates, except for 1-112 on
the circular portion of the crossarm, have
LP [-- I_:A_H_-_OHAGM SYSTEM
achieved the temperature objective.
I-II2 COATING
116
c) Labyrinth seal leakage analysis for re-
generator core - FSH gap performed at
Ford
117
•,)_ p.OOR QUALIT_'_
CORE RAOIUS
CM 5 I0 15 20
I I I J
MM tONi I 2 3 4 5 6 7 8 9
O- O I I I L 1 J
0.001•
005.
0.002 •
NE _ 100 PERCENT:SHAOEO
0.10--
0 CORHING1946ll
0.004.
_, NOK ICO.31
_ 0005,
_ 0.15-
0._
0,067-_
0.20-
0 000._
0.009-1
0.25-
O.OlO_
li17]Tt,141
Table 21. Leakage Air Flow Conditions. 10.28 kPa). Conversely, the leakage for Com-
ponent 2 is substantially higher than Compo-
nents 3, 5, and 6 even though pressure drop is
Component Po PN ] TO approximately the same.
118
SYMBOL COMPONENT
0 OUTER HP "C"
INNER HP "C"
[] _ OUTER LP "C"
0 INNER LP "C"
© 0+0 CROSSARM
0 TOTAL
O
NE = 61) PERCENT
W = AIRFLOW = 0.161 KG/S (0.355 LB/SEC}
I I i I I
To further demonstrate the importance of ring support interface, which results in zero
air temperature, the leakages at cruise and axial distortion of the outer ring of the FSH.
full power were estimated based on ambient Consequently, the distortions predicted are for
air as a function of uniform clearance (Figure the inner ring relative to the outer ring. In
171). In this case, the leakage with ambient addition, to simplify the initial analysis, dis-
air was approximately twice as high as leakage tortion due to temperature and pressure were
based on engine temperatures. evaluated separately. Distortion due to tem-
perature was evaluated at engine cruise (N E =
The next study consisted of evaluating seal 60 percent). Conversely, distortion due to
leakage for the FSH distortions predicted by pressure (isothermal) was evaluated at full
Garrett from their 3-D finite-element anal- power conditions (N E = i00 percent).
ysis, which is summarized on Table 22. For
the current Garrett model, one of the bound- A total of thirteen combinations were
ary conditions assumes axial constraints at the evaluated and summarized on Table 23. The
119
SYMBOL COMPONENT
<)
[] OUTER LP "C"
& iNNER HP "C"
OUTER HP "C"
0 INNER LP "C"
(b 0+0 CROSSARM
0 TOTAL
On
I
PNI o 0.001 0+002 0.003 0.004 0.005
! I i . I
[MMI 0 0.1)25 0.050 0.075 0.10
G87+07114140 CLEARANCE
maximum component gap is predicated by the baffling the compressor discharge flow around
contact point that results from meshing the it, the distortion is reduced significantly. In
axial distortion of the core with that of the addition, distortion of an RBSN housing due to
housing (FSH). If the distortion of the core is pressure is reduced significantly with the in-
greater than the FSH, then a gap will exist at corporation of struts.
the outer ring (components 1 and 2) and leak-
age will be substantial. Conversely, when the
axial distortion of the core is less than the Based on these preliminary results, the
FSH, then the gap at the outer ring is zero and leakage of a non-diaphragm inboard seal sys-
leakage will be minimized. tem was projected to meet the objectives,
provided the clearance between the core and
For the thermal distortions without pres- FSH at the outer ring was minimized. To
sure at cruise conditions, leakage was calcu- ensure this condition is met, the axial distor-
lated for both the current configuration (H = tion of the core should be less than the axial
28.39 W.m2C) and the simulation of a metal distortion of the FSH inner ring (components 3
baffle (H = 5.68 W/m2C) around the outer and 4). In addition, to more accurately predict
perimeter of the FSH. Initial results at seal leakage, axial distortion of the FSH due
Garrett indicated that, by allowing the mount- to the combined effects of pressure and tem-
ing flange of a RBSN housing to heat up by perature must also be determined.
120
A composite coating on a LAS ceramic
wear rig substrate consisting of a pre-heat
treated coating of Ford ATLAS glass frit,
THE EFFECT OF TEMPERATUREON
SEAL LEAKAGE which provides an intermediate bond coating,
and I-I12 plasma sprayed wear face coating
was subjected to I090C (1994F) furnace expo-
sure without failure. The sample accumulated
SYMBOL NE. PERCENT 63 hours at temperatures up to 980C (1796F)
0 6O in the seal wear rig against an LAS core
[] 100
without apparent difficulties. The coefficient
UNSRAOED: AMBIENT 21C {7OF) of friction varies between 0.16 at 980C
SHADEO: ENGINE TEMP. (1796F) and 0.22 at 815C (1499F) with negligi-
ble wear. A friction coefficient below 0.3 is
considered excellent.
121
1125
697-078-351
122
Table 23. Non-Diaphragm Seal Leakage Analysis.
9
\ _ .91-- _ +AF.S.H
LEAKAGE
08JECTIVE: 1.25 PERCENT MAX.
Max
Component Gap, mm
Core Film Total Leaka_e
Speed, FSH FStI Core Dishing Coeff, Loc Loc Loc Loc Loe
4% Contig Matl Type mm WIM2-C 1 2 3 4 6 (kg/s) (%)
60 No strut LAS Coming 0.03048 5.678 0 0 08.04 71.12 50.8 0.000612 0.38
60 No strut LAS Coming 0.03048 28.39 0 0 114.3 116.84 88.9 0.001421 0.88
60 No strut LAS NGK 0.2286 5.678 147.32 147.32 16.002 18.542 119.38 0.011338 7
60 No strut LAS NGK 0.2266 28.39 104.14 104.14 20.32 22.86 88.9 0.007256 4.5
6O No strut RBSN Coming 0.03048 5.670 0 0 58.42 58.42 43.18 0.000506 0.37
6O No strut RBSN Coming 0.03048 28.39 0 0 238.76 231.14 177.8 0.003930 2.4
60 No strut RBSN NGK 0.2286 5.078 147.32 147.32 8.382 6.35 114.3 0.011187 6.9
80 No strut RBSN NGK 0.2280 28.39 0 0 40.64 33.02 30.48 0.000226 0.14
6O Strutted RBSN Coming 0.03048 28.39 0 0 63.5 60.96 35.56 0.000453 0.28
100 No strut RBSN Coming 0.04064 0 114.3 114.3 88.9 35.50 83.82 0.021467 5.7
100 Strutted RBSN Coming 0.04064 0 17.78 17.78 16.51 5.08 12.7 0.001511 0.39
100 No strut LAS Corning 0.04064 0 152.4 152.4 20.066 7.874 12.192 0.033713 0.9
100 Strutted LAS Coming 0.04064 0 20.32 20.32 40.64 12.7 20.32 0.002418 0.64
G87-078-352
123
ensure that the core will contact the FSH. velocity measurements in the regenerator core
The FSH and associated cold seal with the mapping test.
thicker diaphragms were sent to Garrett for
evaluation. The hot wire technical capability required
for testing was developed in a specially de-
In summary, preliminary analysis of the signed calibration tunnel (Figure 173). The
non-diaphragm seal system indicates feasibil- calibration tunnel was utilized to cafibrate a
ity provided the clearance between the core total of eight 2-D and two 3-D hot wire
and FSH is minimized. To ensure this condi- probes for use in the regenerator core survey
tion is met, the axial distortion of the core test. Additionally, an in-house hot wire probe
should be less than the axial distortion of the repair capability was developed to support the
FSH. Based on furnace exposure and seal wear test.
rig testing, two wear face coatings continue to
show promise for bonding to the FSH. Analytically predicted turbine discharge
conditions had to be duplicated for the dif-
5.4.2 Garrett Regenerator Development fuser testing. Specifically, turbine exit swirl,
radial pressure profile, and corrected flow
Two cold flow regenerator test rigs, low rates were duplicated for idle, cruise, and
pressure (LP) and high pressure (HP), were maximum power engine conditions. Hardware
designed and fabricated at Garrett in order to: configurations to meet these requirements are
shown in Figure 174. Preswirl assemblies for
a) Determine circumferential and radial pres- idle (+55 degrees), cruise (0 degrees), and max-
sure profiles imposed by engine geometry imum power (-27 degrees), were fabricated
on the regenerator core along with various percent open areas screens
to generate the analytically predicted 5-per-
b) Evaluate flow profile control mechanisms cent radial pressure gradient.
Construction of an analytical flow and heat Determine circumferential and radial pres-
transfer model of the regenerator system in sure distortion profiles imposed on the LP
3-D form was completed and is discussed in inlet core face by engine flowpath geome-
paragraph 5.4.2.3. try
5.4.2.1 Regenerator Low Pressure (LP) Investigate and evaluate different flow in-
Cold Rig fluencing devices and the effect on overall
regenerator performance
The LP regenerator cold rig design con-
cept, Figure 172 is based on engine/model As previously stated, hot wire anemometry
similarity in areas of flow path geometry, techniques were employed during initialtest-
regenerator matrix frontal area, pressure ing. However, due to the geometry of the 3-D
drop, and engine corrected mass flow in the hot wire probe sensing elements, wherein
turbine discharge plane. Rig objectives in- discrete (matrix cell) velocity jets could im-
clude baseline turbine diffuser performance pinge on an individual probe element, the
mapping and regenerator flow pattern map- results of testing were highly suspect. There-
ping. Instrumentation requirements for the fore, hot wire anemometry data was used to
diffuser performance are shown in Figure 172. ascertain flow trends within the plenums, and
Special instrumentation (hot wire anemom- core pressure drop data was used during later
etery) was required for accurate low level testing for analysis.
124
1 PS TAP NO
1 Ps TAP NO 47
12 Ps TAPS NO :]4
(HOLE PREDRILLED THRU NO 45
ON P/N 3608127)
EQUALLY SPACED
S PT BRA HEADS
NO 20T J NO 25
- EQUALLY SPACED
tHOLES 4 TAPS
REGENERATOR
ARE PREPARED ON
CORE (LP| P/N 3608124
SWAGE LOK
6 REQUIRED
1 PS TAP NO 49_
TYP 6 PLACES
;UST DIFFUSER
19 PS TAPS NO 1
\k 8 C
THRU NO 19
tHOLES FOR STATIC
19 PS TAPS NO 50
EXTEND PS TUBES
THRU NO 68
STRAIGHT BACK FOR
(HOLES FOR STATIC
18.00 MIN LENGTH PRESSURE TAPS ARE
PREDRILLED ON
NO SEALLANT P/N 3608125)
REQUIRED AROUND
THRU NO 12
EQUALLY SPACED
CIRCUMFERENTIALLY
CIRCUMFERENTIALL Y
PS NO62
NO 13
/ NO 84
Ps NO
m
/
- P$ NO 6S
/ PS NO 67
-- PS NO 68
125
/
./
• /
i
126 oi,"i-'.oOi<
QUA//2.M
A series of tests were conducted at simu- drop) for the LP core face imposed by engine
lated turbine rotor exit swirl angles and re- flowpath geometry at the simulated cruise
spective flows to determine the effect of swirl condition.
on regenerator LP inlet pressure distortion.
Swirl angles of +55 degrees (idle), 0 degrees Several flow influencing devices were eval-
(cruise), and -27 degrees (maximum power) uated to determine the potential of reducing
were induced at the rotor exit plane. Concur- LP inlet flow distortion. Downstream devices
rent 3-D analysis showed that circumferential (baffles) showed limited potential for reducing
distortion of comparatively large magnitude LP inlet flow distortion. An upstream
has a negligible effect on regenerator effec- "diverter," Figure 176 showed good potential
tiveness when gas/matrix heat transfer and for redistributing the flow, as noted in Figure
core rotation effects are considered. 177. The parameter U/VRE F seen in Figure
177 is based on 3-element anemometer data
Tests also were conducted at various mass
flows [hence Mach number and plenum head Q
(ev2/2g)] and 0 degrees swirl. These tests 3.8 CM
were conducted to determine effects of mass UPSTREAMDIVERTER [1 5
TURBINE
flow variations on regenerator LP-inlet pres- DIFFUSER
sure. Distortion magnitude remains approxi- -,< EXiT
"\ "_"
o
mately linear with inlet Q as mass flow rates
increase.
Figure 175 presents the observed inlet Figure 176. LP Regenerator Cold Rig
pressure distortion (local cold core pressure Upstream Diverter.
kPa (IHH20i
2.0
1.0
'rEST.7 I[
O-tO_ II
,.,co,.oO,,,A
cRuisc,,,ol,,o,s I CRUISE CONDITION _,.._
CIRCUMFERENTIAL l _, I I
1.5 -- WITHOUT OIVERTER __ 7"-
3.5_[- POSITION. DEGREES--
Ii CRUISE CONDITtON
WITH OIVERTER
/ /
!
I ! I
!
I
25 RAW TES _J
PHI 4 5 | 7 O 5.0 6.0 7.0 6.0
IIN) 4.0
i I I
I I I
CM 10 15 CM 10 i5 2O
RADIUS
RADIUS
U7.07_358 667.078-,180
127
and is the ratio of local to average axial 5.4.2.2 Regenerator High Pressure (HP)
velocity at core inlet. Cold Rig
CLEARACRYLIC
/
_X
COMBUSTOR
REGENCORE /" INLET
G87-078-393
128
cluded for the determination of the combustor Figure 180 shows the HP regenerator cold
annulus inlet velocity profile such that an rig test data used for subsequent analysis.
optimum shape could be determined for the Testing was conducted both with and without
regenerator exit/combustor inlet guide vane the HP-inlet housing (exhaust housing) and
configuration. A uniform circumferential flow confirmed that HP-inlet "flow distortion is
profile is desired at the combustor inlet to dominated almost solely by hot face flow
assure the best flame control and primary/ separator housing geometry (downstream bon-
secondary mixing in the combustor. Effects of net).
this guide vane selection on the regenerator kPa IINH201
flow profile were also determined. IJ /
NP COLO SiS OATA CllLCUMF'ERENTIAL
TEST I(.10 POSITIONS.OESREES
0.44
Regenerator HP Rig Testing 12-12,E) o--340
15 I
path.
liNI 4 5 S 8
t I I
Several flow influencing devices (bonnets) CM 10 15 20
were evaluated on the downstream HP flow- RADIUS
Regenerator Analysis
129
the entire regenerator system. The results core matrix, are determined using local prop-
described here refer only to core effective- erties (i.e.,local Reynold's Number, viscosity,
ness. Mass flows used in the 3-D analysis for etc). The analytical model also includes
both the LP and HP flowpaths have been effects of local radial and axial conductive
adjusted for predicted seal leakages. heat transfer to neighboring elements. Indi-
vidual elements are analyzed for heat transfer
Analytical Model along five paths (four core conduction and one
gas convection path). Time integration is used
Regenerator core effectiveness was ana- to arrive at a steady-state heat transfer solu-
lytically predicted by imposing measured or tion that is consistent with this pressure dis-
prescribed core inlet face pressure distortion tortion profile imposed at the HP and LP inlet
profiles on the rotating 3-D heat transfer planes.
mode. Figure 181 shows the principle features
of the analysis wherein matrix geometry, Sample Procedure
Colburn number characteristic, Fanning fric-
tion factor characteristic and core rotational As an aid in explaining the test and analyt-
speed are program inputs. Heat transfer and ical procedures, the following paragraphs
core pressure drop calculations, within the describe the steps involved in obtaining an
analytical prediction of regenerator perfor-
mance in the engine. Since the cruise condi-
tion is of most interest, it is the subject of the
P = ,_lr, el
example case.
"" ---CORE
Assuming that the core face stagnation
pressure is essentially unaffected by the in-
K, AXIAL STATION strumentation measurement technique, the
GB7.078-364 axial velocity through the core corresponds to
only about 0.25 mm (0.01-inch) H20 velocity
Figure 181. Measured Analytical Flow head (approximately one percent of the peak-
Distortion Model. to-peak distortion level).
130
Figures 182 and 183 describe the raw cold Step 2: Test Data Preparation
rig AP (local cold core pressure drop) data for
the HP and LP rigs. Note the excellent The Ap data shown was scaled slightly
agreement between the theoretical (calculated upward [by the ratio of P(c_,/_-o) 2] to match
from the core matrix Fanning friction factor the latest predicted engine hot face corrected
data) AP for uniform flow and the average flow and Mach number at the cruise condition.
measured Ap in both cases.
This step is required solely because engine
predicted stage points had changed slightly
kPa IIN H Ol between test and analysis stages.
1.0
RP COLO. 'RiG OATA CIRCUMFERENTIAL I ]
0.44 -
TEST..,0. U.,2-aO POSmO,._.
DEGREES Step 3: Analytical Input
I -2 OONNiET e-- 340 [ I
,.,,,,,. '0/ 6 = 0.35 LD/SEC c-- 310
I t o- 2,0 I / The scaled HP and LP pressure field data
1.7
"_" 0.42 - were input to the 3-D analysis as hot face
pressure boundary conditions. The analysis
THEORE L FOR allows a uniform pressure drop bias to pass the
0.40 . I _ _ _ FLOW AT TEST CONOITIONS I required flow rates. However, the variable
portion of the pressure profile is preserved.
The gross level of pressure drop is a result of
core matrix pressure drop while the variable
I lAW TE OATA (profile) portion is the result of flowpath
,,, !
[INJ 4 0 O 7 0 geometry and flow redistribution patterns.
I t f
CM I0 15 20
![....
.7
| THEORETICAL L_P FOR-
_ONIFOflM FLOW AT TEST
|
_
_
---]
_
-3
I
Figure 184 shows the analytical prediction
of capacity rate ratio (CRR) and LP and HP
mass velocities (F = pV), which result from the
imposed
tions.
(test) pressure fields and flow condi-
The mass velocities and CRR are
,, I ,,wTE,,- L L j circumferentially
station in Figure
averaged
184. Note
at each
that CRR
radial
is
IINI 4 5 O 7
I I defined here as the ratio of LP-capacity rate
CM 10 15 2O
divided by HP-capacity rate and is not neces-
RADIUS
Gll7-07_366
sarily equal to CMin/Cma x. Figures 185 and
186 summarize the analytically predicted
Figure 183. Measured LP AP Data From cruise discharge face gas isotherms and mass
Regenerator Cold Rig. flux contours.
131
RATIO
iFi = C
ko/s.m 2 [LiIM/S.FT2|
T 5 = iO03C [200OF]
T2 = IOX 1218Fi
--_ _ ,,,,.f6 = ii¥ : _/AL LD/S-FT2
TEST DATA WI
ANALYSIS I AVG TT : 173C (343FI
2..O L4 4 5 S _ _
PNI
t I J
CN 10 15 29
RADIUS
Sit74711..367
132
hub to shroud. Note the difference in LP and
LBM/S.FT 2 = KO/S-M2
HP sensitivity.
0.5 2.4
MASS VELOCITY IN KG/S-M2 (LB/S-FT 2] 0.6 2.9
Early measured LP-cold flow data for the
0.7 3.4
0.8 3,9 low cruise condition was analyzed with a uni-
0.9 4.4 form (ideal) HP inlet flow. Case 8 results,
° 1.0 4,9
shown in Figure 187, indicates that the distor-
TEST OATA i
tion measured on the LP rig yields an effec-
tiveness degradation of (0.0043) equivalent to
a linear radial LP inlet distortion profile of
ANA_ 0.14 kPa (0.56-inch) H20.
,-.-1 . I +? --0"
13 and 14 can be used to evaluate the effects
of LP-eircumferential pressure distortion.
Case 14 is a case with a hypothetical circum-
ferential pressure distortion of 0.55 kPa (2.23
inches H20) (positive gradient in the direction
of rotation). This magnitude is two to ten
times greater in peak-to-peak magnitude than
the observed cold flow radial distortions, and
yet results in a negligible (A - 0.0001) deg-
radation of effectiveness. Other cases (HP
270° side and negative gradients), not included in
GeT-07e.369 VIEWEDFROM COMBUSTOR
END Table 24 show equal or lesser impact. Cir-
cumferential distortion of any reasonable
Figure 186. Predicted AGT101 magnitude is not considered to impact regen-
Regenerator Local Core Mass Velocities erator performance.
for the Cruise Condition Based on Cold
Rig Pressure Distortions. Cases 9, 12, and 16 are traditional 1-D
analyses and are provided for comparison with
(cases 1 through 8) was conducted using early Cases 10, 13, and 17, which are 3-D analyses.
engine cycle statepoint data corresponding to Cases 11, 15, and 18 are analytical evaluations
a low cruise 11.2 kw (15 hp) condition. Sub- using distortion profiles measured during LP
sequent work (cases 9 through 18) was per- and HP cold flow testing. Both the LP and HP
formed using current 1371C (2500F) engine inlet flowpaths are untreated (no baffles or
statepoints. flow diverters) and the magnitude of distortion
is corrected from cold test conditions to en-
Results of ease studies showed good agree- gine__ope_ating conditions by the ratio of
ment between the traditional 1-dimensional P(_Je/6)'.
(l-D) solution and the 3-dimensional (3-D)
finite element solution for undistorted cases. Cases 11, 15, and 18 results are utilized in
the construction of Figure 188, where effec-
Figure 187 presents results of cases 2 tiveness and fuel flow penalties are projected
through 8. These case studies, with hypotheti- as a function of engine horsepower. These
cal distortion were configured to evaluate and projections are determined through the use of
quantify the effect of radial inlet distortion engine performance and CFDC computer
profiles. The prescribed inlet distortion pro- models. Since the majority of fuel consumed
file for these cases is linear with radius from over the CFDC occurs in the 0 to 29.8 kw (0 to
133
Table 24. Regenerator Analysis Summary.
Effectiveness
ATIATM A x)
Engine LP Core Inlet HP Core Inlet
Case Power Distortion Distortion EHp ELp
*AP maps scaled from cold flow rig for appropriate corrected flow
**Linear variation of (P SHROUD-PHUB) in inches H20.
0.97 ; i \ - "_ • •
_ I [ i I _, I _TEO
I I ] ] t \ [ _ lip SlOE mEAL
P
2_
I I i i : Ire SJpE
mEAL , T",.C_E5 tJ.
[INHzOI 0 0.2 0.4 OJ 0.9 1,0 12 1.4 |J 1.9 2,0 T[ST DATA ANALYSIS
kPa
I
1.0 0.4
I
0 I t I o
0 IO 2O _ 4O 5O 8O 7O 60 on ioo
HYPOTHETICAL LINEAL RADIAL OISTORTION
ENGINE NET POWER. {HORSEPOWERI
OF CORE iNLET VELOCITY HEAD [PSHROUO -- PHURJ
G87.078371
GB7_78.370
134
40 hp) range, the expected fuel consumption
REGENERATORCORE
penalty for an engine without regenerator dis- ASSEMBLY
tortion treatment is predicted to be approxi-
DISCHARGEFLOW
mately 3.5 percent. (COLO GA
New seal break-in interval (ideal con- Hot Regenerator Test Results
ditionsfor approximately 10 hours)
The regenerator hot test rig was assembled
- Core drive torque during engine start and installed in the test facility. During rig
sequencing Builds 1 and 2, minor assembly and laboratory
problems precluded testing. Build 3 of the rig
- Steady-state torque at idle, cruise, was completed and testing initiated. With the
maximum power engine conditions. NGK core and first-generation Ford regenera-
tor seals, static leak checks showed excessive
O Verify matrix Ap/p (HP/LP) at idle,cruise, leakage (=25 percent of compressor inlet
maximum power simulated engine condi- flow). The unit was disassembled and a series
tions of vacuum leak tests were conducted. Several
areas were noted as contributors with a signi-
Measure cavity pressure at core ID under ficant leakage found in the NGK core. This
idle, cruise, maximum power simulated core exhibited excessive through wall porosity
engine conditions, and size-bleed orifice to resulting in approximately 40 percent of the
LP discharge to limit pressure in this area total cold leakage noted earlier. Subsequent
testing of the Corning thin wall cores exhib-
The regenerator hot rig design is shown in ited negligible leakage. Modifications were
Figure 189. The rig was designed to minimize incorporated to the test rig and the Corning
leakage paths (at seal locations)by eliminating core installed for Build 4.
135
Build 4 was completed and the unit instal- accurately to approximately 0.2 percent of the
led in the test cell. Initial operation of the rig HP inlet flow.
was conducted at ideal conditions [equivalent
to 870C (1600F) TIT] for approximately 4 Due to requirements of the 871C (1600F)
hours to break in (or glaze) the seals prior to engine test program, testing was limited to an
performance mapping. idle condition only. Additional testing will be
conducted following engine testing.
Further testing wasconducted at simulated
engine conditions. Instrumentation was lo- At points near idle conditions, leakage was
cated upstream and downstream of the HP and measured at 0.26 kg/min (0.576 lb/min),
LP core faces. Thermocouple rakes were approximately 5.2 percent of test compressor
located in equal area planes at five radial flow. Figure 191 shows the LP and HP core
locations, spaced approximately 35 degrees exhaust temperature profiles at the simulated
apart. idle condition. The tested temperature effec-
tiveness of the HP side of the regenerator was
Dynamic seal leakage was determined 95.9 percent at idle conditions (Table 25).
using a unique helium flow seeding technique
depicted in Figure 190. Helium is injected and Figure 191 shows that the radial tem-
perature gradients of the discharge gases at
the carryover points (170- and 350-degree
arcs) are minimal indicating insignificantflow
distortion effects.
NORMAL
ENGINE
Temperature effectiveness of the regener-
I TURBINE ENVELOPE
mixed at selected stations upstream of the HP Each of these seal sets were installed and
inlet. Flow passing through the HP side of the tested in the hot regenerator rig under nom-
core is then ducted overboard. Conditioned inal operating conditions (T3.1 =120Cor250F,
LP flow is then introduced to the slave burner T5.1 --650C or 1200F).
to maintain proper LP and HP flow match.
Fuel is introduced and combustion initiated. The third seal set with welded diaphragms
Regenerator seal leakage from the HP side exhibited such high seal loading resulting in
(helium seeded flow) to the LP side (unseeded) excessive drive torque and prohibited the mea-
can then be determined using a mass spec- surement of useful data. In fact, while
trometer to measure helium concentration attempting to test these seals, the rinK gears
levels at the LP exhaust. Leakage is measured were separated from two regenerator cores as
136
Table 25. Regenerator Rig
Test Results.
Metal
Engine
(871C - Regenerator
1600F) Rig Test
Predieted Test Results
HP Inlet Tempera- 7O 74
a result of drive torques in the 41 to 62 kg-m Relative to the best of the earlier seal
(300 to 450 ft-lb) range. configurations neither of these seal sets exhib-
ited improvement.
Successful tests were completed on the
baseline and tapered seal sets. The drive Instrumentation was added to this rig to
torque and leakage characteristic for these measure the variations in seal clearance at the
137
PHASE IV -- BASELINE
m_ HX.-021
CX..021
HOT-OYNAMIC
407
(3OOJ
PHASE IV -- TAPERED
8 HX-023
CX-022
117-6l
HOT DYNAMIC
271
NREG ,,_ 12 RPM
'_" {2OOJ
T3.1 = 121C (250FI
6
T5.1 = 649C (1200F)
ll3.2)
_12 E
t IV -- BASELINE
CX-021
(111111
E IV -- TAPEREO
HX-023 CX-022
GB7_7_379A
o
(Ol
0 138 276 4]4 Figure 193. Regenerator Drive Torque.
{OI 1201 140} 160l
138
4.5
I1O.OI
© 1.32 MM (0.052 IN) SEALCLEARANCE
136
_-- [I00) COLDSEAl.:CS-024 _ 2
PHASEV
CORNIN6CORE:S/N FM-44-006 ._ i4.4)
..=.
SPEEO:14 RPM
T3.1 -- 121C 1250F) -_
T5.1 -- 649C1120OF)
0 TESTOATE:3-18/3-17-84
IO) I ] I
0
Figure 194. Phase V Regenerator Seal fOl
0 138 276 4 4
Drive Torque Versus Seal Pressure.
fOl 120J 140) 160}
SEALPRESSURE.
kPa (PSIG)
Relative to the best of the earlier genera- GB7-O78-381A
139
KS/Mill
PHASEIV
paths. Power is input at the planetary sun
n_o)'i / ROVEMRER
SS gear and extracted from the planetary carrier.
/ I0 i't CLEARANCE
= 1,3-2.0 mm IO.05Z-O.077tNI In this planetary system, all elements rotate
and the relative speeds are interdependent.
:--,] /-.,
-- CLEARANCE: 1,3 in \ One power path extends directly from the sun
gear to the carrier; the second power path
passes through the planetary ring gear to a
_ IS.el B variable stator torque converter (VSTC) that is
used as a speed changing device. The torque
converter variable output speed is connected
1 ./ SE
to the carrier through a clutch that is open
12,2
2
1 .//.I_RASE
_-
Ill
during vehicle idle operation and closed during
I1
/ 10.053 till normal driving modes. Speed ratio modulation
across the VSTC results in a variable output
O'l Ot , , , , , i
O 138 276 414 speed of the planetary carrier, which in turn is
IOI 1201 1401 1601 geared directly into the AOD transmission.
SEALPRESSUREOIFFEREllTIALILIPI. kPaiPSli Step ratio changes in the AOD are phased with
I I a off-setting speed ratio changes in the variable
0 200 400
speed gearbox to produce a continuously vari-
SEAL PRESSURE.KPa [PSIGI
R74711-3iN
able drive line system.
Figure 196. AGT101 Regenerator Seal Leakage. The AGT101 drive system schematic is
shown in Figure 198.
140
drawings were completed for the Ford AOD 5.6 Controls and Accessories
transmission modifications, and drawings for
the differential gear and housings had been The engine electronic control unit (ECU)
made at the time of curtailment of the trans- and the fuel control unit evolved significantly
mission and vehicle phase of the AGTI01 pro- during the course of the program. Initial
gram. Consider that although the transmission design of these components was made assum-
arrangement illustrated in Figure 199 repre- ing an automotive installation. The ECU soft-
sents new technology, the components includ- ware and hardware provided for many vehicle
ing variable stator torque converter consist of powertrain functions such as transmission op-
proven technology. eration in addition to engine control, and the
KEY
X RATIO 12 Op
.2' 31T OVERRUNNINGCLUTCH
=" jg" N = 1716-3684
CARRIER
II
N = 4069 - 8736
I _ r--I
ZTLJ 35T [____J J MAIN OIL
i
[]72T 0
Z RATIO alw
Dp = 12
75T
AOD
AOD INPUT SHAFT N = 0 - 2564
(SR = 0.85l
REARAXLE RATIO
/
-__ 8RAKE
- _ STARTER
141
ORIGINAL PAGE IS
011 POOR .QUALITX
41.9 CM
(16.5 IN] = i
I
ACCESSORY
ORIVE
"X" RATIO
\
\
10.80 IN
DIA
AO0
"Z" RATIO
ViEW ROTATED
90 OEGREES
LUBRICATION
PUMP
AOO
INPUT SHAFT
STARTER PAO
G87-078-356
fuel control was designed as a compact unit the transmission as well as the engine. This
for vehicular installation that operated on a 12 unit became obsolete as control technology
volt dc electrical system. Though they rep- progressed during the course of the program
resented the state of 1980 technology, these and the demands of laboratory ceramic engine
components lacked the flexibility required for testing became more and more difficult to
a laboratory test program. As a result, both meet.
components were redesigned Io delete the
vehicular features and enhance the flexibility A new ECU was designed and fabricated
required for laboratory testing. which featured improved flexibility over the
original ECU. The new ECU, shown in Figure
5.6.1 Engine Electronic Control Unit 201, consisted of 3 standard off-the-shelf
boards, 1 iSBX board, 5 custom driver boards,
The initial ECU was based on an Intel 8086 a standard card cage and a RS232 adapter. By
microprocessor and incorporated 10 analog and utilizing the commercial boards the ECU will
2 digital control boards. This unit featured be easily supported or expanded in the future
both static (manual) and dynamic (automatic) to include new functions as they are needed.
control software and monitored all aspects of The commercial boards used in this new design
the vehicle powertrain operation controlling are:
142
1000.
700-
64o
62o
_o
75°
697-078-36 101198-1
143
The ECU logic provides for full authority range of fuel flows from 0 to 20.4 kg/hr (0 to
control of the engine during testing. Engine 45 Ib/hr). The system was driven by a con-
fuel flow and variable inlet guide vanes(VIGV) stant speed 440 vac motor and mounted in its
are modulated according to operator changes own cart for easy access and transportation.
in engine speed setpoints and dynamometer
load conditions. The ECU will provide for 5.6.3 Variable Inlet Guide Vane Actuator
either manual or automatic operation of the
VIGV and start functions. Engine protection is The variable inletguide vane actuator used
provided for low oil pressure,high oil temper- during AGT101 engine testing was a torque
ature, overspeed, underspeed, and extreme motor actuated hydraulically driven unit. The
engine station temperatures (turbine inlet, actuator design was identical to that used in
turbine discharge, regenerator LP discharge). Garrett's GTCP331 series APUs and no devel-
The ECU logic diagram is shownin Figure 202. opment or modification was required.
The original AGT101 engine fuel control Engine temperature measurement for con-
was a three piston'pump with a pulse width trol and monitoring are provided by standard
modulated (PWM) fuel metering unit. This Garrett laboratory thermocouples. Type K
system was compact, driven by a 0.09 kw (I/8 (Chromel/Alumel) thermocouples are used for
hp) 12 vdc motor and mounted on the engine all temperature locations except for turbine
test cart. Repeatability, hysteresis,linearity, inlet which used Platinum/Platinum-10 per-
and frequency response were allimproved over cent Rhodium thermocouples. These probes
existing proportional metering systems. Dif- are a shielded open bead design which opti-
ficulty arose when attempts were made to mizes thermocouple response with respect to
measure fuel flow with the PWM system. radiation error.
The fuel flows required for engine testing The hydraulic system low oil pressure
ranged from 0.36 to 20.4 kg/hr (0.8 to 45 switch incorporates a "shunt disc" actuating
Ib/hr). This exceeded the range of the turbine element. A resistive element temperature
flow meters available and necessitated the use sensor is specified to monitor high oil temper-
of a Coreiolis type mass flow measurement ature and ambient air temperature.
unit such as the one provided by Micromotion
R. The pulse frequency of the PWM system Engine speed sensing is accomplished using
with the piston pump, interfered with the mass an eddy current killed oscillator transducer
measurement of Micromotion system causing with a miniature 1.78 mm (0.070 inch) diam-
erroneous readings. Since fuel flow measure- eter probe tip supplied by Bently, Nevada
ment was required for laboratory evaluations, Corp. This probe is mounted in the engine
an equivalent fuel control was designed and inlet housing and targets the stepped surface
fabricated for use in the laboratory. of the compressor shaft OD.
The new fuel control was based on the Connectors selected for development use
design used in Garrett's GTCP36-100 APU. are MIL-C-5015 threaded connectors with 16
The schematic in Figure 203 shows the fuel gauge contacts. The ECU and engine harness
circuit in this design. This unit featured a had two connectors with 48 and 36 contacts
gear pump with an internal bypass circuit and for total of 84 terminations. The 48 and 36
a combination of 70 micron filterscreen and a contact connectors were common with the
cartridge filter. Fuel was metered with a boom cables and interface connectors in the
torque motor specially selected to allow a Garrett test facilities.
144
ORIG_qAL PAGE I8
_OF POOR QUALIT_
I
I
cp
145
HIGH-PRESSUREPUMP
PUMP OISCRARGEPORT
METERING VALVE H
70-MICRON SCREEN MOTOR
_ PLUMBING TO BE
ItM
TESTING
il PROVIOEDFOR
METEREO
GB7-078.37 PRESSUREIeoJ
O_:LIGINAL PAGE IS
OE POOR QUALITY
146
!
6.0 CERAMIC MATERIALS AND COMPONENT DEVELOPMENT
6.1 Ceramic Materials Testing Many silicon nitride materials were tested
to determine suitablity for AGT rotor use.
Many materials such as ASEA, Ford RM-20,
6.1.1 Fast Fracture and Stress Rupture
Kyocera SN 220M, NGK SN-73, and SN-81
Testing
were eliminated for rotor use based on the
inadequate elevated temperature properties.
The fast fracture, four-point flexure Four more advanced materials, NGK SN-82,
strength of ceramic materials used for com- NGK SN-84, Kyocera SN 250M and Kyocera
ponents in the AGT engine have been contin- SN 270M did have adequate properties for
uously monitored over the AGT program. Both rotors based on the testing of fabricated test
fabricated test specimens and specimens ma- bars. Unfortunately, two of the four mater-
chined from components have been tested. ials, NGK SN-82 and Kyocera SN 270M could
not be successfully formed into the complex
rotor configuration. The remaining two ma-
All four-point flexure testing was con-
terials Kyocera SN 250M and NGK SN-84 were
ducted using self-aligning metal (for room
successfully fabricated into the AGT101 rotor
temperature) and hot pressed SiC (for elevated
shape. Rotors of both materials were cut into
temperature) fixtures. The outer span dimen-
test specimens. The specimens were tested
sion is 38.1ram (1.5 inches) and the inner span
for both fast fracture strength and stress
dimenson is 19.1ram (0.75 inch). The load is
rupture. The material cut from the Kyocera
applied using a crosshead speed of 0.5ram/rain
SN 250M rotors has considerably lower
(0.02 inch/minute). Specimen cross sections
strength at elevated temperatures (Figure 204,
were typically 3.2 x 6.4ram (0.125 x 0.250
View G) and two- to three-orders of magni-
inch) except where noted.
tude lower stress rupture life than specimens
fabricated as test specimens (Figure 204, View
Test specimens were machined with 320 H). The poor elevated temperature material
grit diamond wheels longitudinal to the speci- properties of the Kyocera SN 250M rotors
men length unless noted otherwise. The speci- makes them unsuitable for long term, 1371C
men corners were chamfered 0.127-0.254mm
(2500F) TIT engine testing.
(0.005 - 0.010 inch) at a 45 degree angle. Test
data generated during the first five years of Two NGK SN-84 sintered silicon nitride
the AGT program is summarized in Table 26. rotors were cut into test specimens to com-
In general, the strength of fabricated test pare the fast fracture strength and stress
specimens has been very close to the strength rupture life to that of fabricated test speci-
of specimens cut from components. mens. The fast fracture strength of rotor S/N
135 material (Figure 204, View Q) is slightly
During the last two years of the program more lower than the fabricated specimens (Figure
extensive material property testing was initi- 204, View P), at elevated temperature but is
ated to characterize the advanced silicon ni- still>689.5 MPa (i00 ksi) at temperatures
tride and silicon carbide materials. Typically, <1260C (2300F). The fast fracture strength
fast fracture testing was conducted at up to of rotor S/N 136 is lower than measured on
ten temperatures with between five and thirty rotor S/N 135 but the elevated temperature
specimens per temperature. In addition flex- fast fracture strength at temperature
ural stress rupture testing was conducted at <1260C (2300F) is greater than 586MPa (85
typically three temperatures and at four k-si). The flexural stress rupture life of the
stresses chosen to result in stress rupture Hves rotor specimens are approximately one order
of <150 hours. The materials, test and of magnitude less than the stress rupture life
specimen sources are listed in Table 27. of the fabricated test specimens.
147
Table 26. AGT101 Component And Material Summary.
ACC
Inner DIffuser RBSN Slip As-Fired 49.7 4.5 30 52.1 0.t 2200 10 44.34 8.0 21 ID
Outer Diffuser (RBNI04) Cast I,ongitudineUy 53.2 6.5 10 46.3 5.3 27 OD
Turbine Shroud Ground 50.0 15.4 17 1"5
Oaffle Ileat Treated 54.8 8.5 29 31.1 5.7 5 O
Sin tered Slip Longitudinally 89.8 7.2 9 50.3 13.0 2200 10 119.0 21.4 10 99.0 10.3 [800
Si3N 4 7 Cast Ground
Code 2 63.7 9.3 2200
Standard Oil
Turbine Shroud, SASC Injection As-Fired 48.6 9.5 30 45.0 5.0 2500 10 55.45 7.1 9
ate for Molded
Combustor SASC SUp LongitudinalP/ 49.4 5.8 30 41.4 6.7 2500 10 53.0 7.3 9
oa rrle Cast Ground 51.6 8.9 4
Transition SASC Isopre_ed I,ongitudinally 57.79 7.7 30 56.2 11.9 2500 10 54.4 ! 6.2 5
Due4 Regen- Ground 34.3 ; 9.1 23 36.9 6.8
erator Shield, 41.8 14.2 12
lluckshroud
Ford
I
Rotor SRBSH Sllp I,Onl_itudinally 109.3 19.B 6 73.1 !16.4 2200 6
(RM-2) Cast Ground
NGK
Baekshroud, SIntered Isopr espied Longitudinally 87.6 10.5 10 47.1 13.6 2000 7
Trmlsl lion Si 3 N4 (;round
Duet, (aN-50)
Diffusers
Kyocera
Coming
Flow Separatoe LAS Slip longitudinally 14.0 19.8 II 13.5 9.7 2000 12 12.9 5.3 10 13.4 3.4 1800 5
IIousing l5.4 8. l 2000 10
16.0 7.7 2050 9
All test bars 0.250 x 0.125 inch cross section unle.,B noted. Bars tested in 4-point Rexure, 1.50 inch outer span end 0.75 inch inner _pan. Cross head speed, 0.02
inch/minute
ITcst bar cross seetlon 0.31 x 0.15 inch 4"rest bar cross section 0.236 x 0.1 inch 7Code I = 8%-Y203, 4%-AI203
2Characteristic strength, kst GAs machined, longitudinally ground Code 2 = 6%-Y203, 2%-AI203
OF POOR QUALITY
148
Table 27. Fast Fracture and Stress Rupture Data was Measured for
Many Advaneed Si3N 4 and SiC Materials.
(Figure 204)
Silicon Nitride
ASEA A m
Ford RM-20 B m m
Kyocera SN 220M C D
Kyocera SN 250M E G F H
Kyocera SN 270M I J
NGK SN-73 K
NGK SN-81 L M
NGK SN-82 N O
NGK SN-84 P Q R R
Silicon Carbide
Kyocera SC201 S
Standard Oil SASC T mD
Based on this data SN-84 appears to be a contact area. The specimens were heated to
material that can be used for limited 1371C the appropriate temperature while dead
(2500F) TIT engine testing. weight loaded at a minimum simulated engine
assembly load. Once at temperature, addi-
Over the seven years of the AGT101 pro- tional dead weight loads were applied, as
gram large improvements have been made in required, to simulate engine aerodynamic or
high performance ceramic materials. Addi- mechanical loads and held for 20 hours. Un-
tional work must be done to increase the loading and cooldown followed. The specimens
elevated temperature material properties, then were inspected for sticking phenomena.
fracture toughness and shape capability. Three classifications were assigned; no stick
or reaction (NSR); light sticking (LS) upon
6.1.2 Ceramic Compatibility Testing cooldown, ie, came apart during handling; and
hard sticking (HS), not separable by hand.
In conjunction with ceramic component Concern is raised for LS and HS conditions due
tests, an interface compatibility study was to the following:
conducted. All interface conditions for the
AGT101 have been identified, as shown in
o L8 - longer exposure may result in hard
Figure 205, along with respective stress and
sticking
temperature environments for the three
engine operating conditions [871, 1149, and
1371C (1600, 2100, and 2500F) TIT]. Test bars O HS - could result in component fracture if
of as-machined or as-processed material were the parts thermally expand or cool down at
stacked with a 6.4 x 6.4ram (0.25 x 0.25-inch) differing rates
149
MPz IKStl
150-
1000"
14D-
130-
120-
800'
liD-
100-
90-
600"
80-
IlOl
70-
60-
4O0"
50-
1101
40- MATERIAL -- ASEA SI3N4 2*/2% Y203
DATE RECEIVED-- 1966 IlOI _'t
O" 0 | l I ! I !
TEMPERATUREIF}
,I
0 ,
200 v
400 i
600 w
800 '
1000 I 2'0
0 I 4'0
0
TEMPERATURE. C
GII7-OTB-BO A
Figure 204. View A. Four-Point Flexure Strength of ASEA Si3N4-2½ Pereent Y203 .
150
MPa (KSII
150-
1000'
140-
130-
120-
800"
IlO.
100-
151
90-
600"
80- 151
16D\
\
70-
\_,,\
60-
151
50=
MATERIAL -- FORD RM20 SRBSN
0
I I ! I l I
500 1000 1500 2000 2500 3000
TEMPERATURE (F)
TEMPERATURE. C
GB7Q78.61A
Figure 204 (Contd). View B. Four-Point Flexure Strength of Ford RM-20, HIPped by ASEA,
Cut From Rotor S/N 96.
151
MPz tKsq
150-
1000'
140-
130-
120-
800'
IlO-
100-
I101
90-
•- 600' %%
%
8o- {101
I10i
I0-
O,
U" ! I ! | ! I
500 1000 1,500 2000 2500 3000
TEMPERATURE {FJ
! ! ! ! I I ! !
O 200 400 600 800 1000 1200 1400
TEMPERATURE, C
GD7,.076-$2 A
Figure 204 (Contd). View C. Four-Point Flexure Strength of Kyoeera SN 220M Sintered
SUieon Nitride.
152
MPa (KSI)
80-
TEST TEMPERATURE --
e- 1093C (200OF)
•- 1204F (2200FI
60-
400, SPECIMEN CROSS SECTION -- 3.2 X 6.4 MM (% X ',_ INCHI
m= 300"
40-
30-
200 -
20-
100"
I0-
0 I ] I I I
O01 0.1 1.0 10 I00 1000
TIME TO FAILURE. HOURS
GO7-O78-83A
153
MPa IKSli
150-
1000"
140-
130-
120-
800 • iSi
110-
100-
_m m _ _l_ _ _ m _ _ m _ m ......
_ f301 151 T
80- \ .... 15
f51
I_OI
70-
151 L'lO)
400-
60- IIOI
!
50-
O
O" J i , i l !
TEMPERATURE IFI
I I I i
Figure 204 (Contd). View E. Four-Point Flexure Strength of Kyocera SN 250M Sintered
Silicon Nitride.
154
MPa IKSII
80-
500 %1 • • _A
70-
"_%% %%
400.
'_%%% %%% %%,%
%%_ • _ • %
50-
300-
40-
30-
OATE
RECE,"EO-
lg_ "_"
200-
TEST TEMPERATURE %%
.-12O,C)Z200F) %% i_cFi
nn- 1315C)240OF)
2'0- • -- 1370C 12500F)
0 "
0, I 1 I I I
0.01 0.1 1.0 10 100 1000
TIME TO FAILURE. HOURS
GB7-O78-BSA
155
MPa IKSll
150-
1000"
140-
130-
12D-
I10,
Z_5I
100-
__ _'_" _ _ SN 250M
k
90-
80-
__,_ _l A
70-
00°
400-
0" ! I ! ! ! J
0 500 1000 1500 2800 2500 3000
TEMPERATUREIFI
I I I I I ! I I
0 200 400 600 800 1000 1200 1400
6117
o7sM TEMPERATURE C
Figure 204 (Contd). View G. Four-Point Flexure Strength Comparison of Kyoeera SN 250M
Cut From Rotors and Fabricated as Test Bar Specimens.
156
MPa IKSI)
80-
5O0
70- MATERIAL -- KYOCERASN 250M SSN
%%%%_ee
30- • • • • %_
200-
20-
100-
10-
0 ! I I I m
0.01 0.1 1.0 I0 lOG 1000
TIME TO FAILURE. HOURS
GII7..O78-87A
Figure 204 (Contd). View H. Stress Rupture Lives of Kyocera SN 250M From Rotors is
Considerably Less Than That Fabricated as Test Bars.
157
MPa (KStJ
150-
1000-
140-
130-
120 -
800'
110.
I00._
go.4 tsJ
_=
f5i 15i
804
70.
50.
400-
50-
0 =
0
I I I / I I
Figure 204 (Contd). View I. Four Point Flexure Strength of Kyoeera SN 270M
Sintered Silicon Nitride.
158
MPz (KSII
80-
5OO 70-
O0 •
400,
300"
40-
__ (2500FI
•- 1370C (2500F)
20a
•_ 1427C (26QOFI
O
I I I I t
0.01 0.1 1.0 IO IO0 tO00
TIME TO FAILURE, HOURS
G87_tO-89
159
MPo (KSll
150-
I000'_
140-
130-,
120-
800'
110-
I00" 151
90-
0= 600"
80-
\
70-
60.
41111"
50-
151 \
\
40. MATERIAL-- NGKSN-73SSN
OATERECEIVED
-- 1985 't
gATE TESTED-- 1985 151
30.
200" SPECIMENCROSSSECTION-- 3.2 X 6.4 MM [i/, X _/,,INCHI
CROSSHEADSPEEO-- 0.5 MM/MINUTE(0.02 INCH/MINUTEI
20- OUTERSPAN-- 38.1 MM 11.50INCH)
INNERSPAN-- 19.1 MM 10.75INCHI
10. BARSINDICATEDATARANGE
I J NUMBEROF SPECIMENSTESTED
O" 0 I I I I I '
TEMPERATURE.
C
GBTQ70-90A
Figure 204 (Contd). View K. Four-Point Flexure Strength of NGK SN-73 Sintered
Silicon Nitride.
160
MPa (KSI)
150-
1000"
140-
130-
120-
800"
I10-
I00-
f
90-
600"
80-
60,
400 -
IlOI
50- rio) \
O" D,
I I I I I !
0 500 1000 1500 2000 2500 3000
TEMPERATURE IF)
!
0 200
I 400
I 600
I 800
I 1000
I 1200
I I 410O
TEMPERATURE. C
GB7-O76-91A
Figure 204 (Contd). View L. Four-Point Flexure Strength of NGK SN-81 Sintered
Silicon Nitride.
161
MPa IKSII
80-
IP
%%_ 1315C • •
(2400F)
ol ! I I I I
001 0.1 1.0 I0 I00 1000
087-078-92
A TIME TO FAILURE. HOURS
162
MPa IKSII
150 T
ksi " .,_
IOOO-
140
130
120
.I--'"" L'"'"'I
800"
I10
lOO-
11Ol
" [lOl ] t
[101
I10l
'%%.
,,,
"
I
i
904
600-
_z
x
704 I101
.d
llOll
I
I
I
MATERIAL -- NGK SN-82 SSN
4O0" OATE RECEIVED -- JANUARY 1986
20-
10-
I I I I I I
TEMPERATURE. C
G97_7893A
Figure 204 (Contd). View N. Four-Point Flexure Strength of NGK SN-82 Sintered
Silicon Nitride.
163
MPz (KSll
90-
80- • • • • •
%%%%
5oo zo %%
%%
%%
400 %%%% • ,_
%%%%
• - ,003c
t_FI "....
m- _c 1_00F1 ",,_ _ fl=::
20 .-_.c 12300FI ,3_c
.-13_8c(:,,.00F] (_400F]
lOG SI'EC,MEN
CROSS
SECT,ON
-- -".2
X8.4M,,'_,X'_.,NC,,
OUTER SPAN
- _.1MM,.._o,NCHj
10 tNNER SPAN -- 19.1 MM (0.75 INCH]
o
-,,,. INDICATES SPECIMEN 010 NOT FAIL
0 I I I I I
O.Ol 0.1 1.0 IO 100 lOG0
TIME TO FAILURE. HOURS
GII7_I78-G4A
164
MPa [KSI]
150.
I000-
140.
800"
130-
120-
110.
!.... I.......
100-
90-
600-
80-
151
704
eo_
400"
{
DATE RECEIVED-- AUGUST 1986
O" 0
I T T 1 "1" 1
500 1000 1500 2000 2500 3000
TEMPERATURE IFI
i I I
o 2oo _oo _ 8_o lO_0 doo 14'oo
G67_79-gSA TEMPERATURE. C
Figure 204 (Contd). View P. Four-Point Flexure Strength of NGK SN-84 HiPped
Silicon Nitride.
165
MPa IKSII
150-
1000"
140-
130-
120-
800"
I10-
100-
(4)
]-
(101
_0-
80- (4i
151
600- 70-
9C 14)
400"
50- 14l
0 = 0 !
I I ! ! I
0 500 1000 1500 2000 2500 3000
TEMPERATURE IFI
I
0 '
200 '
400 '
600 '
800 '
1000 12'00 I 4'00
TEMPERATURE, C
H7-O78-9_A
Figure 204 (Contd). View Q. Four-Point Flexure Strength of NGK SN-84 HIPped
Silicon Nitride Cut From Rotors S/N 135 and S/N 136.
166
MPa (KSI)
Ai•i 4D
\ \ \ \\
AA • • • _0 •
500
7
\ '_ • • II| •
51
-- 1204C (2200F) • •
-- 1277C (2300FI • •
?C
ZO0-
O 0
t I I 1 i
OOI 0.1 1.0 I0 t O0 lO00
TIME TO FAILURE. HOURS
G87_7H7A
Figure 204 (Contd). View R. NGK SN-84, Flexural Stress Rupture of Test
Specimens and Rotors.
167
MPa IKSII
150-
1000-
140-
130-
120-
800"
I10-
100-
600-
o!
,mC
I101 (lOll [1
1101
MATERIAL-- KYOCERA
SC-201
(lOl
OATERECEIVED
-- 1985
30- DATETESTEO-- 1965
200'
SPECIMENCROSSSECTION-- 3.2 X 6.4 MM I% X '/, INCH[
20- CROSSHEAOSPEED-- 0.5 MM/MINUTE[0.02 INCH/MINUTEI
OUTERSPAN-- 36.1 MM [1.50 INCH}
INNERSPAN-- 10.1 MM [0.75 iNCH)
10.
BARSINDICATEOATARANGE
[ ) NUMBEROF SPECIMENSTESTEO
0 ! I i ! I !
TEMPERATURE
IFI
I I I ! I I I !
0 200 400 600 800 1000 1200 1400
TEMPERATURE,
C
GB7-O79.98A
Figure 204 (Contd). View S. Four-Point Flexure Strength of Kyoeera SC201 SSC.
168
MPa (KSll
1000"
800 •
600-
=_, .. ]
..=.
_0,
400 -
50. [lOl
1101 I101 1101
I101
MATERIAL -- STANDARD OIL SASC 1101 (IOI
I101
DATE RECEIVED -- 1985
GB7-O78-99A TEMPERATURE. C
Figure 204 (Contd). View T. Four-Point Flexure Strength of Standard Oil SASC.
169
o Detailed inspection after test must be con-
Q Ill 2300F I
12j,O75FATZ.5Ks, ducted to identify problem areas
j ' ',,\I\ 13j,55oo
o Crowned surfaces appear to help in allevi-
ating sticking phenomena
Ill
13) I ,T
Alumina - LAS Sticking Study "
12i 1975F_' AT a.3 KSI / {f--_lJ)-..-_l J .,_
13i 1550F/_ _ " Alumina thermocouple spacers and seals
,1, 2300F j / i I ('_u _ liii, .,nnn_:
have been fabricated for use on the T 4 ther-
12l 1855F _, AT 2.5 KSI "4 1 [ ""_.._'_/ [21_ .....
mocouple. These spacers and seals seat
against the LAS flow separator housing and
the SASC transition duct and are exposed to a
III 1500F AT 350 PSI """"_%'_#_" ENGINE CONFIGURATION
I'l 2500F TIT
peak temperature of approximately 1093C
12) 2100F TIT (2000F). To evaluate the potential of sticking
13) 160OF TIT
at these interfaces, a stack of LAS, A1203,
G67078-100
and SASC materials was exposed to 1093C
(2000F) for approximately 20 hours with a
compressive 15-pound load simulating engine
Figure 205. Interface Conditions for assembly. After completion of exposure and
871, 1149, 1371C (1600, 2100, 2500F) cooldown, no sticking between the LAS and
TIT Engines. alumina or between the SASC and alumina was
observed.
Table 28 summarizes the testing for interface
conditions I, II,and Ill. Testing at condition 6.1.3 Ceramic Interface Evaluation
Ill, depicted in Figure 206, was conducted
under a constant 36.9kN (8.3-ksi)load (engine Studies under the DARPA*/NAVY/Garrett
assembly preload) and results showed no stick- Ceramic Engine Demonstration Program show
ing or reaction. Materials tested include ACC that chipping and cracking of static compo-
RBSN, Standard Oil SASC, Kyocera SC201 nents, which ultimately led to engine failure,
SSC, Standard Oil SiSiC, Corning LAS, and were due to a contact stress mechanism at
NGK SN-50 SSN. interfaces. This mechanism was identified in
the DARPA program and a parallel ONR** pro-
As noted in Table 28, several material gram as localized high tensile stress due to
combinations result in sticking under condi- biaxial loading resulting from a combination of
tions I and II. Additional testing was con- axial aerodynamic loading and radial thermal
ducted for these combinations using flame- expansion relative movement.
sprayed mullite coating on one interface sur-
face. Results indicate that no sticking or Based on the DARPA and ONR program
reaction occurred with flame-sprayed mullite- studies, contact stress appears to be one of
coated surfaces. the most critical considerations of static-
structure component design and material eval-
Test results indicate that the AGT101 cer- uation. In summary, these studies show that
amic engine testing can be performed under for high sliding contact loads a large strength
the following guidelines: reduction resulted when bare surfaces were in
contact, moderate strength reduction resulted
o Attention must be given to material com- with high temperature lubricants present, and
bination selection
o Coated SASC or RBSN can be used for *Defense Advanced Research Projects Agency
selected interface combinations **Office of Naval Research
170
Table 28. Ceramic Interface Test Summary
SASC/SC201 LS 4
Test Cycle
(0.2, 1.1, and 2.5 ksi) (0.2 ksi) NSR = No stick or reaction
2 Evaluated at 36.9kN
(0.2 ksi)
171
interface evaluation was used to evaluate the
LOAD
materials and estimated contact conditions of
-0"
AGT components. (The test procedure is de-
%_ _.J scribed in the First AGT semiannual report.)
SASC
I
p,s Initial tests on
Oil's SASC were conducted
ACC's RBSN
with point contact
and Standard
RBSN
I 6.4ram crown against a 6.4ram crown (I/4-
inch crown against I/4-inch crown) at loads
ranging from 44.48 to 254.8N (I0 to 57.3
GB7OT_IOi
pounds) normal force (F N) and at temperatures
ranging from room temperature to I093C
Figure 206. Compatibility Test Condition (2000F). For the elevated temperature tests,
HI, Interface Material Combinations. the specimens were held at temperature for 30
minutes prior to application of the tangential
little or no strength reduction resulted with a force (FT). A relative movement of I mm
suitable metal compliant layer between the (0.04 inch) was applied at a rate of 0.5ram/rain
surfaces. The test apparatus developed in the (0.02 in/rain) to allow calculation of the static
DARPA program (shown in Figure 207) for and dynamic coefficients of friction.
'I I
[ CROSS
I LOAD
[ CELL [ "EAO
INSTRON
CROSS HEAO
i I
SUPPORT t !
.!
! !
PNEUMATIC
CYLINOEB
LOAD BAR AND i
LOAD _:_
Q
PLATE_
CERAMIC
SPECIMENS --"" FURNACE
I
INSTRON BASE
GB7_79-102
172
Each test was repeated six times to verify a) At room temperature, the curves for both
the test rig reproducibility and to provide a materials were continuous with no abrupt
good data base for the RBSNand SASC. Fig- change between static and dynamic coeffi-
ure 208 shows the degree of data scatter for cients of friction. The curve for RBSN
the static coefficient of friction versus the gradually increased and then decreased.
normal load at room temperature. The scatter Examination of the contact surface sug-
is not excessive. The most important observa- gested that surface damage had occurred
tions are that the SASC has a substantially and that particulate debris was being push-
lower room temperature static coefficient of ed ahead of the contact interface, which
friction than does the RBSN, and the static could explain the steady increase in fric-
coefficient of friction does not vary signifi- tion. Once a sufficient amount of debris
cantly over the load range evaluated for the was'present, it could begin acting as a dry
point-contact condition. lubricant, which could explain the later
decrease in friction. Very little surface
Further information is available by com- damage was visible on the SASC stationary
paring the actual FT versus contact traverse specimen, but a roughening had occurred
distance curves for each material at each on the moving specimen. The accumula-
temperature. These curves for RBSN and tion of surface damage on the moving
SASC under 6.8 kg (15 pounds) point-contact specimen could account for the continuous
are shown in Figure 209 with coefficient of increase in friction.
friction values. These curves were reproduc-
ible from specimen to specimen; the following b) At elevated temperatures, the curves for
observationswere noted: both. materials had a discontinuity between
the static and dynamic friction, represent-
07 ative of a breakaway condition. The mech-
anism has not been fully identified, but is
, / i, / //,"///, "///,/.,",,0 suspected to be associated with sticking
06
due to surface oxidation. Contact surface
_ 9.0
0.3 // l lFl il ilt . . .
sAsc.
R,-/. o.8
0.2
-f ,' _ 4.5 0.4_ ,,
173
c) The dynamic coefficient of friction for but had little effect for elevated temper-
RBSN is lower at I093C (2000F) than at atures.
room temperature and is approximately
constant at 0.45 for normal loads of 4.5 to The point-contact tests at 11.36 kg (25
26 kg (I0 to 57.3 pounds). The dynamic pounds) are considered more severe than the
coefficient of friction for SASC increases static structure components will be exposed to
with traverse distance at 1093C (2000F) in the AGTI01 engine. Current estimates are
and room temperature to the 0.45 range. that the load will not exceed 1.6 kg (3.5
Friction also appears to increase with pounds) over a comparable point-contact area.
normal load at I093C (2000F). The purpose of the exaggerated contact loads
was to identify the mechanisms of contact
Most engine components are pre-oxidized damage and to determine the sensitivities of
prior to rig and engine testing. Figures 210 the candidate ceramic materials to surface
and 211 summarize contact data for pre- damage.
oxidized RBSN and SASC. The RBSN and
SASC were pre-oxidized for 2 hours at 1204C Additional tests were conducted at 11.36
(2200F). Pre-oxidation appeared to decrease kg (25 pounds) or less with line contact. Initial
the room temperature coefficient of friction tests suggest that the data scatter is larger
for line-contact than for point-contact. The
FRICTION
COEFFICIENTS high-temperature friction data are almost
I0 I0 F. LB F
_'d 0 34 033
ID ==_-o
140(]F, 25 LB F N
Pd 0.93-0.70 Ps 030
_ ! io ID ' F 'OFN
0
o
I0 `us 0.15
0 IDOI 0.02 003 0 04 0 IDOl O.ID2 0.03 004 ;'d 0 liD 018
174
of friction appears to be substantially lower After contact testing, each specimen was
for the line-contact condition for both materi- fractured in four-point bending. The strength
als. The line contact friction data for RBSN data are plotted in Figure 213 for point-and
and SASC for the ll.36-kg (25-pound) normal line-contact conditions. Obviously, the RBSN
load are shown in Figure 212. material has lower residual strength than
SASC, and the point-contact results in lower
line-contact conditions. Obviously, the RBSN
_ 90 RBSN. 1100C 0.8
material has lower residual strength than
llOOC SASC, and the point-contact results in lower
0.6
strength than line-contact. More specifically,
4.5 .,,...._ - SASC. RBSN. 1100C the RBSN exposed to point-contact biaxial
0.4 _'-
,, loading, has a residual strength of 121 MPa
v 0,2 __ (17.5 ksi). Strengths of RBSN prior to contact
w,.
z SASC. RT
typically ranges from 275 to 380 MPa (40 to 55
0 r I I
ksi). Strength degradation in the range of 60
Q 0.25 0.50 0.75 1.00
TRAVERSEOISTANCE. MM percent has occurred.
G87-078.107 B
99
90 /
/ EGEND
70
AVERAGE
/ MATERIAL CONTACT
CONTACT TEST
TEMPERATURE
4 POINT
MOR. MPA
_.. 50
RSSN {RBNI041 POINT 1100C 121
• RBSN IRON104) LINE I100C 186
IO
2
10 20 30 40 50 50 70 80
STRESS. KSI
GB7.078 1088
175
tact (and the resulting damage) only occurred contact loading, the contact apparatus data
at high points and varied from specimen to for RBSN and SASC were run through a con-
specimen. Specimens having a low residual tact stress analysis computer program devel-
strength typically had contact only along a oped under an ONR Program. The results for
small segment of the line. As the degree of room temperature and 1100C point- and line-
contact along the line increased, the residual conditions are summarized in Table 29. The
strength increased, suggesting that load distri- II00C results are plotted in Figure 214 and
bution and load sharing are important in mini- compared with baseline four-point flexural
mizing contact damage in RBSN. strength data for the line-contact configura-
tion.*
Figure 213 shows that SASC has higher
residual strength than RBSN. Specifically the The predicted stresses for the point-
average strength of SASC after point-biaxial contact condition considerably exceed the
contact is 258 MPa (37.4 ksi). The average baseline strengths of both RBSN and SASC and
strength prior to contact exposure for the would be expected to produce the degree of
configuration tested is approximately 450 MPa surface damage that would yield the severe
(65 ksi). The resulting strength degradation strength degradation measured. Peak stresses
for the SASC, therefore, is approximately 43 for line contact are substantiallyreduced, only
percent for point-contact and 4 percent for
line-contact.
*Specimen-oriented in the four-point test fix-
To estimate the actual tensile stresses ture with the flat surface in tension and the
applied at the ceramic surfaces during biaxial 0.63-cm radius surface in compression.
Table 29. Predicted Contact Tensile Stresses For Point- and Line-Contact Conditions.
]JS
static coefficient of friction
176
ap. KSI
induce spalling has not been quantitifed, how-
50 100 i50 200 250 300
ever a review of Garrett in-house data sug-
,_ RBSN BASELINE STRENGTH
8O gests that spalling of RBSN parts may occur if
35 SASC BASELINE STRENGTH
weight gains, which occur during the nitriding
I 70
3O I
process, are below 59 percent. A weight gain
I RBSN 6O below this figure indicates that a significant
I • LiNE • _ 0
25
z , I CGNTACT/sAscOBS"
! /.,., portion of Si has not been converted to Si3N 4
If /LINE POINT [ / _'n,_r
a
during the reaction process. In addition, high
2o green densities and thick cross sections inhibit
//CONTACT CONTACT// COI_'r_llr-T
Spalling typically has been attributed to 6.1.5 Laser Marking of Ceramic Materials
thermal stress generated within RBSN when
residuals of Si remain un-nitrided during pro- The effect of laser marking on the strength
cessing. The amount of free Si required to of five ceramic materials was investigated to
177
determine whether this technique would be marking of these materials without heat treat-
suitable for permanently marking AGT101 ing showed a reduction in strength and all
parts. Positive identification of engine hard- fractures originated at the laser marking.
ware for the AGT program is necessary to
keep component traceability. Samples of the ACC SN-501 SSN and Norton NC132 HPSN
five ceramic materials (RBSN, SASC, LAS, test specimens failed at the laser marking,
HPSN and SSN) were used to determine the both with and without heat treatment. But
laser parameters that would clearly mark the the flexure strength of the specimens was ade-
ceramic surface without visible damage. Only quate in allcases.
laser marking of the LAS materials was unac-
ceptable, due to visible damage of legibly In sum mary, laser marking parameters
marked materials. Subsequently, test bar have been established for marking four ce-
samples were marked with a series of XHs ramic materials frequently used on the
along the length of the test bars to simulate AGTI01 program. Properly processed laser
worst case marking orientations. One-half of marked materials show littleor no material
the test bars from each material were given strength loss as a result of laser marking.
the established heat treatment for healing
surface flaws. All test bars were flexure 6.1.6 Slip Casting Rheology Studies
tested at room temperature with the laser
marked surface in tension. Table 30 summar- Two subcontracts were initiated during the
izes the flexure strength data of laser marked summer of 1983 to study the rheology of Si
specimens. Standard oilSASC and ACC RBSN and Si3N4-Y203-A120 3 particulate dispersions
laser-marked and heat-treated materials in water. The program objectives are briefly
showed no reduction in strength due to the discussed in subsequent paragraphs and the
laser marking and did not fracture in the laser results are presented in detail in Appendices D
marked area, as long as the materials were and E to the ninth AGT semiannual progress
heat treated. The flexure strength after laser report.
Mean Mean
Strength Fracture Strength Fracture
MPa (ksi) Origin MPa (ksi) Origin
178
The Si slip program was subcontracted to - Particle size control by elutriation
Dr. M.D. Sacks of the University of Florida to
support reaction-bonded Si3N 4 processing at o Electrophonetic mobility for each powder
ACC. in aqueous suspension
• 179
minor surface erosion on the uncoated sample.
This erosion was judged a result of local
surface damage resulting from the machining
operation rather than the exposure conditions.
These preliminary results indicate that coated
or uncoated HTP may be suitable for use in
the current AGT101 engine configuration and
that the RCG coated HTP may be suitable for
use in higher gas velocity locations. Addi-
tional testing was directed toward evaluating
insulation capabilities under representative
turbine rotor discharge conditions, simulating
gas velocities and temperatures rather than at
the turbine diffuser dump location• Two test
conditions were selected representative of
engine maximum power [966C, 304.8 m/see
(1770F, I000 ft/sec)] and idle [1093C, 106.7
84636-1
GB7-078.110
m/see (2000F, 350 ft/sec)] flow conditions. To
perform these tests, additional RCG-coated
and uncoated test cylinders were obtained
Figure 215. RCG Coated and Machined HTP from Lockheed. The cylinders were 7.62 cm
Insulation From Lockheed. (3-inches) long with a 6.4 cm (2.75-inch) inner
diameter (needed to attain the higher gas
velocity conditions)• The new cylinders were a
THERMOCOUPLE (3l
higher density HTP-16 (16 Ib/ft3)than the
HTP-12 material previously tested•
_ _ SAMPLE CYLINOERS ./ OISCIIARGE
180
_, =. _ _i'i_ _Li _i
_:_
107 M/SEC 94 M/SEC
1093 1350 FT/SECI 1300 FT/SECI
| TEAROOWN| | |TEAROOWN |
I_ -INSPECTION- | INSPECTION |
I l I l II a l
I 2 3 4 5 6 7/
CYCLE
/
TEARDOWN
GII7,.078-112A INSPECTION
Figure 217. Maximum Power and Idle Condition of Lockheed HTP-16 Insulation.
181
OR!GIN._L PAGE IS
OF POO_ QUALLT_
6.2 Ceramic Turbine Rotor
182
OZ _(] 7,',] '"
OE POem qUALIT_
injection-molded rotor. Pure Carbon, in con- Through changing the slip theology (viscosity
junction with British Nuclear Fuels, Ltd and specific gravity) Ford was able to obtain a
(BNFL), fabricated rotors from reaction sin- more consistent density throughout the rotors,
tered SiC. eliminating the cracking problem. Further
improvements in simulated rotor quality were
Although advancements in rotor fabrica- obtained through controlled drying. These
tion were made by all suppliers, only minimal improvements could be seen in the successful
rotor deliveries were made early in the pro- spin testing of simulated rotors.
gram. Standard Oil produced a "spin quality"
SASC simulated rotor, i.e., free of x-ray 6.2.2 Bladed Rotor Fabrication
indications and significant visual defects.
Oarrett spin-tested the rotor, obtaining good Initial bladed rotor fabrication began in
correlation between analysis and material early 1982, with the suppliers demonstrating
properties. A room temperature burst speed limited success. As discussed in paragraph
of 72,400 rpm was achieved. Pure Carbon suc- 5.2.4, the blade cross section was redesigned
cessfully fabricated a simulated rotor from to improve fabricability (ref. Figure 136).
reaction sintered SiC. One simulated rotor, Nominal rotor thickness at the inducer blade
successfully formed, reacted, and inspected, tip was modified from 0.762 to 0.774 mm
was delivered for evaluation. Evaluation (0.030 to 0.040 inch). These changes reduce
indicated that the Pure Carbon Refel material the difficulty encountered in achieving com-
would require additional development for plete.blade fill. Late in the AGTI01 program,
AGTI01 rotor application; thus it was discon- another design iteration was made, shown
tinued from the program. pictorially in Figure 220. This change resulted
183
in both an improved bearing surface and investigated to clean both the powder and the
rotor/compressor attachment. Rotor/com- slip prior to casting but the problem was not
pressor attachment methods will be discussed solved. This experience emphasized the re-
later in section 6.2.4. quirement for a clean-room processing envi-
ronment. Incomplete blade fill also remained
The remainder of the AGT101 rotor effort a problem (Figure 221) despite centrifugal
focused on fabrication by ACC and Ford using spinning during" casting. While ACC was not
a slip cast Si3N 4 approach. Problems were able to solve blade breaking during densifica-
encountered in slip preparation, casting, and tion, it was attributed to non-uniform green
densification. density and/or furnace thermal gradient and/
or non-optimized sintering cycle. Despite
To consistently prepare a high quality slip this, ACC did achieve near theoretical densi-
for casting, the starting powder must be con- ties and produced rotors capable of passing
sistent with respect to purity and particle size 115,000 rpm spin testing. The high tempera-
distribution. While the powder may meet the ture properties of the materials developed by
powder supplier's specifications, there is ACC, however, did not meet AGT101 RPD
usually batch-to-batch variations for which temperature goals.
the user must compensate, normally through
additional powder processing. Powder impuri-
ties can degrade the material properties by
affecting grain boundary chemistry and/or in
the formation of strength reducing inclusions.
A controlled optimum particle size distribu-
tion is required to consistently achieve high
strength and minimize shrinkage and porosity.
To optimize strength, a powder that can be
densified quickly with minimal grain growth is
desired.
OR2G:NAL PAGE IS
184
_)_]_ P_O.OR QUALITY
blade cavities. Blade root cracking appeared observable interior defects confirm the rotor
to be improved by modifications in the wax hub integrity. This initialbladed rotor testing
removal technique. The hub cracking problem indicated the successful transfer of simulated
was improved by more careful removal of the rotor technology to the bladed rotor. Second,
plaster base. Internal cracks were determined the surface features responsible for the rotor
to be caused by density gradients, similar to failure were easily observable prior to spin
the problem encountered in simulated rotor testing. This fact implied that casting and
fabrication. This was corrected through use of sintering processes which produce good sur-
an organic suspending agent and greater con- face finish rotors will increase spin speed
trol of slip viscosity to eliminate slip settling capability. From these results,both Ford and
during casting. ACC were directed to apply fabrication pro-
cesses to improve visual appearance (surface
In addition, as Ford improved material high finish)to rotors being fabricated.
temperature properties, changes were made to The end.of 1982 saw three additional
the slip. One problem this caused was a low
bladed rotors from ACC judged suitable for
green strength and thus a greater risk of
cold spin testing to assess rotor development
handling damage. However, by adding a pre-
progress. All three rotors were slip cast at
sintering step to the densification process,
ACC and sintered by Ford under a Ford/ACC
handling strength was increased. This allowed
agreement. Table 31 gives the densities and
minor machining operations to be carried out
spin test speeds of the rotors. One rotor
on the rotor in the green state, precluding the
failed due to a surface flaw while the remain-
need for expensive, time-consuming diamond
ing two survived the spin test and were select-
grinding of the fully dense rotor.
ed for hot turbine rig testing.
ACC bladed rotor S/N 10191, east in
Table 31. ACC Bladed Rotor Test Results.
October 1981, was judged suitable for spin test
evaluation based on visual inspection, x-ray
radiography, and density evaluation, despite
S/N I Densi_
_m J
Speed, [
incomplete blade fill. Spin testing was per-
L
185
silicon nitride materials). The first rotor mance engine testing. The remaining ceramic
failed the 115,000 rpm spin proof test, burst- engine tests utilizing SN 250M rotors were
ing at a speed of 112,000 rpm. The second limited in speed and temperature in an
rotor was proof tested to 100,000 rpm, which attempt to avoid stress rupture failures due to
it successfully passed. The remaining two the lower material properties.
rotors were returned to NGK for further pro-
cessing. This processing included additional Ttie SN 250M rotor (S/N 256) which had
heat treatment to recrystallize the grain been used in the 85-hour, 1204C (2200F)
boundaries in an attempt to improve the high endurance test (engine S/N 004C, Build 6) was
temperature strength. Both were re-spin spin tested to burst, which occurred at 108,600
tested by NGK prior to shipment to Garrett. rpm. The rotor had been spin tested twice
One burst during the spin test, the second was prior to engine operation: once at Kyocera to
spin tested to 95,000 rpm. This rotor was 115,000 rpm before shaft bore machining, and
never used for engine testing due to the avail- again at Garrett to 105,000 rpm after the
ability of improved rotor materials. (Rotor shaft bore was machined.
material properties are discussed more fully in
paragraph 6. I). The failure mode of rotor S/N 256 (spin pit
tested) was similar to that of rotor S/N 259
Initial rotors received from Kyocera were from engine testing in S/N 002C, Build 18.
fabricated from SN 220M (sintered silicon These failures are compared in Figure 222. In
nitride). These wheels were proof spin tested both rotors, the hub centerline remained
to 110,000 rpm at Kyocera. This was lower
than the desired proof spin speed of 115,000
rpm due to concerns of the material strength
of SN 220M. In response, engine testing was
limited in speed and temperature when testing
the SN 22/)M wheels. Later rotors received
from Kyocera were fabricated from SN 250M,
also a sintered silicon nitride material. These
wheels were proof spin tested to 115,000 rpm
at Kyocera. The SN 250M material has a
higher room temperature strength than the SN
220M material and could thus be spin tested to
the higher speed.
vided as test specimens of the same material. Figure 222. Rotor S/N 256 Failed
These lower material properties in SN 250M During Spin Test in Mode Similm- to
rotors were deemed unacceptable for perfor- Previous Engine Failure.
186
intact and the fracture surface propagated with density. Burst occurred at 121,000 rpm
from the exducer hub zone to the rotor back- resulting in a maximum principal stress of
face. A close examination of rotor S/N 256 332.3 MPa (48.2 ksi). As shown in previous
revealed that the fracture originated near the Figure 223, this correlates favorably with pre-
interior surface of the shaft bore in the area vious high density rotor data. Ultrasonic
of some transverse grinding marks. The stress inspection of rotor S/N 688 revealed a large
concentration characteristic of the machining flaw, approximately one inch from the back-
marks could have caused the rotor to fail. face, rendering this rotor unsuitable for engine
testing. Due to the size of the flaw, expecta-
Rotor Density tions were that the rotor would burst in the
70,000 to 80,000 rpm range. The actual burst
Testing showed a definite correlation be- speed was 101,000 rpm, with a maximum
tween rotor density and burst speed (Figure principal stress of 235.8 MPa (34.2 ksi). The
223). Rotors with a density of 98.5 percent failure of rotor S/N 688 reinforced the reli-
ability of ultrasonic inspection in revealing
flaws and the need for additional data corre-
OENSITY AS AN INDICATOR OF STRENGTH
lating flaw size with burst speed and density
THE DATA SHOWS THAT A DENSITY
OF 98.5 PERCENTOF THEORETICAL1OR 3.22g/cm 3
to determine a maximum allowable flaw size.
iN THIS CASE)IS REQUIREDTO ACHIEVE 15 PERCENT
OVERSPEEOi115K rpm] OF AN AGTI01 ROTOR
6.2.3 Hot Turbine Rig
130-
187
A second ACC turbine rotor, cold spun to on silicon nitride shafts (Figure 224, View A).
115,000 rpm was tested in the hot turbine rig. Thermal cycling consisted of 15 minutes of
A cycle was defined to simulate a combustor soak at 538C (1000F). Coupling environment
flameout while operating at i00,000 rpm at temperatures were measured at the coupling
full load. Three cycles were accomplished on surface using a standard thermocouple. Since
the wheel. After teardown inspection showed a limited number of test specimens were
no evidence of any cracking, rubbing, or other available, the ceramic shaft was removed and
distress on the turbine wheel. As a result of then reinserted into the sleeve at different
this testing, the wheel could be used in a 871C circumferential orientation to avoid single-
(1600F) metal engine without speed restric- assembly effects during testing.
tions.
INITIAL SLEEVESWERE STRAIGHT /BRAZEO JOINT
WALLED WITH DIFFERENT INNER
As confidence was gained in rotor hub
_. IWALL THICKNESSES
integrity and material properties, it was
determined that the hot turbine rig was no
longer necessary. Rotors could be successfully
screened for engine testing through visual in-
spection, density determination and cold spin
pit testing.
4.5 to 5.0 in/F x 10 -6 coefficient of expan- Figure 224. IN907 Ceramic Test Sleeves.
sion).
Initial thermal cyclic testing showed that
Preliminary assembly tests confirmed that thermal "ratcheting" and consequent varia-
diametral interferences between 0.11 and 0.12 tions in length of the coupling assembly were
mm (0.0045 and 0.005 inch) could be made concerns of the sleeve design. Based on these
without subjecting the IN-907 to temperatures results, a coupling was designed, as shown in
in the recrystallization range and further, no Figure 224, View B, to include a straight inner
apparent damage to the ceramic shaft was wall and a contoured open end. Testing was
observed. Therefore, a series of thermal resumed. The -I version, 3.53 mm (0.139 inch)
cycling tests were conducted to determine wall thickness and 22.5 mm (0.886 inch) diam-
dimensional stability after assembly. IN-907 eter ceramic shaft, showed essentially no
sleeves of two different thicknesses, 1.9 and racheting after 350 thermal cycles. The -2
3.0 mm (0.075 and 0.120 inch), were assembled design, 1.9 mm (0.075 inch) wall thickness and
188
25.8 mm (1.015 inch) diameter shaft racheted VACUUM HOLGING
•
L
CLOSECONTROLOF COUPLING TEMPERATUREDURING iNSTALLATION
I
INITIAL ATTACHMENT METHOD INVOLVEO • OXIDATION OF COUPLING (INCONEL 907 -- NO CHROME)
SOLID STUB SHAFT ROTOR • RAOIAL POSITIONING OF COUPLINGRELATIVE TO SHAFT
• BLIND ASSEMBLY
GB7@7647A
u -'TURBINE i
cation to the coupling. Electroless nickel was
plated onto the couplings, eliminating the
GII7_78-48A oxidation problem. This in turn eliminated the
positioning problems through removal of the
vacuum chamber requirement. A new attach-
Figure 225. Initial Attachment Method
ment tool (Figure 227) eliminated the radial
Involved Solid Stub Shaft Rotor.
and axial positioning difficulties.
189
6.2.5 Cold Spin Testing
! Discussion of cold spin testing is incorpor-
ated into the discussion of bladed rotor fabri-
cation and test activities,paragraph 6.2.2.
GB7-07848 A
A Zeiss series 500 coordinate measuring
Figure 227. Installation Difficulties machine was used to inspect blade surfaces
Solved with New Method. (both pressure and suction sides). Side screen
inspection was used to define the blade outline
in the axial-radial plane. An SN 220M rotor
FINAL ATTACHMENT METHO0 INVOLVED
HOLLOWSHAFT ROTOR (S/N-0005-6), and an SN 250M rotor (S/N 254)
were inspected.
190
A B
S|;.Olfl.t
Figure 229. Typical 3-D Views of the Finite Element Blade Vibration Model.
side, so that the blade cross section is no elements after the problem with skewed ele-
longer radial. This SN 250M exducer discrep- ments was identified.
ancy is apparently caused when exducers droop
The Campbell diagram, shown in Figure
under their own weight during densification.
232, was generated for the SN 250M rotor
The SN 220M rotor did not exhibit this droop.
blade at 1371C (2500F) T 4 and i00,000 rpm.
Inducers of the two rotors appeared very simi-
lar. Operating temperatures and stresses were
included to account for thermal softening and
centrifugal stiffening. Rotor temperatures
Turbine blade inspection data were used to
generate a 3-D finite element blade model. used for the 1371C (2500F) T 4 case are the
same temperatures used in the complete rotor
First, a 2-D blade grid was created from side
stress analysis and are discussed in paragraph
screen inspection data. Then, using a least
6.2.7.2 Rotor Stress Analysis.
squares fit, 3-D polynomial surfaces for the
pressure side and suction side were generated Garrett analysis programs ISOVIB and
from Zeiss inspection data. The 2-D grid was EIGEN were used to set up and solve the eigen
projected onto the pressure and suction side problem for each of the seven analysis models
surfaces to create a 3-D FEM. listed in Table 32. Solutions consisted of
natural frequencies predicted for the first
Finite element models of the SN 220M three modes for the seven models, in Table 32.
rotor blade, SN 250M rotor blade, and nominal
blade were generated with skewed exducer 6.2.6.2 Blade Vibration Testing
elements. Another SN 250M and nominal Rotor vibration tests were performed to
blade model were constructed with normal measure natural frequencies, verify mode
191
SN220M SN250M
ROTOR ROTOR
Z = 2.54 mm = 2.54 mm
I0.10 IN) (0.10 INi
.5.1mm -5.1 mm
I-0.20 IN] I-0.20 Inl
x x
40,§ nlm
40.6 mm
11.60 INI it,60 iN)
Y AXIS ram, (INCHES) Y AXIS ram, )iNCHESI
|IT_P+tA
192
-22.9 mm
-22.9 man
(-0.gQ IN)
{-0.90 INi I
SN250M
ROTOR
\\ '\ z : 368,n,, Z = 3.68 mm
11.45 INI
+
x
has very little blade-to-blade variation in fre- cited with a piezoelectric transducer glued to
quencies. Rotors from the same supplier fab- the blades. Holography results are compared
ricated from the same material and by the to predicted mode shapes in Figures 234, 235,
same process also have very little rotor-to- and 236. The close match between predicted
rotor variations in frequencies, as illustrated and observed mode shapes provided increased
by Figure 233. confidence in the accuracy of the finite ele-
ment model.
Data collected from acoustic ring tests are
given in Table 33. These data indicate that
Bullen Test
rotors of the same material had nearly the
same blade natural frequencies. However, SN
250M blades and SN 220M blades had signi- A test plan was developed to address con-
ficantly different natural frequencies. Since cerns about blade vibration in engines. Two
these materials have nearly identical densities different tests were conducted: a magneto-
the difference in natural frequencies was restrictive shaker (Bullen machine) test (to
attributed to geometry differences associated determine strain-to-failure), and a (cold) en-
with the different shrink factors of the two gine motoring test (to assess strain during
materials in densification. engine operation).
193
O PREDICTED
19/REV
ISTATOR
COUNTi
..t
5/REV
4/REV
/REV
T I"
2O 40 80 8O 1DO
a1_711..4
Figure 232. Campbell Diagram for SN 250M Rotors Showing 19/Rev Stator Excitation Line.
194
I"1--
21
2-2 ¸
3-4-
_E
4.s-
_., 5-6-
CONSISTENCY OF 8LAOE FREQUENCYRESPONSE
250-
ii°
ALTHOUGH BLAOE FREQUENCYRESPONSE OF THE
I003- ROTORS FROM ONE SUPPLIER )PLOTTED AT THE
TOP OF THE CHART) OIFFERS FROM THE 8LADE
x FREQUENCYRESPONSEOF A SECOND SUPPLIER
1002-
{80TTOMJ. THE CONSISTENCY DEMONSTRATES
=. UNIFORM MASS 81STRIBUTION ANO GOOO
1001- OIMENSIQNAL CONTROL8Y OOTH SUPPLIERS
I I I I I I% i I I I ! I
14 16 18 2o 28 zs 3o 31 3,
FREQUENCY,Hz x 1000
G87-078-29]
195
0P_GD!AE PAGE I8
OF POOR QUALITY
PREDICTEDSN 220M
PREDICTEDSN 220M BLADEOISPLACEMENT
BLADEDISPLACEMENT
Hz = 23,079
HZ = 16,941
PREDICTEOSN 250M
BLADEDISPLACEMENT
PREOICTEDSN 250M
BLAOE DISPLACEMENT Hz = 20,581
Rz = 14,000
HOLOGRAPHY
OF AN SN 250M ROTOR8LADE HOLOGRAPHY
OF AN SN 250M ROTOR8LADE
G87.078-5 G67_078-8
196
ORIGI_L_.L PAGZ ?_
OE POOl{ QUAI_IY
VIBRATION
lo,,,c,,o
HOLOGRAPHY OF AN SN 250 ROTOR BLAOE
G87_7_7
GB7_7_276
Figure 236. Comparison of Holography
Results with Predicted Second Exducer Figure 237. Initial Rotor Orientation
Mode. Excited Exducer Tips (Bullen Test).
197
MPa (PSIAI
20.7, 3
MECHANICAL _'_ /
STATOR WAKE
AT SOKRPM
pNOUCERRESONANCE)
STATOR WAKE
A AT4OKRPM
(EXOUCERRESONANCE)
0.9- 1--
DIRECTION
VIBRATION
OF
/ ' / 50 KRPM
-.--'-' 40 KRPM
O- oJ |
d a
, !
j
_.02 0.00 0.62 {INCH
•'.5 o5 M.
007-070-279 CIRCUMFERENTIALSPACING
607.076-200
Figure 238. Rotor Re-oriented to Excite Figure 239. Cold Motoring Test
Inducer Tips (Bullen Test). Analysis Results.
gaged and installed in a metallic-structured The resulting predicted blade stresses are
engine (S/N-001, Build 40). The engine was shown in Table 34. This indicates a low hot
then motored with ambient temperature air operational cumulative stress which combines
through the blade resonant speeds. The blade the vibratory peak-to-peak stress to the
vibration amplitudes were recorded. centrifugal and thermal stresses in the blade.
A turbine stator wake analysis was perfor- At around 43,000 rpm the exducer reso-
med to establish the pressure profile at the nates at its first natural frequency with a
stator discharge for the cold test case and a peak-to-peak vibratory stress of 33.1 MPa (4.8
similar profile for the predicted hot operating ks]). During operation this stress is super-
conditions. On the assumption that the blade imposed on a steady state stress of 13.1 MPa
response is proportional to the pressure wake, (1.9 ksi). In comparison with the 620.5 MPa
the blade resonant amplitudes measured in the (90 ksi) stress, calculated from the measured
engine motoring test were corrected to pre- 2280 micro inches/inch strain, that caused
dicted engine conditions. Result from the failure in the Bullen test, fracture is highly
wake analysisare illustratedin Figure 239. unlikely.
198
At about 53,000 rpm the inducer resonates Blade and hub geometries measured from
at its first natural frequency with a peak to the SN 250M rotor, S/N 254, were used to
peak vibratory stress of 101 MPa (14.6 ksi). develop both models. The models thus in-
This is superimposed on a steady state stress cluded the exducer blade "droop" anomaly
of 79.2 MPa (11.5 ksi). Again vibratory failure shown by the "Z-section" measurements
is not expected at this stress level. (reference paragraph 6.2.6, Figure 23 i).
Because this anomaly introduces non-radial
Analysis indicates that the cold condition blade elements, bending stresses are present
is much more severe than the hot operating at speed which would not be present in a rotor
condition with larger driving forces; however, made to blueprint.
this condition can be avoided in engine testing
Thermal boundary conditions for partial
by limiting the speed of the engine without a
flame in the combustor. power and maximum power conditions were
determined from analyses and engine test re-
sults. Analyses were done for maximum
6.2.7 Rotor Stress Analysis
power, steady-state conditions then corrected
according to rotational speed, turbine inlet
AGT101 rotor stresses were predicted for
temperature, compressor discharge temper-
partial power 70,000 rpm and 1204C (2200F)
ature, and mass flow for partial power condi-
T 4, maximum power 100,000 rpm and 1371C
tions. The maximum and partial power ther-
(2500F) T 4, and 115,000 rpm proof test condi-
tions. mal distributions are shown in Figure 241 and
Figure 242 respectively.
An initial model without a fillet between Stresses predicted with these models are a
function of applied rotational speeds and ther-
the hub and blade was developed to help guide
mal boundary conditions. Blade pressure loads
engine test plans specifically for the proposed
were assumed minimal and were not evaluat-
100-hour endurance test. A later model with a
ed.
fillet was developed to generate a more com-
plete stress solution for failure risk assess- Stresses from the first model were deter-
ment as discussed in the following paragraph mined using the Garrett finite element pro-
6.2.8. These models are shown in Figure 240. gram IS03DQ. The principal stress distribution
a,.
GS/-07Ot
199
410C (770F)
471C [880F}
/ 532C (990F)
593C (1100F)
1181C12158F}MAX
649C {1200F)
710C (1310F)
771C 11420F)
TEMPERATURES
IN 827C (1520F)
C IF)
888C (1630F]
949C (1740F]
IOO4C(1840F)
1066C11950F)
[_ 1127C12060F)
710C
1182C12160F)
{1310FI
/ 471C
(880FJ
827C
I 127C{2060F]
GB7-O78-9A
for the room temperature 115,000 rpm proof (paragraph 6.2.7). Life predictions were made
test, maximum power operating condition, and by integrating the risk of fast fracture and
for partial power conditions are shown in Fig- time dependent failure (slow crack growth)
ures 243 and 244. over the area and volume of the AGT101
rotor. These results have helped define the
Stress analysis showed the largest maxi- capabilities of current ceramic probabilistie
mum principal stress location occurred in the methods and have laid the ground work for
blade exducer, where the off-desig n geometry future verification efforts. These results also
induces bending stress. provide an assessment of current ceramic
materials capabilities and their suitability for
6.2.8 Rotor Life Prediction heat engine applications.
200
432C (810F)
485C 1905F)
B 538C IIO00F)
1117C (2043F) MAX
591C (1095F)
643C (1190F)
B 696C (1285F)
907C (1665F)
960C (i 760F)
1013C(1855F)
696C
591C 1066C11950F)
11095F]
/ 1118C(2045F)
\
1013C 802C
(1855F) (1475F) 485C
1066C 1905FI
11950F)
GB7_7_IOA
gorized as surface or internal. Details about the curves in Figure 245 based on a hypo-
test procedures are given in paragraph 6.1. thetical surface characteristic strength and
Weibull modulus of 621 MPa (90 ksi) and 20
Independent surface and volume strength respectively, and a volume characteristic
properties were required to predict the com- strength and Weibull modulus of 689 MPa (I00
bined probability of surface and internal ksi) and 10. These material properties were
initiated rotor failure. The probability of used to generate independent surface and
survival when these failure modes are concur- internal failure occurrence curves A and B.
rent is the product of the probabilities of When both failure modes occur in the same
survival of each failure mode. population, curve C is observed. The apparent
surface and volume curves D and E were
Independent surface and volume Weibull generated by separately plotting surface and
characteristic strength and modulus cannot be internal failure data used to plot curve C. The
simply determined from test data that con- reason for different independent and apparent
tains both modes of failure. The interdepend- failure distributions can be explained by
ence of combined failure modes tends to mask examining the volume failure distributions. At
their underlying independent failure distribu- 724 MPa (105 ksi), 20 percent of the popula-
tions. This is demonstrated in Figure 245. tion would survive volume failures. When both
Monte Carlo methods were used to generate surface and volume failures are present the
201
MAXIMUM PRINCIPAL
STRESS. MPa IKSli
MAXIMUM BLADE
STRESS = 398 MPa (57.7 KSI)
TEMP = 21C [7OF)
\
MAXIMUM HUB
STRESS 301 MPa (43.6 KSII
GBT-OTO-11k TEMP : 21C 17OF)
Figure 243. Principal Stresses for Room Temperature 115,000 RPM Proof Test
Predicted From No-Fillet Model
entire population fails by 689 MPa (100 ksi). Slow crack growth and fast fracture ma-
Therefore, the apparent volume failure dis- terial properties were determined from speci-
tribution is truncated to zero at 689 MPa (100 mens tested under uniaxial stress conditions.
ksi) which is significantly different than the Batdorf's multiaxial fracture criteria was used
independent volume failure distribution. to predict risk of failure in the AGT101 rotor,
Curves D and E demonstrate the distributions which has largely biaxial stresses. The ratio
of data that would be observed from testing of multiaxial risk to uniaxial risk with respect
this material with both failure modes present. to increasing biaxial stress ratio is plotted in
Data for the curves A and B, however, are Figure 246.
needed to determine the independent surface
and volume Weibull strength properties for A multiaxial correction factor, rex, was
risk analysis. selected from these curves according to the
principal stresses at the location being evalu-
Determination of independent surface and ated with the Weibull modulus of the material.
volume strength distributions was accom-
plished through data censoring. Surface and At elevated temperatures the risk of frac-
volume Weibull strength parameters for SN ture increases with time due to slow crack
250M, determined with censoring, are given in growth. Slow crack growth causes cracks to
Table 34. propagate from existing flaws according to the
202
MAXIMUM PRINCIPAL
STRESS. MPz {KSll
MAXIMUM BLADE
STRESS = 290 MPa [42.0 KSI}
TEMP = 1263C (1823FI
\
iSOPLETHS : 5 KSI [35 MPal
MAXIMUM HUB
STRESS = 219 MPa 131.8 KSII
667-07D-12 A TEMP = 1098C (2008F]
Figure 244. Principal Stresses for Maximum Power, Predicted From No-Fillet Model.
slow crack growth power function. The crack TIT, and maximum power I00,000 rpm and
growth rate power function was combined with 1371C (2500F) TIT, are given in Table 35.
the equation for the critical stress intensity to
derive the time to failure equation. The risk of failure in each of the rotor
regions and over the total rotor vo]ume and
The time to failure relationship was com- area for the partial power condition are shown
bined with the Weibull fast fracture equation in Figure 247. SN 250M (as-fabricated) speci-
to calculate the risk of fast fracture at any men slow crack growth data were used for
IzT_e. these analyses. At part power, the hub does
not have the highest stress in the rotor but it
The risk of AGT101 rotor failure was eval- does have significantly higher initial failure
uated with a Garrett developed program that risk than the other regions. This is due to the
performs Gaussian integration of risk over high relative volume and biaxial nature of the
each element from a finite element stress stress. Only the hub exhibits higher internal
solution. The product of all element survival failure risk than surface failure risk, high
probabilities was calculated to determine the enough to initially give the entire rotor a
total survival probability. greater internal failure risk. Later in the
rotor life, surface failure risk exceeds internal
The predicted risk of fast fracture for failure risk, due to the higher temperature at
partial power 70,000 rpm and 1204C (2200F) the rotor surface.
203
k. B = INDEPENDENTSURFACE AND VOLUME FAILURE
OCCURRENCECURVES
G87,078-t
7A STRESS, MPa
slow crack growth data. These results are 0.2 0.4 0.6 0.8 1.0
204
........... 7 ,`¸ /" _'_i _
::i:
"o 'TOTAL
I
.m
' I I_iIl l i ! i i ; I
;i; i I t....rSHAFT RSK/ ! I , ! !:
TIME. HOURS
GD7@7_20
Figure 247. Rotor Failure Probability for Partial Power Operating Conditions.
*o
II [ III
I ] IIIll ]_ _ J_ _ : J ,<
[
]I.' _, i !IIli',_
TOTA<R'"\I II
-_ ----\
HSK zI ,tlil
:][ _._ -'l _l.!/
$ ib , ;-._., 8LAOERISK,
, i I,_ ' _
--Iz-_ l Ili .-'T z ' :
.... i ..... ?tFF_ I I L:,,,,'!i' I i ; ii_ii_
..a _.
/ I11111 I iTI]'i'ir., I I i_j':lij
E
F=o /. I "_FILLET RISK : i "
'O
(
.....itttt i-I
-
TIME HOURS
ira74711-,z2
Figure 248. Rotor Failure Probability for Maximum Power Operating Condition.
advanced materials are measured, the findings material as fabricated in the rotor, is an
presented here give reason for caution. The indication of the importance of verifying
severe reduction in predicted rotor life, as a properties of components, rather than relying
result of the decreased properties of the exclusively on test bar data.
205
ioo
10-1
10-2
10-3
..I s
_ 10"4
,,_ 10-4 10-3 10-2 10-1 100 I03
._" 100
0
O_
0,,,
111-1 HUB
111-2
10"41-..
10-5,
t_ 10-3 10-2 10-1 100 10i 102 103
TIME, HOURS
687-078-24
Figure 249. Rotor Failure Probability for Partial Power Conditions Based
on Properties of SN 250M Rotors.
FLOW
SEPARATOR
HOUSIN|
REGENERATOR
SHIELD
TURBINE
ROTOR
TOAHSITIOH
OUCT ]ii!:]]!i]i
&117,478-79
207
At the beginning of this program, correla- trol. Design and fabrication of state-of-the-
tion between probabilistic prediction methods art structural ceramic components of the size
(especially for polyaxial stress distributions) and shape required for the AGT101 had not
and the limited test data had not been estab- heretofore been attempted. Therefore, the
lished. As a result, the realistic design cri- design of simple component configurations
teria had to be established by testing--initial- with uniform wall thicknesses were pursued.
ly by extensive tests in engine simulated me- Whenever a deviation from a uniform wall
chanical and thermal screening rigs, and final- thickness was required, a gradual contour
ly, in actual engine conditions. change was used to minimize the stress con-
centration effects. The large thermal expan-
The overall design/development philosophy, sion differences between ceramic and metallic
therefore, has been to define problem areas structures dictated the use of unique and inno-
and initiate design changes based on feedback vative piloting systems. To accurately predict
from component testing. Continuous feedback component stresses for this program, exten-
has been made to the analytical process and sive engine instrumentation and data reduction
material selection throughout all stages of rig were necessary to develop the proper analyti-
and engine testing to arrive at a viable and cal thermal boundary conditions. By creating
optimized component design. a high degree of analytical confidence, a se-
lection criteria was established for various
6.3.1 Component Design/Analysis component configuration/material options.
For example, a component design utilizing
6.3.1.1 Introduction varying wall thickness to reduce excessive
thermal gradients during transient thermal
Development of AGTI01 ceramic compo- conditions could only be accomplished by ac-
nents was initiated during the engine configu- curately knowing the flow path heat transfer
ration conceptual design study phase. Twenty- coefficients (HTCs). Likewise, only by instru-
three different engine concepts were review- menting the various rigs and components could
ed. confidence be placed in the fact that these
rigs were properly simulating engine condi-
Based on experience in earlier ceramic tions and proof testing the ceramic compo-
programs, component symmetry, both in ge- nents to a predetermined stress level.
ometry and loading, was pursued in the basic
design strategy to eliminate circumferential A wide variety of available ceram'ic mate-
stress variations and to reduce the complexity rials was considered in this program. To
of the finite element analysis. This simplifi- eliminate extensive design optimization on
cation resulted in reduced cost, both in man- each material/component combination, a pre-
power and computer demands, and rapid anal- liminary evaluation was performed for each
ysis turnaround that allowed for extensive component to identify primary and alternate
design iterations. The engine symmetry also materials. Subsequently, design optimization
provided the capability to fabricate and rig- was performed using a prime material candi-
test components early in the program, thereby date for each component. After design opti-
allowing test data feedback into the design mization was achieved, alternate candidate
program. The flow separator housing is the materials again were evaluated, at which time
only exception to the concept of symmetry. all acceptable material/component combina-
This component will be discussed in detail in tions were assessed.
the component design section.
Because of the lack of ductility in ceram-
Individual component geometries were de- ics, localized stress concentrations cannot
fined to minimize stresses and to provide ease plastically redistribute stresses. Consequent-
of component fabrication and engine assembly ly, conducting detailed finite element model-
while maintaining the required piloting con- ing and eliminating known stress concentra-
208
tions from the design wherever possible be- M = 5.4 KG/MIN 112 LB/MIN) M = 8.8 KG/MIN I}917 LB/MIN]
comes of paramount importance. Whencom- C (FI
additional analyses using a finer substructure I000 : 4.3 KG/MiN 19.6 LR/MIN
model meshwere performed.
Stresseswere analyzed for three modesof
loading enountered during the normal engine 20O
M = 3,8 KG/MIN (5.5 LB/MIN]
0 2 4 8 O I0 29 30 4O 5O 6O 70 SO O0 tO0
two thermal (steady-state operation and light-
IIi/-0711-_ WORST CASE COLO START. SECONOS
off transient)• Shutdown transient conditions
were initially considered but were insignifi-
cant due to the thermal inertia effects of the Figure 251. Worst Case Light-Off
Cycle (1282C).
regenerator core.
209
1371
(25ool
1
1093.{
12oo01
I
871C (1600F)
) _
260 .._ = 0.076 KG/SEC
(5o01
] (0.167 LBM/SEC}
- 93C 12OOF)
! | ! I | l I I I
12.4 MPa (1.6 KSI] 391.5 MPa {56.8 KSI) 965 MPi ll4.O KSI{ 181.3 MPa (25,3 KSII
• FLAT • FLAT
• NO DIFFUSER DUMP SECTION • NO OIFFUSER DUMP
• SCALLOPED BOLT SLOTS • NO BOLT HOLES
UNSCALLOPED SCALLOPED • REDUCED O.O.
GB7_71-59
The stress analysis results for the initial Figure 254. Outer Diffuser BI and B2
inner diffuser is shown in Figure 255. To Configurations.
simulate 3-D effects on this 2-D model, the
outer section of the inner diffuser was The stress analysis results for the scalloped
modeled as a thick rim and parametrically inner diffuser was done for both the maximum
plotted with principal stresses at three loca- and minimum tolerances on the pilot slot. As
tions. The results show that the effect of the shown in Figure 256 the singular effect of the
increased rim thickness is to reduce stresses tolerance within the pilot slot radius ac-
at the pilot hole. counted for approximately a I0 percent varia-
210
8 HOLE OUTER RADIUS HOLE INNER 8AOIUS 7 ¸
100.6 MPz
6 114.6 KSII
5.
4.
3'
2'
__ M,N,MUM
HOLE
OUTER EDGE
_ RADIUS USED ,
I.
_,._ , - _ , _ ......2 4 6
{7.9 KSII TENSILE
MINIMUM HOLE RAOIUS USED O"
MPz (KSII
T
137.8. 20- ._OUTER RAOIUS
7
16-
_ 110.3-
12-
_J_ _ g,.oM_,
_. 82.7"
2.76"
8-
4
R EDGE =:
o ,
0.4 ,
0.8 ,
1.2 ,
1.6 :
2 0 2 :,, 2:s 3:2
RIM THICKNESS. INCH
'
25 '
5O 7'5
RIM THICKNESS, MM {7.9 KSII TENSILE
GO7-O78-53A
tion, the higher stress being predicted for the Figure 256. Inner Diffuser Scalloped
larger radius. The higher stress for the larger Configuration Stress Analysis Results.
radius initially appeared contrary to the com-
mon rules of thumb concerning stress concen- final outer diffuser design. The component
trations. This apparent contradiction was was truncated to inside of the pilot bolts to
rationalized by realizing that the smaller fillet form a completely axisymmetric design. Pi-
radius between the sides and the bottom of the loting is maintained by frictional loading from
slots produced a flat at the bottom, where the an axially spring loaded mechanism. A 60-
peak stress occurred. The larger radius pro- percent reduction in maximum principal stress
duces a full radius at the bottom of the slots. has been estimated by the total culmulative
Compared to the initial configuration, the design changes on the inner diffuser.
scalloped configuration was estimated to offer
a 34-percent improvement. The truncated inner diffuser required the
design and fabrication of an additional com-
The design finally chosen for the inner ponent to provide the outer flow path between
diffuser to meet the program goal had a the outer diffuser to the flow separator
configuration similar to that chosen for the housing. The I093C (2000F) gas temperature,
211
lack of mechanical loading, and the low peak 257 consisted of the shroud, outer diffusers,
gas velocity of 15.2 to 22.9 m/sec (50 to 75 the seal area, and portions of the transition
ft/sec) allowed materials other than mono- duct, stators, and flow separator housing.
lithic ceramic components to form this gas Heat transfer coefficients on the turbine
path surface. Babcock arld Wilcox, Inc., shroud and the outer diffuser were modeled to
vacuum formed A120 3 fiber insulation,coated reflect the absence of the turbine rotor.
with Johns-Manville Cerakote at the surfaces
exposed to the hot turbine exhaust gases, was
TURBINE SHROUD TURBINE
selected for this component and is currently SHROUD
FLOW SEPARATOR
6.3.1.3 Turbine Shroud
S HOUSING
The turbine shroud design (Figure 250) was
the most substantial design challenge of all
the ceramic static structural components.
Functionally, this component must maintain
the outer turbine flow path as energy is con-
verted into power through the turbine rotor.
212
r--
The following results were found from this
SCALLOPED
investigation:
TYPE B1 TYPE B2
Type B3 configuration.
UNIFORM
WALL The next area to be considered was the
THICHNESS
effect of various light-off and operating cy-
TYPE 63 TYPE 84 cles on the shroud stresses in the static struc-
UT,,OTI,,54 ture rig. Six different cycles were considered.
Three of these cycles were light-off cycles to
I149C (2100F), all at idle mass flow conditions
but at different transient rates as shown in
Figure 258. Phase B Turbine Shroud Figure 259. In addition, three other operating
Configurations. cycles were considered, as shown in Figure
260. These included a light-off to steady-
state conditions (cycle 2), a light-off followed
off transient to 871C (1600F) as shown in
by a shutdown after a 1-minute hold at
Figure 252. The comparisons were made
maximum temperature (cycle 3), and a
assuming RBSN as the primary shroud mate-
shutdown from steady-state conditions (cycle
rial. The heat transfer coefficients were
6). Again mass flow was at idle condition
based upon aerodynamic analyses.
during the cycle until the rig was shutdown,
then mass flow was reduced 50 percent.
The Type B1 thru B4 configurations had a
scalloped flange whereas the baseline config- Table 37 shows the results for the effect of
uraton (Type A) did not. In addition, all Type cycle variations. Both the turbine shroud and
B configurations attempted to increase the outer diffuser were assumed to be RBSN. The
structural flexibility to relieve the thermal heat transfer coefficients were based on a
growth mismatch between the outer and inner first set of thermocouple data from a metal
sections of the turbine shroud during transient engine test.
light-off conditions. The Type B4 was a two-
piece configuration with the interface at the The screening rig cycle was selected after
stator support. this study to include a long hold period
213
Table 36. Phase B Shroud Configuration Study.
Time
After
Case Magnitude Start,
NO. Type Material Location* MPa (ksi) sec
IF X 402i
25
40-
15
4-
2-
214
C X 102 IF x IO 2)
]4 25
20-
I0-
8- 15-
f4 = CONDITION B
6-
10-
4-
5-
2- S/D
_ 93c 1200Fi
O- 0
I I ! I I I I
0 80 | 60 240 320 400 480 560 640
687..076-50
(6 minutes) to ensure that the maximum prin- the absence of flow around the shroud flange
cipal stress was realized during lightoff. In and cone. The screening rig also had been
addition, the cycle ensured that the cool-down used to screen turbine shrouds initially without
was less severe than the lightoff. The poten- the use of stators and a backshroud. After
tial for high cool-down stresses occur only in passing this initial test, the stator assembly
the rigs since the regenerator system on the and backshroud were added to the assembly
engine negates the possibility of significant and the turbine shroud was retested. Conse-
cool-down rates. quently, the initial turbine shroud screening
rig test did not include the stator exit swirl
6.3.1.3.2 Shroud Screeninff Rift Analyses flow effect encountered in the latter test.
215
0 0 _ 0 0 0
• , . w
v
v v v v v
• _ _ _ _
0
J
_3
A
A A A _
c/3
v v V v
0
o_
111
0 _
w
III
A
el
V
? ? ? ? o 0
o
0 .__
E_
o
216 tl.
•--4--_ m
217
Table 38. Turbine Shroud Seal Radius Study.
C X 102 IF X 1021
14=
4 MIN
12- 1149C 1210OF)_
I0-
6 MIN -- 871C
18OOFI
0-
649C
1120OF)--
4 g
¢1C 1200FI
0 I
1 1 I 1 1
4 6 8 I0 12 14 16
GOT-070-61
218
The significance of the last item was that
the maximum stresses could be controlled to
occur during the initial light-off where the
environment is more fully characterized and
the remainder of the cycle would function at a
lower stress level. The first ceramic engine
light-off (engine 002C/Build i) had a similar
cycle to cycle ii except stresses were con-
trolled to a 25-percent lower stress level by
decreasing the initiallight-off step and ramp
rate.
219
E-_ m
+°°°
,i,,q
L.
,eu
e-I
o_
_u
E-
"_o
L, ,_J;
m_ 0 0'_
°+1i_ _a
0
m._ _e_ _
220
r13
'0
r;3
.o
m
U3 0
m
r_
E-
E_
0 0 0
! I I '_ .._
_gg
f.
o
_.o
,It
221
1371 _
12_oo)] 222_F
_ ,ogaJ/
" 65,000 RP
=_ 8z6.,J /
,,500, ,,ooo,!/
538.
/
/'.
i
_ (1000) __ / M(0:205125
LBM/SEC)
KG/SEC M = 0.095 KG/SEC
260 / (0.210 LBM/SEC)
II
(OJ0 10
I 15
I 20
| 25
I 30
! 35
!
4O
TIME AFTER LIGHTOFF, SECONDS
GB7-078-390
14 25
3 MIN
12
20-
10-
-_ 6- 15-
z.--
8- 10 MIN
M'J
5-
52C 1125F)
O
0 I I I ] ! I !
0 10 20 30 40 50 60 70 8O
TIME AFTERLIGHT-OFF.
MINUTES
6DT_T&70
222
reduced maximum principal stresses by 63
Q TURBINE SHROUD TURBINE
SHROUD percent (without radiation effects from the
/_ OUTER DIFFUSER shroud to the rig insulation considered).
FLOW SEPARATOR
o The type C3 configuration shroud had the
HOUSING lowest predicted maximum principal
stresses of all configurations considered
(29 percent reduction).
MPa (KSII
I0-
I i I I I I i
B
= LOCATION A (NOOE 1601 = "1 = LOCATION 0 INOOE 403]
40- 'Ill
_1_:35.1 MPa 15.1 KSll
,,,j:
20-
I
J%
/
O--
0 10 20 30 40 50 60 70 80
6D7_7i1-72
Figure 267. Turbine Shroud Stress Response for Ramp Type Cycle (Engine Cycle 11).
223
D]_ _.'00[{QUALITY
UNITS FOR HTC = WATTS/M2C [BTU/HR-FT2-F}
T4 = 671C IIGQOFI
l_l
131 (23l
17 (5]
17 (31
125 1221
toe(35i 125
199 [35i
148
227
358
482
392
551 i971
267 1471
267 1471
!
312 (55J 306 154l
446 IT91 330 (671
SECOND REVISION
FIRST REVISION
GDT-O7t74A
Figure 268. Engine Heat Transfer Coefficients on Turbine Shroud/Outer Diffuser Model.
, FLAT
o NO DIFFUSER DUMP
. NO DOLT HOLES
, REDUCEDO0
62 REGION _A3 ,. _w
GOT_7&75
PREVIOUS CURRENT
GIlT 071i.?ll
224
o The RBSN turbine shroud had the lowest
MPS (115.1 MPa) of the three materials
considered.
o The change from a type B3 to C3 turbine The transition duct provides the outer flow
shroud results in a 36 percent reduction in path between the combustor and turbine
the outer diffuser MPS. shroud. It axially supports the combustor
baffle with a standoff midway along tkge com-
Various materials were also considered for ponent. Three holes are provided to monitor
the turbine shroud and outer diffuser and are the turbine inlet temperature. Mechanically,
presented in Table 42. The analyses con- the component must carry a radially inward
sidered the latest refinements in the model pressure load and an axially compressive load
and boundary conditions and represented the due to engine pressure loading. Thermally, the
thermal conditions for a normal engine light- component is exposed to both a through-the-
off. The current type B3 turbine shroud and wall and axial thermal gradients. Pressure
type A3 outer diffuser was used in the anal- loading is normally negligible, compared to
yses. The results are as follows: thermal loading.
225
m
m
0
_J _J _J _J _J
=_°omo
_J
226
m _
I=
+_i,i
p,
o_M
"F_
_ _I. el.
=E
L •
_+i °-
_._ ,_ ,o
0
0
.M.
227
g82
_'- 782 j
60.000 RPM
I
w.
382 43000. RPM _ -- 0.129 KG/SEC
(720)
i
0 21 C
,(70FI , i , , , , ,
(0) 0 60 120 180 240 300 360 420 480
TIME AFTER LIGHTOFF. SECONDS
GB7-078-392
The combustor baffle diverts the flow from backshroud is significantly influenced by the
the can combustor into an annulus flow circu- turbine rotor. The heat transfer coefficients
lation for the turbine section. It is axially along the backshroud reflect a complex inter-
contained between the transition duct and action between the rotor speed, blade back-
turbine backshroud. The baffle utilizes three face clearance, hub backface clearance, and
struts to interface with the transition duct the resulting hub backface flow distribution.
through the flow path. Mechanically, the Additionally, the large mass of the rotor hub
component must carry a small pressure drop provides a radiation heat sink during light-off
across the component and a spring load. transient conditions.
Normally, mechanical loads are negligible.
The thermal environment consists of radiant A 2-D finite element model as shown in
heat from the combustor and convective heat Figure 274 was created to evaluate transient
transfer along the flow path, peaking at the thermal stresses. The model was initially used
stagnation point on the centerline. to evaluate component stresses in the static
structure rig. Two transient cycles were
The turbine backshroud provides the flow analyzed, the light-off (cycle 9) and the shut-
path boundary at the axial backface of the down (cycle 10) shown in Figures 275 and 276
radial turbine rotor. The backshroud has a respectively. Two different materials, RBSN
circular disk geometry with concentricity to and SASC, were considered for the combustor
the engine centerline provided by a pilot baffle material. The cases considered and
diameter at the turbine stators. The pressure their results for the combustor baffle and
stresses acting on this component are negli- transition duct are shown in Table 43.
gible when compared with the thermal High stresses were found on the combustor
stresses. The temperature distribution in the baffle struts during shutdown. To reduce
228
LOCAT,ON
A, (NODE
_ll
MPz [KSll
°o ,NODE
T.j ----.__to_,o. A_
30 • : LOCAT,DN
C\
NOOE 9331 _ _, ._ COMOUSTOR BAFFLE
24
154.4 (22.4l-
fm
_ _ _ _ _ _ _ • j _, TRANSITION OUCT Z'_
_ 1111
1Z
o//
80 180 240 320 400 480 580 64O
TIME AFTER LIGHTOFF. SECONDS
._ _,..o _ ---- . . --
,oo 1B
•=i_= 8o 1o -
i 2o 5/ GI/17I.II4
° : [NOOE 8251 "_,_.INOOE 1111 _ : INOOE 4,.ql I respectively for an SASC combustor baffle
it
and transition duct during light-off.
I _J
229
C X 102 IF X 1021
14 - 25
12-
1093C [2000Fi
20-
10-
8- 15"
__ 8-
10-
4-
--93C (2OOFI
0 I
! I I J I I I
5 10 15 2O 25 30 35 4O
TiME AFTER LIGHT-OFF,SECONDS
GDT.07&115
cxlo 2 IF X 1021
14-
12-
20 C (2OOOF],STEADY-STATE
I0-
25_093
8-
649C (1200FI
__. 5-
I0.
=__
4 m
I l I I I I i
0 5 10 15 20 25 30 35 40
230
c_
0 0 0 0 0
o_
0
I¢1
231
Changes to the combustor baffle strut off cycle to 1149C (2100F) maximum power
design were not made since shutdown condi- condition (cycle 15), as shown in Figure 278 to
tions during engine operation have been made evaluate rotor backflow effect with engine
much less severe than the shutdown cycle speed. Following is a summary of the signif-
analyzed. To ensure against failures in the icant results:
static structure rig, the shutdown cycle was
made more gradual. The combustor baffle o High turbine backshroud MPS were found in
alternate design configurations were kept as all cases with the rotor modeled.
backup designs.
The consideration of turbine bore cooling
The transition duct/combustor baffle/tur- significantly increased the MPS (66 to 70
bine backshroud model was then modified to percent increase) on the turbine back-
reflect engine conditions. The primary differ- shroud. MPS occurs after engine speed
ence consists of including radiative and reaches I00,000 rpm.
convective heat transfer to the turbine rotor.
The turbine rotor component has a large O The effect of rotor backflow circulation
thermal inertia and acts as either a heat sink reduced the MPS on the turbine back-
or source during transient operating condi- shroud.
tions, in addition for the 1149C (2100F)
development engine with the dual alloy O The effect of mixing in rotor backflow
metallic turbine wheel, turbine bore cooling circulation increased the MPS on the tur-
would impinge upon the backshroud. bine backshroud.
Table 44 shows the results of a study on o The effect of the rotor on the transition
the dual alloy rotor effect on the transition duct and combustor baffle stresses is
duct, combustor baffle, and turbine back- insignificant.
shroud stresses. For MPS locations refer to
Figure 274. The study considered effects with o The MPS on the transition duct does not
and without turbine bore cooling, backflow occur during the initial light-off, but after
circulation between the rotor and backshroud, rotor speed reaches I00,000 rpm.
and mixing of the circulation. Midway through
the study the analysis was updated to include Table 45 shows the results for various
the change from an A1 to A2 type combustor component materials considered for the all
baffle (Figure 277) and an SSN to SASC ceramic engine with an SSN turbine rotor.
turbine backshroud. All results are for a light- The analyses assumed rotor backflow circula-
tion with mixing, but no rotor bore cooling.
For comparative purposes the operating cycle
(cycle 15) was the same as for the previous
engine analyses. The results for these anal-
_THICK
LOCALLY < '_ yses are as follows:
THINNEO--'-4"
O The transition duct MPS is almost indepen-
dent of the choice of materials for the
combustor baffle or turbine backshroud.
- _ WALL
WALL/__
232
_'_ o,1 _1 _ _1
E-.<
0
.m
Q;
:E •D _D 0 0 0
E-.<
a
!-
0
S 0
0
E-.<
e. °_
o
iT. UO_
_J
0
c-
O
o
._ 0 _
ZI
0,._
m_
a
o _ o o
Z Z _ 0
r_
_J
_
.!
_J
233
cxlo z IeXtOZl
1149C [2100Fi
21, 100
11.5-
60 KRPM
-60
i 6,8?.- 12.6-
-o.
v,
KDPM
E 8.4- .40
4.49"
-- 21C I70F) 0
Oo O I I I I I I I
G|T.OTli.11|A
234
0
_A
0 O
0 _ 0
¢1
_-' III
e_
C
0
°_
a
0
II
!°
0
II.
235
,,,q
m. <
_ _ n
_ _ |
a
ii!
236
UNIFORM CENTER THINNED
THICKNESS HOLE SECTION
_Y AI A2
6117-0711-1
Ilia /
Figure 279. Alternate Configurations
of the Turbine Backshroud.
didates were
deflections along sealing surfaces
and associated stresses.
evaluated
Two material can-
for this component,
!
LAS and RBSN, although LAS was the only
material from which actual components were
made. STRESS VALUES AT SIMILAR HOUSINGLOCATIONS
237
A 3-D finite element model was created of gradients were being created in the housing
the thin wall configuration and stresses and from the heat sink effect of the outer flange
deflections were determined. The model was being exposed to compressor discharge air. To
constrained against rigid body motion only for eliminate this heat sink, another configuration
evaluation of thermal stresses. For evaluating (type Xl) was created without this flange.
pressure stresses, the model was axially con- The axial support was thereby removed to the
strained at all of the circumferential row of diffuser end of the flow separator housing as
nodes that interface with the flow separator shown in Figure 282. Insulation would be
housing support ring. In addition, nodes at the
location of the piloting slots were constrained LOCALIZEO
STRUTS
against rigid body radial motion. Pressure
stresses and deflections were found accept-
able, but both thermal stresses and deflections
at the regenerator seal surface were found to [
be excessive. The thermal stresses and
deflections during light-off increased with
-_ I LE
time during the transient interval and were
found to be maximum at steady-state operat-
ing condition. To reduce the deflections at
the regenerator seal surface, a strutted con-
figuration was created. Four struts were SUPPORT PIN
located 60 degrees apart, two in the HP side, FIXED HERE
238
Table 47. Flow Separator Housing Pressure Stresses.
,i
Flow Separator
Housing
239
_m IMILSI _ ; RGSN TYPE B2 {STRUTTEOJ "- : RBSN TYPE 61 [ORIGINALI
_m {MILS) v , HOT I.D. SEAL e , HOT GO. SEAL
1015-
152.4 -
50.8-
101.6-
D- .=.
iG
_ -50.6-
",.,... ,,_,_ i'°',
' g
50.8-
=,_.J
O-
"",-- _... '-9O I-,1.9)
-IOl.fl-
-50J-
-152.4_
-1el,G,
-9O -80 -30 0 30 80 9O DEGREES
-9O -80 -6O 0 30 8O 90 OEGREES
ANGULAR POSiTiON
ANGULAR P_SITIGN
G|7_/|-124
||7-o70-1 _6
ym (MILSI v _ LAS TYPE B110RIGINAL} o :LAS TYPE D2 ISTRUTTEDI platform deflection than the B1 configu-
101.0- ration.
] [
[2.7J 8#
HP.._I i _ LP
z.,,_,. The X1 configuration had 95 percent less
5_.G-
11.51 38 _-_,..
,_ -50.8-
% The low spot on the inner regenerator seal
axial surface is located midway between
-101.6-
'-,,, 1 the crossarms on the HP side of the flow
-152.4 -
_'-,, .137 {-5.41 separator housing.
i 1 h
-9O ..60 -30 0 30 6O 90 OEGREES
240
The MPS is very sensitive to the assumed
heat transfer coefficient between the flow
LASTYPE B1 CONFIGURATION separator housing flange and the compres-
120(] FLANGE
HTC= 31.2 WATTS/CM
2 -K {5.5 BTu/HR-FT
2 -F]
i2192l-
sor discharge temperature. The MPS is
more sensitive for components made from
RBSN than LAS.
"\
o The strutted (B2) configuration MPS is sig-
\ nificantly higher than the MPS for the
\
[1112]-
\ original (BI) configuration.
'%
k-- o The MPS occurs at the outer surface of the
300 L
241
0 At the higher value of heat transfer coeffi-
0 RBSNH = 31.2 WATTS/CM
2 -C 15.59TU/HR-FT
2 -FI cients (31.2 watts/cm2C) the regenerator
* RBSNH = 5.7 WATTS/CM
2 -K 11.0 BTU/HR-FT
2 -F) seal platform deflections are greater for
LAS H = 31.2 WATTS/CM
2 -C [5.5 RTU/HR-FT2-F[ housing. At the lower value of heat trans-
fer coefficients (5.7 watts/cm2C) the op-
pm MILS) Q) LAGH = 5.7 WATTS/CM
2 -C II.O 8TU/HR-FT
2 -F)
posite is true.
254-
I0 t
"" "_
"
; 21618.5)
__
il L. O The strutted (B2) configuration has a signif-
293.?-
icantly lower level of regenerator seal
_ 152+4-
_=
--I_I
tP,
......... -+,,
t2715.+oI
platform
average)
deflections
than
(68 percent
the original
on the
(B1) eonfigura-
-, 101.6- lion but has a higher variation (100 per-
I I _ cent) in-deflections.
50.8'
667.,076-1269
ANGULAR
POSITION.OEGREES flow separator housings occurred at steady
state conditions. Consequently, the MPS for
Figure 288. Steady-State Cruise Thermal these configurations also occurred at the
Defleetions at the Regenerator Seal for steady state condition. Figure 290 shows the
Type B1 RBSN and LAS Flow Separator
TRANSIENT
L/O CYCLE8
Housing. Mrs (KSIJ
FLANGEHTC= 31.2 WATTS/CM
2 -K )5.5 BTU/HR-FT
2 -P
172.3' 25
I tL
ROSNB2 CONFIGURATION 137.9" 20
&/m [MILS) FLANGE
HTC= 26.4 WATTS/CM
2 -C 15.0BTU/RR-FT
2 -F] [ 133 MPI 119.3K',
($TEADY-STATEiJ_
254-
103.4- 15
_.2"
/t
f
68.9. lO
_ 152.4.
34.6- 5 //
._ 101.6- /
o/
50.8- 0 4 8 !2 I6 20 24 28 32
TIME AFTERLIGHTOFFo
MINUTES
167-071-130
O-
Figure 289. Steady-State Cruise Thermal transient MPS response for the type B1 con-
Deflections at the Regenerator Seal for figuration, which was typical for the con-
the RBSN Type B2 Flow Separator Housing. figurations with the outer flange exposed to
the compressor discharge air. The MPS for
deflection is similar to the MPS. Specific- the flangeless (X1) configuration was found to
ally, the deflections are very sensitive to occur during the transient light-off interval of
the assumed value of heat transfer coeffi- the operating cycle. Table 49 shows the MPS
cients, greater for RBSN than for LAS. for two cases that were considered. The first
model, as with the steady-state analyses
242
Table 49. Flow Separator Housing Transient Thermal Stresses
With
Inner to Time After
Case Configuration Outer Cone Magnitude, Start,
No. Type Material Radiation Location MPa (ksi) SCC
11 X1 RBSN No G 900
Cycle 8 Lightoff
*For locations see Figure 283
neglected the radiation between the inner and transient temperature responses were com-
outer cones of the flow separator housing. pared to the test results. Initialcomparison
The latter analysis included this radiation. showed a significant lag in the temperature
The results are summarized as follows: response in the analytical model compared to
test results. Inclusion of cross radiation
Without cross radiation from the inner to between the inner and outer cone of the flow
outer cone, the MPS is higher for the separator and increased heat transfer coeffi-
flangeless (Xl) compared to the original cients helped but still were insufficient to
(B1) RBSN flow separator housing at show correlations. The most reasonable
steady-state conditions. hypothesis is that combustor heat reradiating
from the transition duct should have been
With cross radiation, the MPS is lower for modeled since it apparently provides a signifi-
the flangeless compared to the original cant heat input to the flow separator housing.
RBSN flow separator housing at steady- The foregoing conclusion is that the transient
state conditions. response and perhaps the MPS is less than
determined from analyses.
o Including cross radiation reduces the trans-
ient time to MPS. 6.3.1.6 Turbine Stators
In September 1985, the metal engine (S/N The design and development of the turbine
001/Build 34) was tested with 32 thermo- stators (reference Figure 250) is primarily
couples attached to a metallic flow separator controlled by its severe thermal environment.
housing. Additional instrumentation was used High core flow velocities produces high heat
to monitor the inlet guide vane setting, flow transfer coefficients, which coupled with the
path temperature, and engine speed. Data was required nonuniform vane profile,creates high
recorded and reduced for three transient light- thermal stresses at the vane trailing edge
offs to low cruise (60,000 rpm) condition. The during engine light-offs. High reliabilityand
boundary conditions and light-off cycle was survivability is also essential to ensure that
duplicated with an analytical model of a even minor stator damage does not lead to
metallic flow separator housing and resulting secondary impact failure of the turbine rotor.
243
The initial development effort concen-
trated on the segmented stator concept
designed in 1980. Both RBSN and SASC
stators were fabricated. In November 1984 a
stator thermal
the turbine shroud
screening test was run using
screening
objective was to thermally
rig. The test
shock stator seg-
/
ments (RBSN) to normal
tions (plus 25-percent
engine start condi-
stress margin). Follow- /
ing the test, no cracks were found in the
stator trailing edge.
244
metallic stator assembly as shown in Figure
294. This run occurred in conjunction with a
similarly instrumented flow separator housing.
The transient thermal resl_onse for three light-
STRAIGHT
CUTBACK
G97-071£132
•6
8.18
9.19 e 4
e2
FILLET
X
Gmt_7_l_4 ENGINE
245
offs were recorded and reduced. Engine light-
off parameters were then simulated in a 3-D
thermal analysis of the metallic turbine stator
model. Temperatures from the analysis were
than compared to the measured test results.
A good correlation was found using the origi-
nally calculated heat transfer coefficients if
the measured thermal response was assumed
to lag due to thermocouple limitations. Two
representative comparisons between the MIN = 239C 1402F)
T15J T12J
1200 1200
,4 . ,,,
(32) D 8 16 24 32 40 48 56 54 132l O O Ie 24 32 40 48 56 64
6|7_T&i35A MIO-VANE
LEADING
EDGE MID-VANE
TRAILING
EDGE
Figure 295. Typical Correlation Between Test and Analytical Turbine Stator
Thermal Response.
246
MPa IKSII
• STRAIGHT-CUT VANE * CUTBACK VANE
103.4.
(12.9
KSll _._ ..........
68.9-
a.
E
34.4-
/ MAX
: 95.,
M,,,
,,2.o7
K.,,,
MIN = 16.1 MPa [-2.329 KSI]
O-
MPa (KSli
C (F) -0.7 ,0.1
815 ° 13.1 119
I v SIG'I STRESS
zeo 30
40.7 5.9
/ 54.4
68.2
7.9
9.9
/
[,-
82.0 11.9
260-
Z i i 95.8 13.9
MATERIAL: RBSN
CYCLE 17 GD7.076-138
Oq
247
6.3.1.7 Combustor Assembly The critical design loading for the com-
bustor component is thermal loading. Mechan-
The combustor assembly (Reference Figure ical loading consists of small axially com-
250) was designed to have a low emissions and pressive loading from the combustor spring
specific fuel consumption (SFC) capabilities. and compressive hoop loading from the small
To meet these goals a lean burn concept was radially inward combustor p.ressuredrop. The
utilized in con]unction with a regenerative thermal loading is induced by the flame radia-
combustor inlet air source. The lean burn tion and gas convection of the combustor.
concept creates a uniform lean fuel-air ratio Circumferential and axial hot spots can also
that minimizes NO x. The high inlet temper- be created, the severity of which depends upon
atures cause the CO and HC to be oxidized to the fuel nozzle performance.
an acceptable level.
To evaluate thermal stresses in the com-
Development of the combustor design has bustor assembly, the axisymmetric finite ele-
evolved to the existing combustor assembly ment model shown in Figure 301 was used.
configuration as shown in Figure 300. The The model consisted of the combustor end of
modular main fuel nozzle incorporates an axial
the engine that included all components from
ignitor. It includes a pilot combustor with a the engine housing inward. The finite element
full open radial inflow swirler at the pilot exit.
model was based upon an earlier design that
The absence of holes in the liner walls and the
did not include the pilot combustor compo-
low temperature differential between combus- nent. Convective heat transfer coefficients
tor inlet and discharge temperatures mini-
were analytically derived and applied as
mizes thermal stresses.
boundary conditions. Flame radiation was
considered as well as radiation between engine
NOZZLE ROME components and to the engine external
\ SPACER SWIRLER / environment.
GII;..071_I 4|
248
982C i1900F1
II 87,c, EI - -------
II
l I i___ r_,] t"
....
#'#-'I@_,_=__:_.,,___._-----1204C
_IIOI_CIIDOOFi
12200F) ALL TEMPERATURES IN C IFI
_......__- ISOPLETH iNTERVAL 111C {2OOF)
1465C i2669FI
GiT-OT&I42A
Figure 302. Combustor Assembly Steady-State 1371C (2500F) Max Power Temperatures.
MAXIMUM PRINCIPAL
STRESS
G67-076-|43
Figure 303. Combustor Assembly Steady-State 1371C (2500F) Max Power MPS.
The transient start stresses were evaluated variations of the flame or gas within the
with the lightoff cycle to 1281C (2337F) cruise combustor were not considered in these
condition as shown in Figure 304 (cycle 22). analyses. Consideration of these variations
Shutdown stresses were not analyzed due to would probably make significant increases in
the benign effect of the regenerator system. MPS levels but was not evaluated due to the
The MPS responses are shown in Figures 305, uncertainty of the actual combustive environ-
306, 307, and 308 for the four ceramic com- ment.
bustor assembly components. The highest MPS
was 32.4 MPa (4.7 ksi), located at the outer 6.3.1.6 Component Assembly/Sealing
edge of the combustor support, and which
occurred 180 seconds after lightoff. The design of ceramic components must
take into consideration the interfacing of high
In summary, the analyses showed very low temperature brittlematerial into an assembly.
thermal stresses for the assumed combustor This section specifically addresses these
burner condition. Axial or circumferential design considerations. They include designing
249
CX 102 (FX 102j
14-
100
1280C 12337F]
-80
35 KRPM
.80
KRPM
I_ = 0.16 KG/SEC [0,357 L8/SEC) -40
s
M = 0.07 KG/SEC
(0.150 Lg/MINi
(70F)
I I I i I I I
5 I0 15 29 25 30 35 40
TIME AFTER LIGHT.OFF, SECONDS
UT.07D-144
41.4
-- 41.4"
55.1-
27.6
41 e C i 27.6" f
J
13.8"
13.8 /
/
O- p'A O- O
0 40 90 129 IN) 20O 240 280 329
O 40 60 129 160 290 240 280 320
TIME AFTER LIGHTOFF,SECONDS
TIME AFTER LIGHTOFF,SECONDS
607-076-1450
Figure 305. Spacer Sleeve (RBSN) Start Figure 306. Nozzle Support (RBSN)
Transient MPS. Start Transient MPS. *
the axial and radial support system, sizing and address these design considerations, it is a
controlling the critical dimensions to ensure prerequisite necessity to have a thorough
against interference between ceramic com- understanding of the mechanical and thermal
ponents, and designing the sealing interfaces growth of the overall engine during its duty
to obtain optimum engine performance. To operation. On the AGTI01 program initial
250
MP| KSli
68.9- 3
REGENERATOR COMBUSTOR8AFFLE/
L STACKUP STATOR/BACKSHROUO
, NODE 45 __J__l
5,5.1-
ll/Ill-lSth
NODE 818
design effort was accomplished using analyti- A subassembly of the inner stackup is the
cally determined _cowth and was updated as combustor baffle/turbine backshroud, and
engine test data became available. turbine stators stackup. The inital design for
this engine did not have this subassembly
To control the axial positioning of the stackup, but had the inner ceramic loadpath
ceramic components, springs have been used going directly through these three ceramic
to axially load these components against con- subassembly components. The incorporation
trolled surfaces. This thereby eliminates the of this subassembly stackup design was a con-
possibility of component failure due to sequence of seal improvements, as discussed
thermal interference between the ceramic and later in this section, made at the flow separ-
supporting metallic components. Five sets of ator housing, transition duct, and turbine
ceramic component stackup as shown in Figure shroud interface.
4
251
the flow separator housingis axially piloted by The components are axially loaded by the two
the regenerator stackup. The regenerator regenerator diaphragm seals. The flow
shield was designed to be loaded by an outer separator housingsupport ring was constructed
combustor spring more lightly loaded than the to, minimize the thermal growth differential
inner stackup. Again, this spring was sized to •between the engine housing and the regener-
meet a 6-g lateral shock load and to allow for ator components. This provided a more uni-
growth differential between the outer stackup form seal performance and regenerator drive
and the enginehousing. torque.
The diffuser stackup consist of the inner The radial support for ceramic components
and outer diffusers and is loaded by a com- must be able to maintain the concentricity of
pression spring against the turbine shroud. As these co.mponents without introducing any
shown in Figure 310 changes have been made mechanical interference. Two types of
to the first generation support system. The piloting methods were used to maintain con-
first generation load spacer in a series of tests centricity of the ceramic components to the
had a tendency to become cocked and wedged engine centerline. One of these, an eccentric
in the guide sleeve. The load spacer was pin in a radial slot, was used to pilot the flow
changed to a ceramic ball supported by a separator housing. This system consists of
conical spring. A stiffer spring was also used three radial slots in the outer rim of the flow
to increase the axial support load from 9.5 kg separator housing through which three
(21 Ibs) to 36.3 kg (80 Ibs) force. On previous metallic eccentric pins, mounted to the main
testing (static structure build 9) failure of the engine housing, maintafn component concen-
outer diffuser was attributed to vibratory tricity. A more innovative method is used to
energy from this spring-mass system. pilot the turbine shroud module. This method
consists of a three support rocker assembly
The regenerator stackup consists of the (Figure 311) that replaces sliding friction with
regenerator core and flow separator housing. rolling friction at a highly loaded interface.
TURBINE TURBINE
% i
SHROUD SHROUD
J
I
OUTER
DIFFUSER
OUTER
DIFFUSER
I iNNER
DIFFUSER
INNER
OIFFUSER
__ LOAD
SPACER
6|7_7_140
COMPRESSOR
BACKSqROUO
1
Figure 310. First and Second Generation Diffuser Support System.
252
Component concentricity is maintained in this
configuration through interfacial friction at
the rocker contact zone.
SECONOGENERATION
ROCKER/ECCENTRIC
FIRST GENERATION
ROCKER/ECCENTRIC
TURBINE
;RROUO
GB7_TO-151A
253
clearances between the rotor to shroud inter-
face were determined for transient and
/----'T--V
steady-state operating conditions. Since close
turbine running clearances are critical to opti-
mum engine performance, instrumented engine
PREVIOUS FAILURE ORIGIN testing is normally conducted to verify
analysis. This criticality is compounded with
SLOTTEO CONFIGURATION
the low rub tolerance of ceramics compared to
metallics. On metallic engines, verification is
usually made by using capacitance probes
between the turbine shroud and rotor to mea-
I ,'
I I I sure clearances.
capacitance
On ceramic
probes do not function.
fore, the approach followed
components,
There-
was to measure
SLOTLESSCONFIGURATION
running clearances with the early metallic
version of this engine. These clearances were
G|7_7_152 then adjusted to account for the difference in
materials and higher operating temperatures
Figure 313. Slotted Versus Slotless Turbine of the all ceramic engine. Further discussion
Shroud Configuration. of the turbine clearance evaluation can be
found in engine design and development (Sec-
shown to adequately retain the turbine shroud tion 4).
in position in a shake-table test. The slotless
configuration, which relies upon frictional There are three high temperature leak
loads alone to maintain turbine shroud posi- paths from the HP to the LP cavities in the
tion, withstood a 12-g load. static structure of the engine as shown in
Figure 314 that require the use of ceramics.
The radial clearance between ceramic
These seal areas are:
components was also sized to eliminate poten-
tial thermal interference during engine opera-
tions. The stackup of ceramic components has
to be designed for unconstrained thermal REGENERATORSHIELD/
FLOW SEPARATORHSG. -_
growths without any radial interference _,__ .TURBINE
between adjacent stackups. In addition, /" SHROUO
corner and fillet radii had to be sized to
preclude the possibility of mating components
contacting within the radii. An example of
this occurred during development assembly of
static structure rig, build 7 when the flow
separator housing failed. Disassembly and
inspection of the fractured component
revealed the presence of an interference
between the fillet radius of the flow separator
housing inner lip and the corner radius of the
mating regenerator shield. The corner radius
was increased to a larger value than the fillet
REGENER*TO,
SR,E,.O
EXHAUST ]'
radius in the mating part, thereby eliminating
GDT_T&IS,1
the possibility of localized contact within the
radii.
Axial clearances between the rotor to Figure 314. High Temperature Ceramic
backshroud interface and axial and radial Seal Areas.
254
o Turbine shroud/flow separator housingseal housing area. Because of space limitation, the
o Regenerator shield/flow separator housing wave spring was removed and the piston ring
seal was loaded by the inner combustor spring. To
o Regenerator shield/exhaust housingseal allow the for differential thermhl growth
between this seal area load path and the
Early testing (static structure rig, build 4) combustor baffle, backshroud, and stator load
investigated the usageof a ceramic fiber seal path, a wave spring was inserted into the
between the turbine shroud and flow separator latter load path as shown in Figure 316.
housing. The rig was assembledand a static
leak check performed. The results indicated a The axial interface between the
gross internal leak at the fiber seal area. The regenerator shield and the flow separator
fiber was replaced with ceramic ring seals for housing relies upon the outer combustor spring
all subsequent testing. load to control the seal leakage. Testing of
this seal area indicated a very low leakage
To investigate the performance of ceramic rate that met design criteria.
ring seals, static seal leakage rigs were de-
signed. These rigs were designed to measure The two piston ring seal concept was
seal leakage as a function of seal force and adopted for the regenerator shield/exhaust
pressure differential at the three high housing seal area. The axial load was provided
temperature seal areas. In addition, each rig by a ceramic wave spring in the stackup.
has the capability of establishing the degree of
concentricity between parts being sealed so 6.3.2 Rig Design/Development
that seal performance can be measured and
compared to predetermined amounts of 6.3.2.1 Introduction
eccentricity.
The ceramic structural parts received from
For the baseline configuration the leak AGT101 program suppliers are qualified for
path at the turbine shroud/flow separator engine testing according to the flow chart
housing area was found to be the most critical shown in Figure 317. The iterative design/
in terms of performance loss. The baseline inspection/test/redesign approach in devel-
configuration consisted of a single LAS piston oping engine quality hardware is designed to
ring between the turbine shroud and flow eliminate discrepant parts before they reach
separator housing axially loaded by a ceramic the engine test phase. Each component is,
wave washer. The following results were therefore, subjected to 40X visual and dimen-
noted. sional inspection, non-destructive evaluation
(NDE), and series of rig tests for final qualifi-
o The effect of the axial spring load on the cation prior to engine installation. A list of
seal performance in the baseline seal all of the rig tests used in this qualification
configuration was negligible. process is shown in Table 50.
255
CONFIGURATION2
.
[---1
LOAO
1
REACTION
CONFIGURATION__ '
IL
]i]. 2/
i O.IR-D.
O"D
I I I I I I l
O 16 32 48 64 (PSIG]
I I I l I
O 11 22.1 33.1 44.1 kPa
RIG PRESSURE
6B7.07i1-154
256
RECEIVING
DESIGN VENDOR
INSPECTION
MECH PASS
FAILURE
SCREENING
ANALYSIS
RIGS
THERMAL I_K{2_F]
SCREENING STATICRIG
RIGS
687478-280
sembly. Further, the static structures rig base for evaluating thermal, stress, and risk
evaluates the sealing capability, component analysis tools and methodologies.
capability, axial and radial pilots, contact
loading, and stresses at elevated temperature. 6.3.2.2 Mechanical Screening Rigs
Components that fracture during any phase of
this evaluation undergo intensive fractography Mechanical screening tests have a dual
and analytical reevaluation to determine the purpose; establish overpressure capability and
cause and recommended solutions. The maxi- measure strain, and qualify parts. Initial tests
mum operating condition for this rig was set were performed on the flow separator housing,
at 1093C (2000F), which corresponds to the regenerator shield, and those components that
maximum operating temperature of the regen- provide the attachment between the ceramic
erator in the AGTI01 engine. turbine shroud and metal compressor back-
shroud. These parts have low thermal stresses
To evaluate ceramic structures upstream due to a combination of uniform heating or to
of the turbine exhaust, such as the turbine, a low thermal expansion coefficient (i.e.,lithi-
stator, shroud, backshroud, combustor baffle um aluminum silicate material).
and transition duct at the higher flow path
temperature of the engine, another rig, the The test fixture for the regenerator shield
1371C (2500F) static rig is used. Long-term screening rig is shown in Figure 318. The
testing at 1371C (2500F) temperatures is per- initial regenerator shield test incorporated the
formed in this rig to investigate the high use of strain gages to measure strain distribu-
temperature effects on ceramics, such as tion and magnitude during pressurization. This
static fatigue, contact loading, and endurance. instrumentation was installed as a checkout of
the test procedure. Pressure was applied until
In addition to screening substandard com- a strain level equivalent to 137.8 MPa (20 ksi)
ponents, the component test rig provide a data was achieved. This stress level was selected
257
Table 50. Ceramic Component Rig Tests.
Flow Separator Housing Rig Mechanieal screening of flow Internal pressure proof test of
separator housings HP cavity
Stator Torch Test Low-cost thermal screening Lightoff thermal shock testing
of turbine stators using oxacetylene torches
Static Structure Rig Long term elevated tempera- Elevated temperature testing
ture interface evaluation of up to 1093C (2000F) with a
all static structure compo- gentle lightoff and cool-down
nents cycle. Uses an internal com-
bustor.
1371C Static Rig Long term maximum tem- Elevated temperature testing
perature interface evaluation up to 1371C (2500F) with a
of turbine section static gentle lightoff and cool-down
structure components cycle. Uses an external com-
bustor.
258
because it exceeded the predicted combined
thermal and mechanical stress exposure in
operation and is less than one-half of the
material characteristic strength.
G87-078-262
259
air bleed valve. Using gaskets and o-rings, the shroud attached by three sets of rocker com-
high pressure cavity is sealed so that pressure ponents to an aluminum plate which functions
can be applied to simulate engine operating as the compressor backshroud. The objective
of this test is to subject the three rocker
pressures. The flow separator housings are
screened at pressure levels that represent 125 assemblies and shroud attachment area to a
percent of the maximum mechanical loads 1814 kg (4000 lb.) axial load. This represents a
exerted in the engine at maximum power con- pressure load 25 percent greater than the
dition. maximum power pressure load.
261
DISCHARGE
HEATED
AIR
SUPPLY
6117-07D-2115
Figure 322.
Screening Rig.
LJ
outer diffuser rig uses. In addition to mon-
GD7-078-266
itoring the combustor discharge temperatures,
two thermocouples monitor the flow temper- Figure 323. Transition Duct and
ature at the T4.1 ports on the transition duct. Baffle Screening Rig With
The acoustic emission probe is positioned onto Original (top) and Final (bottom)
the transition duct at the third T 4 port. Configurations.
/'D
262
uses as a support platform a piece of Lockheed then reconfigured to the previous insulation
HTP-12 insulation which is formed to provide arrangement. Again, tests were run with and
both the support and a portion of the discharge without stators. Finally, the new insulation
flow path. This also has proved inadequate piece, which nests behind the turbine shroud,
due to erosion in the flow path ahead of the was installed with tl_e remainder of the rig
struts. Other changes in this rig include employing the former insulation. This con-
increased insulation along the rig inner walls, figuration was run to provide data on any
change from aviation fuel to natural gas, and effects that this single change may have. The
the addition of a viewport to visually monitor 3
4
the mechanical integrity of the transition
duct. The change was made from a liquid fuel
burner to a natural gas burner for better
lightoff characteristics and more stable opera-
tion under severe transient conditions, leading
to more repeatable screening tests.
263
results of this test are discussed further in the O Rig modification was made to include a
analysis and design section on the turbine ceramic transition duct, combustor baffle
shroud (paragraph 6.3.1.3.2). and seal rings into the flow path. This was
done tq more closely simulate engine heat
As a result of rig testing with a metallic transfer coefficients on the turbine shroud.
shroud the following changes were made:
The rig discharge section of the insulation
The lightoff cycle required to proof the was replaced with Lockheed HTP-12 type
turbine shroud was made less severe and insulation.
became dependent on the shroud material
being tested [changing from 93 to I149C Two ceramic waveguides are now utilized
(200 to 2100F) to approximately 93 to in this rig test; one in direct contact with
871C (200 to 1600F)]. the turbine shroud mounting flange and the
other in contact with the transition duct.
O The housing cavity insulation was reduced
to allow for more cross-radiation between O A viewport has been added at the forward
sections of the turbine shroud. end of the rig to allow for visual inspection
of the turbine shroud and transition duct
Continued rig improvements were made as interface area.
a result of further rig problems. Some
changes were made only to be later discontin- The thermal cycles for the screening rigs
ued. A chronological order of these problems are defined so as to simulate stresses which
and changes are covered in detail in a previous exceed analytically predicted engine stresses
report*. The design changes made that have under normal start conditions by 25 percent.
been incorporated into the final rig configura- A normal engine start in defined as ambient to
tion include: 1218C (2200F) in five seconds at idle air flow.
These proof cycles are given in tabular form in
*Ninth Semiannual Report - Advanced Gas Tur- Table 51. The test cycles for the turbine
bine (AGT) Technology Development-NASA shroud have been rigorously developed by
CR - 174886 determining heat transfer coefficients for
_Jsec
Trig, At_o, ts/D,
Component(s) Material (Ibm/rain) c (F) sec sec
264
both the engine and rig from test data and The original and final configurations for
verifying or updating the accuracy of the the ceramic static structure rig are shown in
finite element thermal and stress analyses. Figure 325. The original static structures rig
The cycles for the other components were had two air inlet supplies that simulated com-
developed assuming similar flow conditions pressor discharge (HP), and turbine inlet con-
occur in the engine and rig. ditions (LP) in an open loop configuration. A
OISCHARGE
o To evaluate the durability of the ceramic
assembly under the following conditions:
265
three inch lab combustor provided thermal ceramic bolt assembly, the other on the flow
start transient and steady-state conditions separator housing. These locations were se-
under AGTI01 simulated engine idle and cruise lected so that all components could be con-
airflow conditions. tinuously monitored through one of the two
component assembly locations. The acoustic
Air, as hot as I093C (2000F), entered the monitor detects ceramic component fracture
structures rig through the inlet duct and then incidence through a high frequency transducer.
diffused through the ceramic transition duct; The system eliminates rig disassembly be-
thus heating the combustor baffle, turbine tween thermal start transients in which no
shroud piston rings, segmented turbine stators, high energy acoustic events are detected.
turbine backshroud, inner and outer turbine
diffusers, and LP side of the flow separator The last static structure rig test (Build 13)
housing. The air then passed through the was run in March 1985. Sufficient confidence
regenerator. was gained in the ceramic static structures rig
testing so that ceramic structural components
The cold, HP air entered the rig at temper- are now considered qualified for engine use
atures up to 93C (200F), flowed along the without passing through this phase of screen-
compressor backshroud and compressor hous- ing. The static structures rig was therefore
ing, turned in the exhaust cover, and was modified for use as a hot regenerator seal
heated through the regenerator. The air then leakage test rig.
flowed over the HP side of the flow separator
housing, around the transition duct through the 6.3.2.5 1371C (2500F) Static Rig
regenerator shield, and out of the rig.
The intent for this rig was as a vehicle for
Initial testing of the original static struc- performing tests at 1371C (2500F) of major
ture configuration showed a combustor insta- structural components, including transition
bility problem related to an improper pressure duct, combustor baffle, turbine backshroud,
drop across the burner. This can result in a stators, and turbine shroud. During maximum
lack of flame containment within the primary operating conditions, those components being
zone of the burner and, in fact, "allow" the forward of the rotor where work is extracted
flame to extend well into the turbine flowpath from the flow will be exposed to temperatures
region. The ceramic structural components up to 1371C (2500F). Those components aft of
would thereby be locally heated in an atypical the rotor will never be exposed to tempera-
manner. tures higher than I093C (2000F) in the engine.
Therefore, components such as the diffusers,
Attempts were made to alleviate this prob- flow separator housing and regenerator core
lem by modifying the combustor to operate at are fully evaluated in the aforementioned
a higher burner pressure drop, but satisfactory static structures rig.
combustor performance was never fully at-
tained. The solution to this problem was The 1371C (2500F) milestone was initially
achieved by using a singular flow arrangement achieved in a backshroud/stator/turbine shroud
with the engine metallic combustor. The final screening rig in April thru May 1984, although
rig configuration, used since August 1984, only for a short term cycle. To demonstrate
therefore simulates engine conditions more survivability over an extended time period a
completely. separate rig was developed.
266
THERMOCOUPLE This rig was first used in August 1984, but
TURBINE SHROUD
IT4.1I
ACOUSTIC EMISSIONS PROBE was unable to meet the 1371C (2500F) objec-
TRANSITION OUCT tive because of the fracture of ceramic com-
ACOUSTIC EMISSIONS PROSE ponents. Testing on this rig was terminated
and development of an improved rig was ini-
tiated. In the interim, until a replacement rig
was developed, 1371C (2500F) testing was
done using the backshroud/stator/turbine
shroud screening rig. This was done for two
reasons: to avoid thermal growth damage to
the 1371C static rig inlet housing due to
different heating rates in different areas, and
to avoid risking the flow separator housings,
which are not required for the 1371C (2500F)
testing.
THERMOCO_,
The dead weight employed was made of
300 Series stainless steel, insulated for protec-
,_l 4'
ACOUSTIC EMISSION tion. Unfortunately, it reached a high enough
PROBE
temperature at approximately 25 minutes
GBT-O78-269A
after achieving the 1371C (2500F) test tem-
perature, that premature shutdown of the rig
Figure 326. 1371C (2500F) Static was thought prudent.
Turbine Rig Original (top) and Final
(bottom). In May 1985, additional testing at 1371C
(2500F) was attempted. To extend the running
from previous screening rigs in that the in- time at the 1371C (2500F) temperature condi-
coming air enters via the flow separator hous- tion, the dead weight system was changed to
ing "smile" prior to combustion in the rig incorporate ceramics. However, the amount
burner. For this initial test a natural gas pre- of weight that can be physically installed in
heater was not used, as originally intended, the rig envelope was found insufficient. A
due to concerns about rig inlet housing integri- pressure differential at light-off between the
ty when exposed to heated inlet air. This flow path and the cavity surrounding the test
means that incoming air prior to combustion pieces caused the transition duct to move
was in the range of 93-121C (200-250F). The upward (axially) and then bounce back down
heating effect of the regenerator core was not upon the rest of the stack of parts. Further
simulated in this test. modifications to the loading system for this
267
rig were made to allow extended operation at In November 1984, all turbine shrouds were
1371C (2500F) test temperature. These modi- mechanically tested along with the rocker
fications included a component loading system assembly to proof these components against
where a spring load is transmitted through engine maximum pressure loading. A hydraul-
three air-cooled metal bolts. These bolts then ic press was used to incrementally apply a load
load a modified turbine shroud and thus the up to 1814 kg (4000 Ibs). This corresponds to
stack of ceramic parts. This arrangement is 125 percent of the maximum pressure loading
illustrated in Figure 326 (bottom view). of the engine. The first two shrouds to be
tested were an RBSN shroud from ACC and an
6.3.3 Component Rig Testing SN-54 shroud from NGK. The SN-54 shroud
passed the test undamaged while the RBSN
6.3.3.1 Mechanical Screening Rig Testing shroud failed at 1315 kg (2900 Ibs). The origin
of the fracture was located in the radius of
the piloting slot on the shroud flange.
Testing was conducted on three mechanical
screening rigs; namely, the regenerator shield
During December 1984, two additional
rig, the flow separator housing rig, and the shrouds, an RBSN, and SN-54 shroud were
turbine shroud/rocker assembly rig.
subjected to the mechanical proof test.
Again, the SN-54 turbine shroud passed the
The initial testing with the regenerator test while the RBSN shroud failed at approx-
shield rig subjected the ceramic shields to an imately 1315 kg (2900 Ibs). The origin of the
internal pressure loading that would screen out fracture was located in the same area as the
material flaw sizes that had strength less than previous failure.
137.8 MPa (20 ksi). Four regenerator shields
from Standard Oil (SASC) were tested and one Due to the two failures of slotted RBSN
failed at a pressure loading equivalent to 124.1 turbine shrouds during mechanical screening, a
MPa (18 ksi). design modification was implemented to
strengthen the area where these failures initi-
Subsequent regenerator shields were tested ated. This modification resulted in removing
at a lower internal pressure that induced the slots on the flange of the shroud. Mechan-
stresses (48.2 MPa) equivalent to 125 percent ical shock testing of the turbine shroud/sup-
of the maximum stress level encountered in a ports/compressor backshroud assembly had
normal engine operation. Fifteen regenerator shown that these slots, initially designed for
shields made out of SASC from Standard Oil piloting, were not needed to control piloting.
were received and tested and all passed with- The first modified RBSN turbine shroud was
out any damage. mechanically screened during April 1985. The
shroud passed the test, the first RBSN shroud
The flow separator housings were tested in to do so, and indicated that eliminating the
a pressure rig at the vendor (Corning) before stress concentration of the slot increased the
shipping to Garrett. Pressures were specified
load carrying capability to the require_ level.
for this test to simulate the maximum pres-
sure loading in the flow separator housing All turbine shrouds were henceforth fabri-
during engine operations (44.8 MPa). In addi- cated without the slots on the shroud flange.
tion to the testing at the vendor, testing was Of the remaining shrouds tested, only one, S/N
also conducted at Garrett, in another dupli- 726 (RBSN), failed below the required load.
cate rig, to substantiate that no strength de- Failure was attributed to a pre-nitriding crack
gradation had occurred whenever the flow in the shroud flange. Shroud S/N 744 (RBSN)
separator housing was reworked. In all cases did pass the test but was rejected for further
whenever components were reworked and re- use because of the presence of a crack/flow
tested, the components passed the rig test line found on the shroud flange. All the SN-54
without damage. turbine shrouds from NGK and SN 250M tur-
268
bine shroudsfrom Kyocera passedthe mechan- S I
ical screeningtest.
I FAILED
A variation of this rig was used in April
1987 for a series of tests to assessthe struc- PASSED
6m
tural integrity of the lower contact washersin
the rocker assembly. Washers supplied by
NGK (SN-54) and Kyocera (SN 220M) were
tested to load up to 1814 kg (4000Ibs) through E
rocker supports.
269
was intended only as an interim test until the Initial testing of inner and outer diffusers
more refined thermal screening rigs became resulted in fractured components starting
available. from the bolt holes in the inner diffuser and
bolt slots in the outer diffuser. Progressive
Some of the stator vanes from both ACC design changes were made in conjunction with
and Standard Oil survived the worst case start analysis to increase test success. Design
simulation. Those made out of RBSN tended changes on the outer diffuser included scal-
to fail at processing defects that were de- loping the outer ring, slotting from the inner
tected by radiography, others failed at the to outer diameter, and finally eliminating all
mold line at the radius between the trailing of the outer rim and bolt slots by piloting off
edge and the platform. The SASC stators the inside of the rocker assembly (Figure 328).
tended to fail at the radius between the trail- Likewise with the inner diffuser, slotting from
ing edge and the platform. Those stators that the inner to outer diameter, removing the
survived the thermal shock test gave reassur- outer rim and changing to bolt slots, was tried
ance to the adequacy of the existing stator before the final change was made to truncate
design. the outer diameter to below the rocker assem-
INTERMEDIATE
SHAPE- SLOTTED
ORIGINAL
SHAPE
UNSCALLOPED SCALLOPED
INTERMESMTE
SHAPE
FINALSHAPE- TRUNCATEO
270
Y.O01{ QUALITY
bly, thereby eliminating the bolt slots in the ability, laser marking of all ceramic compo _
component (Figure 329). The initial goal was nents was also initiated. No deterimental
to screen a few components for application in effects from the marking were noted (see also
the static structure rig before a rigorous test paragraph 6.1.5).
cycle was used to proof components for
normal engine use. These components were
The test history for the other screening
qualified and on February 5, 1985 proof testing
rigs also proceeded on a similar and concur-
was initiated. To insure component trace-
rent path, whereby early testing took place in
conjunction with analysis to optimize the com-
ponent design. Numerous design evaluations
were made with the transition duct/combustor
baffle thermal screening rig. Design evalua-
tions on the transition duct centered around
the design of the standoff for the combustor
baffle struts and the T 4 thermocouple holes.
The primary justification for the final design
choice was based on manufacturability and
functionality since, except for one design
choice, no degradation in test results was
evident for any choice. Degradation in com-
ponent strength was noted in testing of two
ORiGiNAL SHAPE (RAO}AL SECTiONI
components with thermocouple bosses brazed
-- WiTH SLOT to the transition duct. The braze material was
-- WfTROUT RAOIAL SLOT
271
o
Initial design activity on the turbine shroud data base evolved that allowed for compara-
focused on the effect of wall thickness. When tive evaluation of the performance of various
poor results were obtained for both the thin or ceramic materials in a simulated engine envi-
regular wall thickness components, a com- ronment. Figure 331 shows the test results for
pletely new design concept study was initi- RBSN (AiResearch Casting Company, SN-54
ated. The outcome of that analytical study (NGK-Locke), SASC (Standard Oil) and
was the varied wall thickness turbine shroud SN-250M (Kyocera) materials used on the
design which would provide for a more uniform AGT101 engine components. Both SN-54 and
thermal response (Figure 330). Initial testing SN-250M showed better consistency, although
their data base was somewhat smaller. SASC
showed better success with the combustor
baffle application than with the transition
duct, perhaps, because of fewer stress concen-
trations in the combustor baffle design. RBSN
tended to do better on components aft of the
stator, when combustor pattern factors are
less pronounced.
NORMAL ENGINE
START 1371C 12500F1
Static structures rig testing was initiated
in July 1982, with primary intent to simulate
At DESIGN 83 DESIGN
173.7 MPa i25,,2 KSII 111.7 MPa (16,.2 KSII steady-state engine idle conditions at a 871C
(1600F) T4.1. The initial build suffered the
N74171_77
fracture of an outer diffuser along a radial
line. Thereafter, the rig was rebuilt sub-
Figure 330. Turbine Shroud Design stituting an updated outer diffuser design,
Evolution. containing a radial stress relief slot (reference
paragrapha 6.3.1.2). Another (partial) tear-
of this design was not encouraging due to the down and rebuild ensued, this time due to a
presence of a large stress concentration at the suspicious acoustic event, before the rig was
seal land radius that was not detected in the successfully run (as Build 03) of the metallic
analysis. Subsequent testing of this design was engine. This successful series was run at
made successful by a combination of a larger turbine inlet temperature of 871C (1600F) at
seal land radius, a better control of the finish airflow rates of 75.6 and 113.4 g/sec (i0 and
within the seal land radius, and improved ma- 15 Ib/min), to simulate engine test bed idle
terial properties. and cruise flow conditions. A total of 15 start
and shutdown thermal transient cycles were
An attempt was made to improve the mar- completed, with an average start transient
ginal capability of the original design by r_a- time of 120 seconds. In addition, shorter
chining a full radius cutback in the stator vane thermal start transients were run in the range
trailing edge. An apparent improvement in of 15 to 25 seconds to 871C (1600F) demon-
strength was noticed in testing. All sub- strating the capability of the ceramic static
sequent stators were made with the cutback structural components to withstand current
trailing edge. Three integral stator assemblies metallic engine test bed start transients.
from Ford were also tested and all resulted in
failures. At test completion, the rig was disas-
sembled and none of the 49 ceramic compon-
As the component designs became finalized ents were damaged. Also, no areas of inter-
face deterioration were detected.
along with the proof cycle requirements, a
272
687-078-354
273
Subsequent builds again encountered set- dimensions of 38.1 microns (0.0015 inches)
backs. In one case, an experiment with a total-indicated-reading (TIR) through the
fibrous seal between the turbine shroud, tran- cyclic testing of Build 08.
sition duct, and flow separator housing gave
unfavorable leakages when compared with the Rig Build 09 incorporated a completely
ceramic seal rings they replaced. In another new set of ceramic hardware and was con-
case, instability of the rig combustor due to ducted to the same test cycle as Build 08. At
the inadequate control of the pressure drop two minutes into the second cycle the acousti-
across it resulted in a typical heating of the cal emission monitor picked up a continuous
ceramic components and consequent fracture. high energy output from a rocker assembly
In still,another case, a stack calculation error sensor. Due to high energy indications, the
resulted in a "thermal jack", or interference test was terminated and the rig disassembled.
between parts as they grew at differing ther-
mal expansion rates during the course of test- Upon disassembly, component inspection
ing, and thus catastrophic failure of several revealed a fractured turbine shroud and a chip
ceramic components. And in the subsequent from the outer diameter of the outer diffuser.
build (Build 07) a radius mismatch between the The turbine shroud fractured at a surface
regenerator shield and the mating pocket or defect approximately 3.18 mm (0.125 inch) in
platform in the flow separator housing was the depth. In addition the outer diffuser housing
cause for failure of the flow separator housing stackup was loose due to apparent sticking at
during assembly. the number two and three bolt locations. It is
believed that the vibratory energy from the
The replacement flow separator housing outer diffuser to the turbine shroud driven by
for Build 08 had a fillet smaller than the the recirculating flow behind the outer dif-
corner radii in the mating regenerator shield. fuser, contained sufficient energy to propa-
In August 1983 a complete set of ceramic gate the existing surface defect and chip the
structures was tested to a cycle 25 percent outer diffuser. To preclude the potential for
more severe than the cycle defined for the this problem to reoccur, the spring load across
first set of I149C (2100F) engine testing with the inner and outer diffuser stackup was in-
ceramic cod_ponents. Seven cycles were com- creased from 9.5 kg (21 Ibs) to 36.3 kg (80 Ibs).
pleted. On the lightoff for the eighth cycle
rig testing was terminated due to excessive The rig was reassembled with a replace-
high-to-low pressure internal leakage. The rig ment turbine shroud as Build 10 and run to the
was disassembled and inspected for component same cycles as with Builds 08 and 09.
damage.
At 19 minutes, 20 seconds into the first
Minor chipping was noted on the following transient cycle (1093C) a 91 db event was
components: combustor baffle strut, eccent- recorded on the flow separator housing acous-
ric spacers, flow separator housing ID seal tic emission monitor. The count rate for the
ring, and T4.1 (TIT) thermocouple load spa- event (approximately 450 counts) indicated a
cers. None of the noted chipping was a result probability of fracture. However, no changes
of material interface sticking. The excessive were noted in rig HP or LP inlet pressures, and
leakage that terminated the test was due to there was no fluctuation in regenerator drive
the collapsed diaphragms on the regenerator torque following the event, therefore, the test
inner seal as a result of overheating. was continued. After the successful comple-
tion of ten cycles the rig was disassembled.
Turbine shroud alignment is of paramount
importance in maintaining proper turbine rotor At disassembly it was noted that the inner
running clearance within close tolerances. diffuser and the flow separator housing had
The ceramic rocker/eccentric assembly suc- fractured. It is believed that the flow separa-
cessfully maintained cold assembly runout tor housing fractured at the time indicated by
274
the acoustic monitor and was caused by a stress in the above listed components. The
radial interference between the flow separator shock wave created by the strain release in
housing and the ring support housing. Inade- the backshroud at fracture is believed to have
quate diametral clearance between the insula- caused the failure in the interfacing compon-
tion preform (in its coated and hardened con- ents.
dition) and the inner diffuser has been deter-
mined to be the primary causeof the fracture The solution to the rig failure was two-
of the inner diffuser. The anti-erosion coating fold. First, the turbine backshroud was par-
on the insulation preform is applied by brush, tially stress-relieved by redesigning, and ma-
and so coating thickness is difficult to control. chining a 3-inch diameter hole through the
Also, the insulation material is subject to center of the component. The void area was
shrinkage in use, another obstacle in control- then filled with Lockheed HTP-12 insulation.
ling its geometry. The 3-inch diameter hole removes the current
peak stress area of the component, effectively
The objective for Builds 11 through 13 was lowering the maximum principal stress by 88-
to subject the ceramic static structure com- percent. Secondly, an improved fuel metering
ponents to a start 25 percent more severethan system was installed to preclude burner/con-
the development engine start, which would be trol instability, thereby minimizing the proba-
equivalent to the normal engine start. The bility of a rig induced failure.
initial test for Build 11 utilized the two flow
path rig configuration used on all previous In September 1984 another set of static
static structure rig test. A three inch labora- structure rig components was assembled as
tory burner is located in-line of the low pres- Build 12 and run with the same test objectives
sure air supply. This burner had never been as for Build 11.
usedat the higher massflows required for this
start cycle and was unable to maintain the Five cycles to 982C (1800F) were accum-
proper burner control to achieve the desired ulated, after which the rig was removed from
lightoff. The rig was consequently recon- the test cell and disassembled. All major
figured to include the engine combustor by ceramic components were intact; only a few
using a single flow configuration as in the minor discrepancies were observed. These
included chips on two of the three spacers
engine.
separating the inner and outer diffusers; two
A successful lightoff was achieved with the very small chips on the inner diffuser, and a
new rig configuration but was terminated prior small chip due to contact stress on the flow
to achieving the desired maximum tempera- separator housing seal ring. Successful com-
ture of 982C (1800F). The test was termi- pletion of this test represented the first time
nated due to the occurrence of coupled acous- that a full set of ceramic static structure
tical emissions from the two probes and a components were proof tested to such severe
simultaneous drop in rig inlet pressure. Disas- thermal shock conditions.
275
tion. The high level AE indications may be 1149C (2100F) and 1260C (2300F) respectively.
attributed to the insulation breaking up, or The third cycle reached 1371C (2500F). After
perhaps to the effect of a too rigidly mounted 3.5 minutes at 1371C (2500F) a high acoustical
AE probe sweeping a surface as the rig ex- emission event occurred.
pands and contracts. The test was considered
completed. Disassembly revealed fractures to the tur-
After Build 13 confidence had reached a bine shroud and the integral stator ring. The
stator failure was secondary to the turbine
level that a check screen of the entire ceram-
shroud fracture. The most likely explanation
ic structural assembly was no longer felt nec-
of the fracture was that the pressure differ-
essary as long as components were still quali- ence across the stators created a force suf-
fied on smaller subassemblythermal and me-
ficient to counteract the spring load holding
chanical screening rigs. The static structure
the ceramic stack together. Thus, the as-
rig was therefore modified and used as a hot
sembly was sensitive to any fluctuations in
regenerator seal leakage test rig. pressure. Initiation of fracture was at the
6.3.3.4 1371C (2500F) Static Rig Testing turbine shroud seal land outer diameter (CO)
where contact was made with the transition
This section covers the high temperature
duct. Prior to further testing the rig under-
testing of ceramics to investigate effects such
went modifications to the axial spring loading
as static fatigue, contact loading, sticking,
mechanism.
and endurance. Testing was conducted in
three different rigs throughout the duration of
In mid-May, 1984 another set of ceramic
the program before a specific rig for high
components was assembled in the modified rig
temperature testing was finalized.
and tested to a maximum temperature of
The initial testing was done in the back- 1371C (2500F) according a cycle similar to
shroud/stators/turbine shroud screening rig that used for the previous test. Although
with improved insulation in mid-April, 1984. acoustical emissions indicated a high energy
The objective was to subject the ceramic output after shutdown, rig teardown revealed
transition duct, combustor baffle, turbine all components intact, with the exception of a
backshroud, stator assembly, and turbine spalled wave spring. Wave spring spalling had
shroud to the high temperature cycle defined been traced to the quality of the powder used
in Table 52. The first two cycles only reached in the manufacture.
Table 52. Test Cycle for Initial The design of the backshroud/stator/shroud
1371C (2500F)Testing in the screening rig limited the 1371C (2500F) test-
Stator/Shroud Screening Rig. ing to short term exposure. The hot static rig
was designed for long term exposure of elev-
Time, Temperature
min, C (F) ated temperatures to the ceramic components.
The original configuration for this rig had the
t 6 649 (120Oi flow path of the incoming air different from
4 815 (1500) the flowpath of previous screening rigs in that
4 982 (1800) the incoming air enters via a ceramic flow
4 1149 (2100) separator housing prior to combustion in the
4 1260 (2300) rig burner. Goals for this initial test were to
4 1371 (2500) establish proper rig setup in the test cell,
5 rampdown to 649 (1200) verify rig build procedure and operation, and
4 649 (1200) achieve a 1371C (2500F) temperature. The
Shutdown intended maximum temperature of 1371C
(2500F) was not achieved because of com-
*Light-off to 649C (1200F) in 15 second_ ponent failures during start. Rig disassembly
15 second ramps I revealed a failed turbine shroud, integral
276
stator assembly, seal assembly. The most high stress levels normally would not occur.
likely cause for the fracture was contact load- Also, several stators were noted to have stuck
ing near the fillet area of the shroud where it to the turbine shroud. This phenomenon was
mated with the flow separator housing seal analyzed and it is felt that the sticking was
ring. due to metallic deposits emanating from the
metal-sheathed thermocouples employed in
Further testing at 1371C (2500F) was con- the rig.
ducted in October 1984 using the backshroud/
stator/shroud screening rig as a test bed in In April 1985, further 1371C (2500F) test-
lieu of the previous hot static rig. The ceram- ing was conducted, this time employing a new
ic hardware in the backshroud/stator/screen- rig design similar in configuration to the back-
ing rig Build 06 was subjected to 30 minutes of shroud/stator/shroud screening rig, but orien-
operation at 1371C (2500F) and 75.6 g/sec (I0 ted in a vertical position. This was done for
Ib/min) airflow. No fractures occurred during two reasons: 1) to allow a dead weight to
the operation. supply the required load to the ceramic stack,
and 2) to preclude the possibility that dis-
Two significant observations were made charge quench water would back up into the
during rig disassembly. Insulation which sup- rig. This rig would be used for all subsequent
ports the turbine shroud and the rest of the 1371C (2500F) testing. This rig's first test was
ceramic hardware, consisting of a silicon diox- identified as the 1371C (2500F) static rig
ide insulation with an alumina based rigidizer, Build 01.
yielded during the test, allowing the parts to
drift axially by approximately 1.3 to 2.5 mm The dead weight employed was made of
(0.050 to 0.i00 inch). The insulation also stuck 300 Series stainless steel, insulated for protec-
to the turbine shroud when the latter was tion. Unfortunately, it reached a high enough
removed from the rig. Further, examination temperature at approximately 25 minutes
under magnification on the three struts on the after achieving the 1371C (2500F) test tem-
combustor baffle and the mating areas of the perature that premature shutdown of the rig
transition duct revealed glazing in these areas, was thought prudent. Upon disassembly four
although no component sticking was observed RBSN stators were found lightly stuck to the
(the parts were freely disassembled). Success- RBSN turbine shroud and the LAS spacer ring
ful completion of this test represented the melted. The melting of the LAS spacer ring
first time that these components had been was believed to be caused by a combination of
exposed over a long period (30 minutes plus) to a hot spot in the flame and leakage through
1371C (2500F) temperatures. the seal assembly.
A subsequent attempt to repeat the test, Build 02 incorporated an RBSN spacer ring
(backshroud/stator/shroud screening rig, Build and a stator assembly consisting of both RBSN
07), but substituting a turbine shroud of RBSN and SASC stator segments. To extend the
for the SSN turbine shroud, was aborted ap- running time at the 1371C (2500F) tempera-
proximately 5 minutes after reaching the ture, the dead weight system was changed to
1371C (2500F) temperature. The rig was shut incorporate ceramics. However, the amount
down after a shift in the stack of the ceramic of weight that could be physically installed in
parts was noted. Subsequent disassembly re- the rig envelope was found insufficient. A
vealed that this was due to relaxation of the pressure differential, at the test light-off,
insulation, as had previously occurred. Unfor- between the flow path and the cavity sur-
tunately, quench water used to cool the dis- rounding the test pieces caused the transition
charge ducting backed up into the rig, passed a duct to move upward (axially) and then bounce
dam intended to contain it, and as a result the back down upon the rest of the stack of parts.
turbine shroud and backshroud both were frac- Because of this failure no test time at 1371C
tured. The fractures originated in areas where (2500F) was accumulated for this build.
277
Rig modifications to allow for 1371C this test the coating was not satisfactorily
(2500F) testing were completed in early July evaluated due to failure of the turbine shroud.
1985. An external spring loading mechanism This was caused by inadequate clearance be-
was used to provide the axial force to contain tween the SASC turbine shroud and the RBSN
the ceramic components. This rig configura- transition duct to allow for the differential
tion was tested for the first time in late July thermal growths.
1985 (Build 03) and was successfully operated
at 1371C (2500F) for 2 hours. Stators made of The test objective for Build 08 was to
silicon carbide (SIC) and reaction-bonded sili- evaluate SN 250M material in an assembly
con nitride (RBSN) were alternately used to with SASC material. After 13 hours of testing
evaluate interracial sticking. Teardown in- at 2500F three pairs of SN 250M stator seg-
spection of the rig revealed glass formation, ments were found stuck to each other but not
primarily on the stator and baffle feet sur- at the stator to shroud interface. In addition,
faces; however, there was no evidence of a glassy deposit was found at the center
sticking. portion of the SASC turbine backshroud.
The next build (Build 04) incorporated an Build 09 consisted of a complete set of
all RBSN stator set and RBSN turbine shroud ceramic components made out of SN 250M.
to evaluate interfacial sticking at the shroud/ The rig was run for 14 hours at 1371C (2500F)
stator interface. No results were obtained. A and similar results to build 08 test were found
light-off was attempted using an off-the-shelf on disassembly. The glassy deposit was again
automatic control system. Thermocouple re- found on the center portion of the backshroud,
sponse in this rig (the thermocouples are but this time the backshroud was made out of
shielded in a ceramic sheath) was too slow for SN 250M. This would seem to indicate that
adequate control, and as a result ceramic the glassy deposit was not reacted from the
fracture ensued. backshroud surface. Two pairs of stator seg-
ments were also found stuck to each other and
Builds 05 and 06 each accomplished 12 one stator stuck to the turbine shroud.
hours at 1371C (2500F). Build 05 showed
sticking at the stator/turbine shroud and sta- To date, limited sticking at 1371C (2500F)
tor/stator interfaces. No damage was seen at has been seen. No failure has occurred due to
either interface. Previous builds had showed sticking. Interracial distress seen between the
the transition duct/baffle interface to be a transition duct and combustor baffle can be
problem when using the same material for eliminated by using an alternating material
both parts. This problem can be eliminated by stack in this area. More time at temperature
using an SASC transition duct/RBSN baffle is needed before drawing any conclusions
combination. about possible detrimental effects of the
stator/stator and stator/shroud sticking that
Build 06 showed no sticking. Unlike the was seen.
RBSN stators in Build 05, the SASC stators did
not stick to either the turbine shroud or to 6.3.3.5 Ceramic Seals Testin_
each other. As in Build 05, alternating mate-
rials at the transition duct/baffle interface Performance measurements made during
eliminated problems encountered in earlier engine testing of the ceramic-structured and
builds. all ceramic engines indicated power output
was below design calculations. Excessive
The test objective of stator rig Build 07 leakage through the ceramic sealing areas was
was to determine the effectiveness of A1203 suspected as a primary reason for the lack of
Sol-Gel coating on SASC parts to prevent power. The three sealing areas of interest
sticking. Preliminary results using test bars included the turbine shroud/flow separator
have shown this to be an effective coating. In piston ring seal, the regenerator shield/flow
278
separator housing butt joint seal, and the shroud piston ring seal solid stack arrangement
regenerator shield/exhaust housingpiston ring in the turbine shroud seal pocket. The spring
seal. These seal areas are shown in Figure load was transferred from the turbine shroud
332. In order to isolate and measure leakage stack to the baffle/backshroud/stator stack by
through these areas, three cold static seal rigs inserting a 17.8 cm (7-inch) ceramic wave-
were designed and fabricated. Each of the spring between the baffle and backshroud. Rig
rigs madeextensive use of engine hardware in measurements of the new configuration
order to simplify fabrication. By measuring showed a 50-percent reduction in leakage over
cold seal leakage, the rigs were able to gen- the single LAS configuration as shown in Fig-
erate performance data for new seal designs ure 336.
which could be compared to performance of
existing configurations. The rigs were also Leakage testing with the single LAS seal
successful ]n measuring the effects of seal configuration was done to determine the ef-
loading, concentricity between sealed parts, fects of axial load on the seal performance.
and effects of pressure distortion on seal per- Seal loading was varied from 2.27 to 25 kg (5
formance. to 55 Ibs) over the range of engine pressures.
REGENERATORSHIELD/ TURBINE SHROUD/ As shown in Figure 337 there was no signifi-
FLOW SEPARATORHOUSING FLOW SEPARATOR cant benefit from increased loading.
BUTT JOINT SEAL / PISTON RiNG SEAL
REGEHEBATOR
SH, LO/ / / Single LAS seal testing also indicated that
EXHAUST HOUSING PISTON __ _::_ ./__ /
eccentricity between the turbine shroud and
flow separator has a significant effect on seal
performance. This increased leakage up to 25
percent in a position of 1.52 mm (0.06 inch)
eccentricity over the concentric position.
279
PA3612096-1
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GD7_7_271 MS9491-24 P
280
LP
OUAL FLOW SEPARATORSEALS WITH
HP
TURBINE SNROUOSEAL
RP
LP
S SEAL RING
229 CM [9 INCHI
TURBINE 'SHROUO 17.8 CM (7 INCHI
TURBINE DACKSHROUO OUAL SEAL RINGS
WAVESPRING
RP
\
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2.
l' I
UT@TS-_Z
Figure 334. Single LAS Flow Separator Figure 335. Dual LAS Flow Separator
Seal Configuration. Seal Configuration.
allows for thermal growth of the regenerator activated. Optimum axial load was less than
shield and uses pressure to conform the seal to 2.27 kg (5 pounds). A typical seal leakage
the surface of the shield. Testing showed that curve is shown in Figure 339. Further seal
seal performance needs improvement at lower testing will focus on methods of improving this
pressures where the seal is not pressure- seal's low pressure performance.
281
[LD/MINI
20-
KG/MIN
0._" O ; SINGLE
= OUAL
0,5"
,,t
IPSIGI
O- e
i ! _ I ! f !
54
8 IR 24 32 40 48 56
MPI
,:,, & ,'-.. 2_o & & &
RIG PRESSURE
eJt4;l_74
KB/MINI
I
KG/MIN
0,75,
1.8-
025-
0,4"
O- 0 , . , , , , . ,PS,_.,
O IR 24 32 40 48 56
I I I I I a MPa
129 lIK) 240 300 360
RIG PRESSURE
282
(,_JGL_AL PAGE [S
OF. POOR QUALITY_
U7_T&2'Tfl
283
ILB/MIN
1.0-
KG/MIN
LEAKAGE
AS A FUNCTION
0.375" OFENGINEFLOW,PERCENT
0.8--
I -- 3.1
2 -- 2.0
3 -- 1.2
0`§ :; I:I e/
0`25-
6 -- K1
0.4" 2
0.125.
0.2 "
O,
I I I I I ! I I IPSIGI
0 8 16 24 32 40 49 56
; I I I I I I MPa
60 120 I DO 240 300 360 420
RIGPRESSURE
G87-0;6-277
Figure 339. Regenerator Shield Seal Leakage over Operating Pressure Range.
284
APPENDIX A
The following section describes the pro- In 1983, a new composition (92 percent
gress made in developing the standard process- GTE SN502 + 6 percent Y203 + 2 percent
ing procedures using GTE SNS02 powder, the A120 3) was introduced. This composition,
material properties of the rotors, and the designated as Code 2, was developed in an
more recent efforts of developing alternate AMMRC contract "Low Cost, New Shape
materials and processing procedures. Ceramic Radial Turbine Program" (Contract
285
No. DAAG46-81-C-0006). Because of the 2.3 Mold Fabrication and Casting Procedure
lower Y203 and Al20 3 contents, this new Developments
composition was believed to have superior high
temperature properties. Optimization experi- Net shape casting of a bladed rotor re-
ments were then conducted to establish a quires an organic shell mold with the correct"
procedure to achieve desirable slip properties. configuration, dimensions, and a defect free
The procedure produced well dispersed slip inner surface. A procedure was developed to
with consistent properties when materials fabricate such a mold from either a rubber
were taken from the same lot of GTE SN502. pattern or a water soluble wax pattern. The
development effort was primarily performed
using rubber patterns. This development was
A series of slips was tested using the
aided by the expertise that exists in the Wax
Haake viscometer at 25C, with the CVl00
Department at ACC.
measuring drive, and the AZ30 measuring sys-
tem. Yield points of the slips were then Several shell mold materials were evalu-
determined on the shear stress versus shear
ated with varying degrees of success. A
strain rate curves. Table 53 seems to indicate
paraffin based material, optimized for wax
a correlation between yield point and gelling.
patterns, was initiallyused for mold fabrica-
This investigation led to the use of the Haake
tion with rubber patterns. The paraffin based
viscometer to control the quality of the slip
material was opaque and did not coat the
prior to casting. blade edges well. Ethyl cellulose and butyrate
based dip seal materials provided transparent
Table 53. Yield Point of Slip and
molds helpful in obtaining complete filland
Quality of Casting.
excellent edge coating but were not dimen-
sionally reproducible. Subsequently a trans-
lucent mold material (LN 209-218) was
Slip Yield
developed, similar to the original material,
ID Point,
with improved edge coating capability.
No. Test Date Pa Remarks
286
O-Rb_tN_AL PAGff, I_
OF POOR QUALITy
these problems, a screening and de-airing of The as-cast rotor often exhibited cracks on
the slip immediately before casting was incor- the dome because of a fast casting rate in the
porated. dome area where the slip is in direct contact
with the plaster mold. This cracking problem
In addition, a pouring device was developed
was eliminated by soaking the piaster mold in
whereby slip is withdrawn from the bottom of
water prior to use.
the container. This was to eliminate the
contamination from the foaming foreign sub-
2.4 Drying and Pre-Sintering Developments
stance which always appears on the skin layer
of the slip and produced defects in the initial Cracks often developed during drying of a
experimental castings. ceramic part. This is particularly true for
Incomplete fill near the upper blade tips large size rotors with varying thicknesses.
was one of the major problems when bladed Improper drying also would result in cracking
rotor casting efforts were first introduced. To during pre-sintering or sintering. At the
overcome this problem a procedure to spin the beginning of this program even the bladeless
mold during slip pouring was incorporated. simulated rotors cracked consistently. Figures
Another improvement in casting procedure 340 and 341 show two examples. Conse-
was the control of pouring rate by using a quently, a major effort was devoted to solving
separatory funnel. this problem.
Figure 340. Cracked Dome On a Figure 341. Part After Sintering Cracked
Bladeless Rotor Casting After Into Several Pieces Due to Incomplete
Drying. Drying.
287
The initial experiments included the use of Iniection Molding
a desiccant to absorb moisture from the part
and oven drying at 150F as the final step in
A Tempcraft plunger type injection molder
the drying procedure.
was used in this effort. A large number of
This procedure was not successful even silicon nitride simulated rotors were injected
with the simulated rotors. Another experi- to eyaluate the wide variety of molder adjust-
ment involved drying the part at room temper- ments. These included variations in injection
ature for one day followed by vacuum drying pressure, tool clamp pressure, flow control,
for three days. Again the parts cracked into barrels and nozzle temperature, injection and
several pieces. Additional experimental trials cooling time. In spite of the wide choice of
included drying the parts in a plastic box, with parameter variations, a problem of air entrap-
or without venting holes for a period of up to ment within the rotor persisted.
several weeks and the use of manually con-
trolled humidity oven. This was then followed
It was decided to modify the simulated
by oven drying at 90F. None of these experi-
rotor tool configuration. Originally, the base
ments showed any significant improvements.
portion of the tool was made in two halves in
The major breakthrough occurred when a order to permit future simulated vanes at the
programmable humidity oven was introduced. vertical parting lines. However, it was found
This humidity oven enabled more systematic that the tool could not be clamped with suf-
control of the drying environment. A success- ficient pressure to resist flashing. This caused
ful cycle for the rotor was developed. The release of injection pressure resulting in poor
cycle starts at a high humidity (80 percent surface and incomplete mold fill. A new one-
relative) and low temperature (77F) and ends piece base section was built which eliminated
with a low humidity (20 percent relative) and the flashing problem and improved surface
high temperature (185F). Final drying is cosmetics but did not eliminate air entrap-
accomplished in an air oven due to the tem- ment.
perature limitation of the humidity oven. This
drying cycle shortened the previously un-
The next tool modification designed to
successful long cycle to 9 days and produces
solve the problem of entrapped air was to
consistently crack-free bladed rotors.
provide the capability to evacuate the cavity
Prior to the demonstration of ACCts prior to injection. It was found that the
sinter/HIP capability, dried castings were vacuum had to be turned off simultaneously
shipped to Ford or ASEA for densification. To with material injection or the material would
avoid shipping damages, a pre-sintering cycle flow into the vacuum system requiring ex-
was developed. This sintering cycle was to tensive clean-up. However, even with the
impart sufficient strength to the rotor without ability to evacuate the mold cavity, air within
causing cracking or noticeable sintering. The the injection molder barrel enters the mold
cycle was successfully established with the with the batch material when injected.
100 psi furnace. This pre-sintering cycle has
beome a standard procedure prior to sintering
Originally, the entrapped air in injection
even for rotors sinter/HIP'ped at ACC.
molded simulated rotors was assumed to be
the major reason for the inability to produce a
2.5 Configuration Evolution
O satisfactory rotor. In an effort to determine
Rotor efforts at ACC were initially the actual material flowpath during injection,
directed toward fabrication of both injection a clear plastic was substituted for the Si3N 4.
molded and slip cast rotors, a simulated rotor The material flowed from the backface (where
configuration (bladeless rotor) was used in it entered the tool), moved along the tool wall,
both approaches before a bladed rotor config- and on into the shaft end and sealed off the air
uration was introduced. trapped in the center.
288
As a result of this experiment, muchof the Another modification affected blade thick-
problem encountered with voids in the injec- ness at the saddle area, blade to hub filled
tion molded rotors was traced to the fact that radius, transition changes at the saddle area
the rotor was not cooled sufficiently within between the blades and a belled saddle to hub
the tool to solidify the binder bef6re holding line radius definition. This modified design
pressure was lost. Pressure time was thus was named the "B" generation. Another dif-
increasedfrom 6 minutes to 30 minutes. When ference between the "A" & "B" generation is
the resulting rotor was split open, it was solid the "A" generation utilizes reusable rubber
throughout, showing no evidence of voids. patterns while the "B" generation uses injec-
Subsequently more rotors were injected that tion molded water-soluble wax patterns.
did not have any flaws as determined by visual
inspection and X-ray radiography. However, 2.6 Densifieation Process Development
cracks developed in the rotor in the initial
binder removal experiments. Prior to 1983, the only high temperature
furnace available to this program for densi-
To solve the binder removal problem, many
fication of slip cast parts was the i00 psi N 2
studies were conducted. Initially, a study was furnace at ACC. Many cycles were experi-
performed to determine whether rotor hub mented with in this furnace using Code I
size is a critical factor. For this evaluation, composition test plates as well as rotors. The
crack-free molded bladeless rotors were
theoretical density of Code 1 is 3.30 g/cm 3
reduced in size by lathe turning and evaluated (based on the rule of mixtures). Typically the
in the vacuum dewax cycle. Again, dewax test plates achieved densities in the range of
cycles resulted in rotor cracking, indicating 3.18-3.22 g/cm 3, while the rotors could only
that rotor size was not a major controlling achieve 2.78-3.04 g/cm 3. Parameters investi-
variable.
gated included soak temperature and time,
Additional experiments using various heating rate, furnace load, and kiln furniture
thermal cycles in a nitrogen atmosphereat I0- history. In addition to the sample densities
12 psig pressure were tried, but results were (plate versus rotor) effect noted above, it was
inconclusive. The injection molding approach found that kiln furnitures previously exposed
wasdiscontinued in 1981. to an oxidizing environment had a detrimental
effect on densification. It was also found that
Slip Casting "samples with lower weight loss exhibited high
strength at room temperature.
The very first castings were made using
the bladeless rotor or simulated rotor con- Due to the low densities obtained at ACC
figuration. The first casting was made in a using the 100 psi furnace, an arrangement was
metal mold with a plaster base. In subsequent made to densify rotors at Ford and ASEA.
castings, the metal mold was replaced by Ford has a 1500 psi furnace and ASEA has
plaster and then by rubber. glass frit encapsulation plus HIP'ping tech-
nology. Initially Code 1 rotors could be densi-
Bladed rotors were fabricated using rubber
fled only to 3.20 g/cm 3 at Ford. As a result of
patterns based on an actual metal rotor until a
continued materials/process development at
metal pattern with allowance for 14.5 percent
ACC and cooperative efforts at Ford, bladed
sintering shrinkage was obtained. Scale-up
rotors were sintered to 3.27 g/cm 3 in Novem-
was successful. All castings, by November
ber 1982 and further increased to 3.30 g/cm 3
1981, were aimed at producing parts with the
in October 1984. Similar densities were also
14.5 percent shrinkage. obtained in rotors densified at ASEA. In June
Mold design changes were made in 1985. 1983, ACC had demonstrated a capability to
The present rubber pattern was changed from sinter/HIP bladed rotors to 3.26 g/cm 3 (Code 1
14-5 percent (AI generation) to 17.0 percent and Code 2). The Code 2 composition has a
(A2 generation) shrinkage allowance. theoretical density of 3.26 g/cm _. In 1984 the
289
densification processes at ACC, Ford and One of the original slip-cast mold config-
ASEA all could densify rotors to densities urations consisted of a plaster base that con-
higher than 98.8 percent of theoretical. As a tained the backface shape and an all-rubber,
result of the good ACC sinter/HIP densifica- tw.o-piece mold for the hub and shaft. An
tion results, shipments of rotors to Ford and iteration designed to reduce the length of
ASEA were discontinued. casting time involved changing the all rubber
portion of the mold to one-half rubber and
2.7 Alternate Raw Materials Development one-half plaster. Several rotors were cast in
this dual-material mold, but the portion of the
Limited availability, inconsistency in
casting in contact with the rubber face ex-
quality, and the higher cost of GTE SN502 hibited what could be classified as an out-
Si3N 4 powder have been the impetus for the gassing condition with extensive surface
search for alternate sources of Si3N 4. Various
porosity. A thin wax coating was applied to
silicon nitrides were investigated as potential
the rubber face portion of the mold, which
replacements for GTE Si3N 4. Some of the
improved the condition only marginally. The
results are described in the following para-
casting surface in contact with the plaster was
graphs. excellent.
Denka 9S Si3N 4 was milled with additives, Another mold was prepared that was en-
prepared as slip and cast into rotors. Sintered
tirely plaster. The shaft portion was coated to
rotors yielded final densities of 3.23 to 3.26
render it non-absorbent in order to prevent
g/cm 3. However, more optimization experi-
preliminary casting in this area inasmuch as
ments are required before a stable and con-
slip is poured through the shaft end of the
sistent slip can be routinely prepared.
mold. The casting appeared to be free of
UBE SN E02 and SN E05 Si3N 4 were evalu- flaws both visually and by X-ray radiography.
ated as a replacement for GTE. 100 percent The above two experiments were conducted in
SN E02, 100 percent SN E05 and blends of E02 1981 on simulated rotors.
and E05 (25-75, 50-50, and 75-25, percent by
An all plaster mold using plaster inserts
weight) all exhibited lower viscosities and
between the blades was tried. For the purpose
faster casting rates than baseline castings.
of initial evaluation, the plaster inserts were
However, all developed cracks prior to
made individually without proper tooling.
sintering. Most blades were damaged while the inserts
were being removed. It suggested that pre-
Starck H-2 Si3N 4 showed little dis-
coloration on rotor blades but was difficult to cisely fabricated piaster inserts and a con-
make into a consistent slip. A new procedure trolled plaster insert removal mechanism
was recommended by Allied Central Lab. This should be developed before the potential of
this technique could be truly evaluated.
involved preparing the slips of Starck Si3N 4
and the premilled additives (Y203 and AI20 3) An inverted wax shell mold, to form the
separately and then blending them together blades, hub, and shaft was attached to a
after adjusting them to a common pH. How-
plaster base. A wax pattern dome with a
ever, slips continued to be very viscous. No
funnel at the top center was welded to the
improvement in slip viscosity occurred after
upper wax shell that formed the blades (1981).
pH adjustments and lower solids content.
This technique resulted in visually crack free
rotors but it required a much longer casting
2.8 Alternate Casting Procedures
time. In addition, it was difficult to form a
Investigated
precise dome contour. The wax dome in the
Long casting time, poor casting surface above arrangement was replaced by a plaster
quality, incomplete fill and discoloration plate with the dome contour. The slip was fed
problem were addressed by trying a variety of in both from the top and bottom, in separate
alternate casting techniques or mold designs. experiments; all castings were cracked (1985).
290
Evacuation through the plaster mold base I) Analysis
was aimed at reducing casting time, especially
Many organizations have been contributing
for the B generation rotor configuration. This to this effort. Table 54 summarizes the
approach was discontinued due to the lack of results.
proper equipment.
o Garrett - SEM/EDX t 1982
Hydrostatic pressure casting was accom- Green as well as sintered blades were
plished by placing a just poured casting and examined (Figure 342). The discolored
mold into a 1500psi maximum pressurevessel.
area appears denser in the green state
The vessel was then pressurized to various and contains heavier atomic number
pressures and held for different lengths of elements.
time without heating. No obvious improve-
ment in rotor quality wasobserved. EDX (energy dispersive X-ray) was used
to compare the discolored area with the
2.9 Blade Discoloration normal area. EDX shows that the dis-
colored area has higher concentrations
of Al and Y. It should be noted that
As the casting procedures were established EDX at Garrett could not, in 1982, de-
and drying cracks had been routinely elimi- tect elements with atomic numbers less
nated, more attention was paid to other than II (sodium). In the same investi-
aspects of rotor fabrication problems, such as
gation, a flower-like structure was
a blade discoloration. An interesting observa-
found in the discolored region. EDX
tion was first made in 1981 that a darker band found that the flower structure con-
always appeared near the tip of each blade.
tained higher concentrations of Mo and
This discoloration first shows up in the green Y than the normal area. This was the
rotors as a dark grey color. Upon pre-
only time that Mo was found in the
sintering this discoloration turns to black material.
while the base material becomes white. After
sintering, this discoloration remains black o Seal Lab - SEM/EDX
while the base material turns to the normal
dark grey. When examined under a 30X micro- Several green rotor blades were
scope it was found that, after sintering, there analyzed at Seal Lab with a more sensi-
were always mud-like cracks associated with tive EDX (wavelength based) in an
the discolored area. These mud-like cracks attempt to compare the concentrations
were judged to be the cause of failure in the of lower atomic number elements
spin test performed at Garrett. Consequently, (N<II) between the discolored and
the elimination of the discoloration was iden- normal areas. Several energy levels
tified as a major program objective. were used. Table 55 lists the results.
It shows that oxygen, Na (or Zn) and Y
were detected or existed in higher con-
Two parallel approaches were taken to
centrations in the discolored region
combat this discoloration problem, namely I) that in the normal area. Carbon was
analysis and 2) process variation. The first
only found to be higher in the dis-
approach was aimed at determining, chemi-
colored region at 20 KV, thus is con-
cally and microscopically, the difference sidered inconclusive.
between the discolored area and the normal
area. The second approach was empirically to o Oak Ridge National Lab (ORNL) - Super
observe the effect of processing parameters Microprobe
on the degree of discoloration and the move-
ment of the discolored area. Some major A sintered rotor blade was examined at
findings are described in the following: ORNL using their high sensitivity super
291
Table 54. AGT1Ol Rotor Discoloration Analysis.
Discolored Area
Compared with
Analyzed by Method of Analysis Normal Area Sta_e of Process
Garrett ('1982) SEM-EDX Higher AI, Green (AGT)
Higher A1 and Y Sintered (AGT)
Allied (March 1986) SAXPS (Small Area X- Lower Y203 Pre-Sintered (AGT)
Ray Photo Electron
Spectroscopy)
SEM-EDS Higher AI and Y Green (T-2)
Higher AI Pre-Sintered (AGT)
Higher A1 and Y Sintered (AGT)
Seal Lab
(September 1984) SEM-EDX O, NaJZn, Y Green (AGT)
NASA (March 1986) SEM-EDX Sintered (AGT)
ORIGINAL PAGE IS
292
QI_ £OOK QUAL!TM
Table 55. Diseoloration Analysis of a niques. Although there were some dif-
Green Rotor. ferences in results found by different
techniques, the most consistent results
are that the discolored area contains
higher Al and Y concentrations than the
Elements Deteeted
EDX normal area.
Voltage Discolored Normal
(KV) Area Area 2) Process Variation
293
This experiment and the above experi- properties through the rotor. The baseline
ment indicated that the discoloration process has produced rotors with very uni-
phenomenon occurred after the mold form PSD in the green rotors. To verify
_as filled, i.e., during the casting this particle size distribution measure-
period. The segregation or migration of ments were made at different locations on
certain species which resulted in dis- several rotors to determine whether there
coloration occurred during the casting is any variation in particle size distribution
time which ranged from one to four within dried green rotors. The results from
days. one randomly selected rotor showed that
no significant difference in PSD was found
o Plaster Patehed Blade Tip Mold within the rotor (Table 56).
One-half of the blade edges of a wax Table 56. Particle Size Variation
mold were cut off and then sealed with Within a Green Rotor.
plaster. This was to provide faster
casting time (minimizing materials
migration/segregation) near the blade Pereentiles of Particle
area where discoloration occurred. Size, l_m
This experiment resulted in a broader
band of darker color parallel to the Loeation 90th 50th 10th
plaster seal on each blade which was Dome 2.62 0.90 0.36
sealed with plaster. The remaining Leading Edge 2.61 0.90 0.36
unmodified blade of the same rotor Blade 2.64 0.90 0.36
showed the usual pattern of discolora- Trailing Edge 2.58 0.90 0.36
tion. Shaft 2.60 0.89 0.36
A rotor was cast with no additives in During the AGT program, 50 turbine rotors
the slip. No discoloration was observed were shipped to Garrett. Many of these rotors
on the blades. were spin tested and exceeded the 115K rpm
proof test requirement. None of the rotors
Another rotor was cast with a slip con- could be considered "engine quality" due to
taining Y203 but no Al203. It also did missing blades, surface porosity, and dimen-
not show any discoloration. sional deviations from the print.
294
The stator vanes were to be injection
molded, and all the other parts were to be slip Other parameters also affect slip
cast reaction-bonded Si3N4. The technology behaviors. Experiments aimed toward density
baseat ACC prior to the start of this program control of silicon slips prepared with various
was the establishment of a silicon slip, desig- fractions of air classified powder were per-
nated as RBN-104, and the demonstration of formed. Limits exist between pH and green
the net shape casting capability of various density such that the controllable range of
small engine components under several green density by pH and adjustment alone
government programs. It was initially appears to be between 1.65 and 1.75 g/cm 3.
assumedthat this baseline technology could be
transferred to the fabrication of large AGT It was also recognized that small amounts
components without any significant develop- of impurities such as calcium, deleteriously
mental efforts. As the program proceeded, it affected slip rheology and subsequent casting
became apparent that improved materials and and nitriding results.
processing procedures would need to be
developed. It was also found that slip casting 3.4 Castin_ Procedure Development
and other processingsteps were very sensitive
to tooling/design changes. A flow chart of the overall slip casting
process is shown in Figure 343.
3.2 Materials Development
One slip casting iteration was tr}ed in
efforts to eliminate center line shrink in the
The original baseline compositions were
backshroud. The backshroud was cast to a
established using silicon powder supplied by
thickness of one to one and a half inch using a
Kawecki Berylco Industries (KBI). Later in the
net shape form one surface of the backshroud.
program KBI discontinued operations necessi-
The backshroud plaster mold to an otherwise
tating evaluation of other sources of supply.
solid ingot, as is shown in Figure 344 and 345.
Silicon was then obtained in lump form as ore
This is an effective method to produce the
directly from the mine which reportedly sup-
backshroud avoiding flow lines, centerline
plied KBI's material. The ore was pulverized
shrink and air entrapment, but requires con-
by an outside source and returned in powder
siderable green machining.
form. Analysis revealed high impurity levels
and slip preparation was difficult and not
3.5 Drying and Prenitriding
reproducible. Other sources of high purity
silicon powder were evaluated and Kemanord,
Drying of large, slip cast components,
Sweden, was finally selected as most reliable
especially those with non-uniform wall thick-
with respect to purity, consistency of product
ness, has proven to be one of the more crucial
and availability of supply.
steps in processing. Extensive evaluation of
drying and prenitriding cycles were conducted.
3.3 Pre-Casting Materials Preparation It is apparent that components such as the
Development turbine shroud and transition duct must remain
in the plaster mold after casting for a length
Materials preparation prior to actual cast- of time to achieve good green strength. Sub-
ing underwent continuous evaluation. Particle sequent to removal from the mold, it is essen-
size distribution (PSD) and surface area (SA) tial that the casting be permitted to dry
of silicon powder are important parameters in slowly and completely before attempting to
controlling slip rheology. Experiments were prenitride. Several techniques have been used
conducted using the air classifier to separate which include controlled humidity drying, dry-
the powder into different PSD fractions and ing in an enclosure and subsequent exposure to
observing slip behavior as a function of warm dry air, slowly heating in an oven over a
particle size. long period of time to the boiling point of
295
HI-PURITY Si
I
PATTERN
PREPARAT ON I MILLGRIND [ I CHEMICAL
ANALYSIS I CASTING I
I I I I
MOLD
[PREPARATONI
[
I
PLASTER
MIXING I PREPARATIONI
I
i PARTICLE
SIZE DISTRI8
I
I MOLD
REMOVAL
i
I
I
I REMOVAL
PATTERN I I SURFACE
AREA I DRY I
I SLIP AGING
I
I
I FILTER
EVACUATE
AND
I _D_I
I ! I
I SHIP I
296
GlhlGINAL PACE IS
OF POOR Q[_,.,_,.I.1TY
water and, allowing the part to remain in Plates were cast to determine the effect
vacuum for several days prior to prenitriding. of nitriding aid. Compositions investigated
Several backshrouds and some transition ducts include the baseline 3 percent Fe203, 1.5
have survived prenitriding and machining but percent Cr203 and 1.5 percent Fe203 plus 1.5
the turbine shroud continues to crack during percent Cr203.
prenitriding. The nitriding aid billets were machined
into test bars. One-half of each of the speci-
3.6 Nitriding Development
mens was nitrided in staddard nitriding cycle
Early work investigation nitriding capa- and the remaining half was nitrided in an
bility included nitriding thick sections, atmosphere containing a 4 percent helium
nitriding aids, and the effect of a 4-percent addition.
helium addition to the normal H2-N 2 nitriding The results are tabulated below.
atmosphere.
H2-N 2 H2-N2-He
Test plates of RBN-104 material were cast
Nitriding Aid MOR MOR
in thickness ranging from 1/4 inch to 1 3/4 Chemistries (ksi) (ksi)
inches to evaluate the nitriding capability of
the standard cycle. These plates were nitrided Baseline (RBN-104, 47.0 47.0
and were evaluated for the presence of 3 percent FeO 2)
unreacted silicon. The nitriding of thick sec- 1.5 percent Ye203 39.7 41.7
tions indicated that sections in excess of 1/2 1.5 percent CR203 38.8 38.8
inch thickness contained mostly unreacted sili- 1.5 percent Fe203 +
con in the center. However, these evaluations 1.5 percent Cr20 3 41.8 41.0
were conducted with little mass of material in
the furnace and a relatively short cycle. Since The new nitriding aids and nitriding cycle
then it has ben found that nitriding is far more showed no improvement over the standard
efficient when a large load mass and longer nitriding cycle and the baseline material, RBN
cycles are used. 104.
297
This PageIntentionally Left Blank
298
APPENDIX B
299
PRECEDING PAGE BLANK NOT FILMED
SRBSN Material Development and for the highly stressed turbine rotor. Yttrium
Characterization oxide was selected as the sintering aid for
these materials as good strength at high tem-
Sintered Reaction Bonded Silicon Nitride perature was retained by early hot pressed
(SRBSN) describes a class of material combin- silicon nitrides containing this additive(3).
ing reaction bonded silicon nitride and sintered However, the Y203 - Si2N 4 system is sus-
silicon nitride technologies. ceptible to oxidation, particularly with applied
stress at intermediate temperature regimes.
The consolidation process, outlined in Fig- Consequently, time-dependent property deter-
ure 346, begins with the addition of a sintering mination also became an important aspect of
aid to a fine-grained, high purity silicon the material characterization. These two
powder. Components are fabricated from this characteristics, strength (flexural stress
mixture using standard green forming rupture) and oxidation resistance, dominated
processes including slip casting and injection the evaluation program and determined the
molding. The part is then nitrided and sin- developmental iterationsof this material.
tered to near-theoretical density.
Four grades of slip cast, yttria-doped
SRBSNs were developed at Ford, code
numbered RM-0 RM-I(4), RM-2(5) and RM-3.
FORD SRBSN PROCESS The properties of each of these grades are
summarized in Table 57.
SILICON POWDER + SlNTERING AID[
! RM-0 Material
300
Table 57. Slip Cast SRBSN Material Properties.
i,
Density (g/cm_ 3) 3.05 - 3.31 3.20 - 3.25 3.26 -3.31 3.26 - 3.34
Oxidation MOR
Stress Rupture
1000C, 20 ksi
time dependent
failure (57 hrs
avg)
Oxidation testing was again performed at ments. Again, no visible cracking was ob-
700 and 1000C. Exposure times were in- served under any test condition; however,
discoloration was noted. These data suggested
creased, up to 700 hours, and two new tests
wei-e introduced. Oxidation kinetics were that an oxidation problem stillexisted.
determined by sequential weight gain mea-
surements and thestrength after oxidation
was ascertained. This testing revealed that Residual strength after oxidation exposure
the reaction kinetics were different for each was measured. Figure 348 shows the strength
test temperature (Figure 347). At 700C, the decreasing substantially when samples were
kinetics were linear, and influenced by the oxidized at 700C, but deteriorating only
testing sequence, while at 1000C, parabolic slightlyafter the 1000C exposure. Addition-
behavior was observed. Lower weight gains ally, the strength decrease at 700C was
were recorded for samples exposed for 700 dependent on the testing sequence, as evi-
hours without removal for weight measure- denced by the uninterrupted data point. A
301
120
RM-I Uninterrupted
12
z
O
N 700°C
E 80
o IO ¢:3
X
E 0
n-
8 UJ
__ 60
W t,.
-1-
6 I000 °C I-
Lu (.9
(.9 z 40
Z tU
OC
"t- k- m
O .4 (/3
I-
2O
700°C Uninterrupted
O I 1 I I I I
0 0 200 400 600 800 I000 12OO 140C
0 IOO 200 300 400 500 6OO 700
TEMPERATURE (°C)
TIME (hr.) Figure 348. Strength After Oxidation
Figure 347. Oxidation Kinetics in RM-20. of RM-I.
correlation was obtained between the oxi- attributed to a superior microstructure con-
dation kinetic and the strength after exposure. sisting of a matrix of interlocking needle-like
The strength dependence on test conditions grains (Figure 349), a structure found to result
also suggested a potential thermal shock prob- in optimum properties in hot pressed silicon
lem. nitride(7). Increased process control also con-
tributed significantly to these improved
RM-2 Material results.
The objective of this development iteration The oxidation kinetics at 700C are para-
bolic, as are the 1000, 1200 and 1400C data
was improvement of the low temperature
properties of the material as a function of (Figure 350). However, the 1000C data con-
tinue to reflect anomolous behavior with
both the oxidation kinetics and factors con-
noticeable weight gains. The strength- after-
trolling the strength reduction after oxidation.
oxiation data (Figure 348) show that the
This was accomplished through control of the
secondary Y-Si-O-N phases present in the severe 700C problem of RM-I was solved; only
a minor strength reduction was measured at
material via further refinements in sintering
1000C.
conditions and enhanced quality control.
Testing to this point revealed no serious
This material itertion yielded a higher problems with the RM-2 material. Additional
characteristic strength (107 ksi) and Weibull testing was undertaken to examine the mate-
modulus (21.I). These improvements were rial'sthermal shock resistance (in response to
302
l
!
1.5
I
B
"-. 1.0
1200 %
Figure 349. Microstructure of RM-2. 700°C
1-
test results obtained for RM-I) and stress __
I,i 1000 "C
ol
rupture behavior.
303
The strength and Weibull modulus are 100
ksi and 19.0 respectively, essentiallythe same I000°C
as in RM-2. Again, these data consolidate the
results of numerous batches. Figure 351 com-
pares the strength/temperature data for
RM-I, RM-2 and RM-3, showing slightlylower
strengths for the RM-3. A
E
120 o 1.0
tU
I00 n-
LU
Z
1400 =C
"I"
... 75 0
m
Or) RM -3 "I"
n- LU 1200°C
O
=E
50-
700°C
0 I I I
0 I00 200 50,
25- TIME (hr.)
304
exposure. Additionally, it presents no time- stant, and the primary objectives of the pro-
dependent stress rupture problems for stress gram were:
levels up to 40 ksi and temperatures betwen
800 and 1000C. i) Development of process techniques for
casting crack-free turbine rotors using the
While RM-3 exhibits significantly improved fugitive-wax process.
properties over earlier SRBSN materials,
further advances are still possible and appear 2) Fabrication of rotors of the RM-20 mate
305
II
PREFORM
i,
NITRIDE
fill l
COMMINUTION
FABRICATION
(SLIP CASTING)
BISQUE FIRE
GREEN MACHIME
_ t_ i_
INSPECT
ii
SPIN TEST
306
b) RM-20 Rotor Fabrication suspension, would break down over a long
period of time, resulting in poor viscosity
Slip Cast Material Preparation control. Wet milling and screening experi-
ments were designed to eliminate agglom-
Early studies (12) examined the production erates in the RM-20 casting slip. Screening
of stable slipsfor the casting of RM-20 rotors. was only partially effective, and wet milling
The objective of this work was the develop- drastically changed the powder particle size
ment of a slip,free of outgassing, with good distribution. The best result was achieved
flow characteristics,stabilitywithin the cast- with a combination of dry ball milling and
ing time period and demonstrating little limited amount of wet milling.
thixotropic behavior. Slip deflocculants
evaluated were a) Keltex, b) Dispex A-40, c) Table 59 summarizes this procedure which
Dispex N-40, and d) California 226/35. calls for 48 hours of dry milling,followed by
removal of the balls and the addition of water.
Of this group, Dispex A-40, in concentra- This suspension is then tumbled 72 hours. The
tions of 0.26 percent, produced the best mill is recharged with grinding media and the
results. Figure 354 shows the viscosity rela- suspension is wet milled for 1.25 hours. The
tionship with spindle rpm for various levels of grinding media are removed, the viscosity of
Dispex A-40. Initially, a problem was the slip is adjusted to 125-150 cps via water
encountered in casting the shaft (the last addition and the slipis tumbled 16 hours.
portion of the rotor cast), wherein the slip
became thixotropic, causing slumping and dis- Table 59. Improved RM-20 Slip
tortion. This problem was eliminated by sub- Preparation Procedure.
stituting Displex N-40 deflocculant for
approximately 50 percent of the A-40 defloc-
culant. - 48 hours dry milling
One problem associated with slip con- - 72 hours tumbling, no milling media
sistency is the presence of agglomerates in the
slip. These agglomerates are formed during - 1.25 hours wet milling with grinding media
dry milling of the RM-20 powder. The ag-
glomerated powder, when placed into slip 16 hours tumbling, no milling media
& .34%
200 0.43% DISPEX A-40
CONCENTRATION
[3.26 % BY WEIGHT
I00
>
RPM
0 ! I I I
I0 20 50 I00
Figure 354. Relationship of Viscosity Vs. Spindle Speed for
Various Concentrations of Dispex A-40 Deflocculant.
307
This procedure produced a casting slip of caused large deflections in thin sections of the
good stability and excellent consistency. casting molds. The molds had the form of a
Several rotors were cast with this improved rotor sitting on a flat disc and clamped to a
technique. plastic base which loaded the wax mold on the
webs formed between blade tips. Mismatches
Rotor Slip Casting between the plaster and mold caused distor-
tion in the wax. This type of mold, and the
Historically, blade cracks and inferior technique used to clamp it, were changed to
microstructures in blade tip regions resulted in eliminate distortions in the wax.
low rotor yield. Also, a high proportion of spin
pit failures originated in blades that appeared A new method of dipping the wax mold,
sound, which suggested that subsurface using an aluminum contoured plate, was devel-
defects were controlling quality,, even in oped. The plate matched the base contour of
rotors that passed visual and Zyglo inspec- the water soluble positive wax and had the
tions. To overcome these problems, a sys- web sections between blades machined away,
tematic review of all the steps in the casting leaving a ledge of aluminum 0.060 inches wide.
process was undertaken, starting with the The positive wax was held down loosely with a
composition of the waxes used to make the bolt and a cap. Any stress on the positive wax
molds. could cause a crack which would translate into
a web inside the wax mold and a corresponding
Thermal Expansion of Negative Fugitive Wax crack in the cast part. The contour of the
aluminum dipping plate wax was produced in a
The wax used for casting molds at Ford
computer-controlled mill. The same program
was a product of the Freeman Company, was used to mill this exact contour into the
called "Dip Seal". In 1985 Freeman ceased
surface of the plaster on which the wax mold
marketing this product and an analysis of the sits, thus assuring a perfectly matched inter-
wax was made to determine whether it could
face. The first molds, produced by three dips
be duplicated "in-house". By analysis the wax
in a 155F McCaughin dip wax, were heavy
was primarily paraffin (65 percent) and 35
enough to allow filling of the mold without
percent methyl stearate. The later was
mechanical clamping. This arrangement was
deemed undesirable due to its' insolubility in slightly modified when the thickness and
toluene, the solvent used to remove the wax
weight of the molds were changed; however,
from the casting. A large change in the
the unstressed mold feature (except for stress
thermal expansion rate of paraffin occurs at caused by the slip itself) was retained.
rather modest temperatures (28 - 34F). This is
caused by a solid-phase change in the crystal Wax Removal
structure of the wax and results in a five-fold
increase in an already high thermal expansion
While the triple-dip molds produced a high
rate. Therefore, casting and wax removal is percentage of crack-free rotors, 24 hours were
now done at constant temperature to avoid required to dissolve the wax. Removal was
any expansion damage to the casting. accomplished by immersing the wax-covered
To replace the Freeman Dip Seal wax, a casting in toluene without agitation and at
casting wax (LN-209-218) was purchased from constant temperature. Thinner molds could be
J.F. McCaughin Co. This material is a bees- expected to dissolve quicker and less time in
wax-paraffin-carnauba mixture with a melting toluene would be a desirable result. It was
temperature of 150F. also suspected that soaking the wax caused it
to swell slightly, stressing the blades of the
Mechanical Strength of Negative Fugitive Wax casting. Hence, thicker molds could be
expected to stress the castings more than thin
Because of the low elastic moduli and ones. Initial attempts at a single dip, thin
strength of waxes, slight forces or loads mold produced problems in the wax positives.
308
.- _. ._ <,:_b_r;__
Positive Wax Preparation ring about 6 inches in diameter, 1 inch high and
0.060 inch thick was fabricated. This ring
Polishing the wax with 4-0 steel wool elim- weighed 70 grams and, when placed on the wax
inated surface defects and improved wax re- mold at the tip of the blades, held the mold
moval from the casting. Two new problems down (Figure 355). Because of the perfect fit
occurred in the thin wax molds; splitting of of the wax to plaster, there was no deflection
the mold down the blade edges and surface of the wax.
contamination by traces of lubricant used in
Wax removal was accomplilshed in 6 to 8
the injection molding of the wax positive. The
hours (versus 24 hours for the triple-dip wax
lubricant was elimiinated by two consecutive
mold).
cleanings in an organic solvent.
Material Quality In Rotor Blades
The problem of mold splitting was caused
by the uneven coating of wax around the edge Spin pit tests of visually sound rotors pro-
of the blades. At the corners the wax deposit's duced a large percentage of blade failures.
are very thin. Chamfering this edge on all This suggested that the blades had subsurface
blades caused a more even layer of wax and cracks initiating failure(s) at speeds well
reduced this tendency to split. below those at which hub failures occurred.
To assess the qualify of the subsurface blade
Single Dip Molds material, the sound blades were lightly glass-
beaded after the rotors had been bisque fired.
Initial attempts to use single dip molds Removal of the surface disclosed porous mate-
proved difficult. The wax molds were 70-80 rial at the blade tips. To overcome this, the
grams lighter than previous molds. Unless the castings were spun at 100 rpm while pouring.
slip was poured into the mold slowly and This application of centrifugal force enhanced
carefully, a leak would start at the mold/ the migration of the material to the tip and
plaster interface, quickly draining the slip and significantly reduced the number of blade fail-
ruining the casting. To overcome this, a steel ures.
Figure 355. Single Dip Wax, Plaster Base and Steel Retaining Ring.
309
Remaining Problems With Wax Molds and Wax inspection and subsequent sintering. This
Positives problem is most severe during the placement
or "packing" of the rotor in the power blanket
Two problems remain with the wax sys- for sintering. Therefore, a presintering or
tems. First, the positive has a tendency to "bisque" firing treatment was developed to
distort with shelf time. This tendency to partially consolidate the casting and provide
stress-relieve and hence distort is well under- adequate handling strength.
stood in the dental profession where critical
dimensions in wax patterns must be main- The bisque firing cycle consists of slowly
tained. This problem has not been addressed, ramping in a nitrogen atmosphere to 1500C
but it will be a deterrent to accurate blade and holding at temperature for 2 hours.
forming. This deformation also causes the During this cycle the casting undergoes partial
shaft diameter of the wax positive to ovalize consolidation, as indicated by a 2.5 percent
by 0.010 to 0.020 inch over a few weeks. linear shrinkage, which is sufficient to impact
Blade deformation has not yet been defined. suitable handling strength. An additional
Possible solutions for this problem include advantage of bisque firing is that it permits
refrigerating the wax positives until they are machining of the casting with standard high
useds or using them immediately after they speed tool steel, and thus reduces costly
are molded. diamond grinding of the final component. This
pre-sintering cycle does not impede the final
Secondly, the inside surface of the wax sintering kinetics. This process is now used on
mold develops a rough surface even though the all castings.
wax positive is polished smooth before drip-
ping. Apparently, the 150-160F melting tem- Sinterinff of Rotor
perature of the water soluble wax is too close
to the 150F melting temperature of the dip The sintering time/temperature profile
wax. Lowering the temperature of the dip initially developed was a single-step cycle.
wax to its lowest usable point improves the This cycle was adequate for the densification
surface texture, whereas raising the tempera- of the original platformed rotors but yielded
ture or holding the positive in the dip wax unpredictable blade distortion in the rede-
longer than required heightens the effect. signed rotor castings. In addition, consider-
These bumps on the casting not only destroy able fusion of the packing powder occurred,
the smoothness of the component surface, but increasing the difficulty of removal, particu-
give the mold wax a rough surface, making larly between the blades. Packing powder
removal more difficult. The surfaces can be compositional changes reduced but did not
smoothed after bisque firing by sanding, but eliminate the problem.
this is a tedious job and should be avoided.
A two-step sintering cycle was developed
In summary, the process modifications to reduce blade distortion and facilitate re-
described have produced a marked improve- moval of the packing powder. The first step
ment in rotor fabrication. Approximately 70 of the dual cycle incorporated a packing pow-
percent of slip east rotors have been crack der (boron nitride, silicon nitride, yttria and
free. There is, however, a need to improve siliea) and a 12 hour temperature ramping
the quality of the material in the blade tip schedule that had three discrete temperature
region of the rotor. holds: 0.5 hours at 1520C, 0.5 hours at 1620C,
and 4 hours at 1720C. Neglilgible fusion
Rotor Heat Treatment and Equipment occurred within the packing powder.
Pre-Sintering of Rotor
The second step of the sintering cycle
The dried RM-20 rotor castings are ex- utilized a compositional change in the packing
tremely fragile and difficult to handle through powder and a single temperature hold of 12
310
hours at 1800C. This compositional change was generally dark in color and has a well-
and increasedtemperature and hold time pro- crystallized secondary phase. The interior
vided greater availability of Si0(g) to maintain region of the rotor is lighter in color and
the required oxynitride composition within the shows (by x-ray diffraction) a predominantly
rotor, resulting in full densification. This glassy second phase. Scanning electron micro-
packing powder was easily removed. scopy indicates that the densities and chem-
ical compositions of both regions are identical.
At the completion of the two-step cycle, a Cold spin testing of several rotors produced
nominal 18 percent sintering shrinkage and blade separation failures at the intersection of
final densities of 3.24 to 3.28 g/cma were the two regions. Fracture origins could not be
obtained. Observed blade distortion was min- identified but separation occurred near the
imal. interface of the duplex zones in all of the
blades• This zoning interface may have acted
The two-step cycle approach, although as a stress riser and produced premature fail-
greatly improved over the earlier one-step ures.
cycle, considerably increased the process
complexity and total time neededto complete An investigation of heat treatment tech-
the sintering cycle. Each step required a niques to crystallize the interior region of the
complete temperature cycle with re-packing rotor, and the elimination of the duplex inter-
of the rotor between cycles. In addition, an face, was undertaken. A half-fraction of a
undesirable extra handling of the fragile rotor 24-1 statistically-designed experiment was
was incurred. used to study four variables (nucleation tem-
perature and time, growth temperature and
Consequently, a new cycle was developed time) at two levels each, requiring 8 heat
for the final rotor iteration. Its main features treat cycles.
were:
Test bars cut from sintered rotor #40 were
a) A one-step sintering cycle heat treated• A 0.025 inch layer was ground
from each test bar. X-ray diffraction analysis
b) A 36-hour hold (compared to the 12- hour
revealed that all eight heat treatment cycles
hold) at the maximum temperature
resulted in a crystallized second phase. How-
c) Two discrete temperature holds: 1 hour at ever, when the 0.063 inch-level (maximum
1500C and 36 hours at 1800C. depth of test bar) was examined, four of the
eight bars retained some glassy phase.
d) Two discrete temperature ramp rates:
300C/hr up to 1500C, followed by 50C/hr
Table 60 summarizes the eight heat treat
to 1800C.
cycles and the x-ray diffraction results. These
e) The packing powder, which included 24 initial test results indicate that devitrification
percent boron nitride, was packed loosely. of the glassy second phase throughout the
rotor (over 1 inch depth) would require further
In this one-step sintering cycle, shrinkage was cycle modifications.
nominally 18 and a final density of 3.28 to 3.29
g/cm 3 was obtained. The packing powder was Full size rotors were heat treated, sec-
readily removed and blade distortion was min- tioned and examined by x-ray diffraction to
imal. determine phase composition. One rotor (#64)
was heat treated using a cycle similar to cycle
Post Sinterlnff Heat Treatment of RM-20 #HT4; however, the hold time at the "growth"
Rotor temperature of 1450C was increased from 4
hours to 96 hours. Rotor #63 was heat treated
All of the pressureless sintered rotors had using a cycle similar to cycle #HT7 with an
a duplex zoning structure• The exterior casing identical increase in hold time. The relevant
311
Table 60. Summary of Heat Treat Cycles and X-Ray Diffraction Results.
differences in their cycles, as shown in the The secondary phase composition of rotor
table, were in their "nucleation" temperatures #64 was identified as:
and duration times.
The results of these tests show that the YIoSi6024N2 ("H") + Y2Si2 07
two heat treatment cycles did affect the sec-
ond phase throughout the interior of the two + Y2SiO5 + a small amount of glass.
rotors, although not to the same degree. The
original #HT4 cycle, used on the test bars, After the heat treatment, MOR test bars
resulted in some retained glass (see Table 60). were cut from rotors #63 and #64 and from
Similarly, the modified #HT4 cycle (rotor #64) rotor #65 which did not undergo post-sinterlng
resulted in more glass than the modified heat treatment.
#HT7s cycle (rotor #63).
The secondary phase composition of rotor Room temperature four-point MOR bend-
#63 was identifiedas: ing tests were then carried out on five test
bars from each rotor. The results are sum-
Y10Si6024N2 ("H") + Y2Si20 7. marized in Table 61.
Heat Cycle
Rotor # Mean MOR Std Dev (See Table 60)
(ksi) (ksi)
312
These results show some deterioration of reduce the faster deterioration of the floor
room-temperature strength with decreasing relative to the rest of the hot zone, caused by
levels of glass in the secondary phases. It is spilled packing powder reacting with the floor.
expected, however, that high temperature To minimize the down-time needed for a hot
strength will be greatest in the rotor with the zone rebuild, two additional hot zones were
least amount of the glassy secondary phase. built, Table 62 shows the marked improve-
ments achieved with in-house furnace modifi-
The overall strength level of these rotors is cations.
approximately 30-35 percent lower than the
test bar strengths of 125 ks{ previously re- d) Spin Testing RM-20 Rotors
ported. A chronic problem in any material/ General Review
component development program is that of
Extensive changes were made in the meth-
obtaining material properties similar to those
ods used to mount spin pit arbors to AGT
of the test bar material in a large component, rotors and the manner in which the rotors are
such as the AGT rotor. In this case, the
balanced. Previously, the final spin pit arbor
difference in strength is attributed to poros-
was mounted using "Loctite" and a 0.001 inch
ity. Such porosity is believed to occur during to 0.002 inch loose diametrical fit between the
the long sintering times required to achieve
arbor and the rotor. This technique did not
high density. An effort was made to eliminate
produce perfect concentricity between rotor
porosity in the RM-20 rotors with hot isostatic shaft and the outer diameter (O.D.) of the
pressing (HIP).
steel arbor on which the assembly is mounted
and spun during balancing. Tests revealed that
Sintering Equipment this method introduced unbalanced forces
which then had to be removed by grinding
The pressureless sinterlng process utilized
away rotor surfaces, usually the blades.
a cold-walled vacuum furnace and a refractory
Obviously, this was unacceptable for rotors
metal hot zone. A major drawback of this
which might be engine candidates. To over-
system was reactivity of the SiC(g) with the come this problem, a press fit arbor was
shot refractory metal. The hot zone was
designed and the balancing process was split
limited to approximately 15 to 18 cycles
into two parts; an initial balance check and a
before a complete rebuild was required. Sig-
final balance operation.
nificant in-house modifications increased the
furnace life to approximately 25 cycles, but Initial Balance Check
further improvement was necessary. There-
fore, a furnace manufacturer was contracted To reduce the extensive grinding previously
to redesign the hot zone and other deficient required to balance rotors, a method of re-
areas to improve the sintering enviornment. locating the geometric center of the rotor
shaft through the mass center of the part was
The new design provided for a smaller, adopted. The mass center was located and the
more efficient hot zone faced with 0.005 inch shaft portion of the rotor was ground as close
thick tungsten sheet. After several cycles, to the center of the blades as possible. A
deterioration was noted which rapidly acceler- steel sleeve, 3.50 inch long with 0.070 inch
ated with subsequent use. The hot zone be- wall thickness, was press-fitted to the shaft.
came unusable after 23 cycles. An in-house The press was 0.0015 inch on the diameter and
redesign and rebuild effort resulted in an the sleeve was fitted by heating before instal-
improved hot zone. Reconstruction included lation. The sleeve was installed while the
the replacement of the 0.005 inch tungsten rotor was still mounted on the grinding ma-
face with 0.020 inch molybdenum sheet and chine. When cooled, the O.D. of the sleeve
molybdenum rods added to the ceiling struc- was ground to fit the half-bearings of the
ture for support. A sacrificial molybdenum balance machine. The initial check of unbal-
sheet was placed over the floor in order to ance was then made. Results revealed from
313
Table 62. Life Improvements Resulting from Furnace Redesign.
Previous Latest
Category Design Design
40 _ercent to 60 percent less unbalance than encountered to 0.010 - 0.040 oz-in, an amount
rotor: mounted with Loctite. With the direc- which can be corrected by grinding without
tion and size of the unbalance known, the destroying the rotor blades.
offset of the rotor shaft could be calculated.
The geometrical center of the shaft could be
e) Spin Testing of RM-20 Rotors
relocated in greater proximity to the mass
center, further reducing the unbalance and
Spin tests of RM-20 rotors were conducted
allowing finalbalancing with minimal grinding.
in a vacuum pit using a Barber Stockwell
Final Balancing 150,000 rpm air turbine. A summary of test
results,along with failure analysis comments,
isshown in Table 63.
After the initial check, the sleeve was
removed by heating it to 300F to 400F. The
rotor was returned to the machine shop, This series of tests revealed an increasing
mounted and adjusted until the shaft portion uniformity in the speed and type of component
had zero runout. The machine check was then failure. All rotors in this group were crack
adjusted to reposition the mass center at the free, based on visual and Zyglo inspection, and
rotational center and the shaft was reground fully bladed. All were cast with the same
to run true to the mass center. The steel spin- techniques, by the same people, from RM-20
pit arbor was installed with a 0.003 to 0.004 SSN material. Although previously tested
inch diametrical press fitand itsO.D. ground rotors (RM material) failed at higher speeds,
to fit the balance machine half bearing. The they were not fully bladed and blade failures
quill shaft hole was also ground true to the predominated. Most of the earlier rotors
mass center during this stage. These steps tested were made of SRBSN material.
were allaccomplished without dismounting the
rotor from the original machine position used In the RM-20 rotors, there was a general
to regrind the shaft to the new location over trend toward improved blade quality, as re-
the mass center. The rotor was then final flected by the number of hub failures in the
balanced by grinding on the back and on the early stages of RM-20 material development.
shaft just forward of the blade root on the This suggested that the large flaw size of the
exducer end. These steps reduced the unbal- cast rotor material (as compared to test bars)
ance from the 0.160 - 0.200 oz-in, previously was controlling the ultimate failure speed of
314
Table 63. AGT RM-20 Rotor Spin Test Results.
**In several rotors (as noted), blade failure at lower speeds preceeded the final
hub failure.
these rotors. All of these rotors were pres- firing by ASEA Cerama using their proprietary
sureless sintered with a 36-hour hold at tem- glass encapsulation process. HIPping condi-
perature. This long hold time was believed to tions were a maximum temperature of 1700C
result in increased porosity and correspond- and a soak time of two hours at a pressure of
ingly lower strength, having a pronounced 160 MPa.
affect on the highly stressed hub during spin
testing. One noteworthy aspect of the failure of
the HIPped rotors was the recurrence of blade
In an effort to reduce porosity, rotors No• failuresat speeds below the utlimate hub burst
75 through No. 105 were HIPped after bisque speed• Rotor No. 94 failed in three blades but
• 315
reached the limiting speed of the spin pit air It was observed that even when the percent of
turbine without hub failure and was retired total porosity was small, large isolated pores
with the hub intact. This rotor was within 940 existed throughout the sample. The largest
rpm of the 105,000 rpm qualification speed pore of each sample was measured and re-
when a blade failed and it sustained a 112,980 corded. The relationship between the rotor's
rpm ultimate speed without hub failure;indi- burst speed and the largest pore size of its
cating that HIPping raised the hub strength to corresponding fragment was plotted and is
adequate levels, but blades again became the shown in Figure 356. This plot shows the data
limiting factor. Blade quality and strength fallinginto two groups: one group had smaller
adequate for a 95,000 rpm hub capability were pores, corresponding to rotors with the higher
now the criticalparameters determining rotor burst speeds. The second group had larger
durability. This is also illustratedby rotor No. pores, corresponding to the rotors with the
105 which failed in three blades before hub lower burst speed. In addition, when the
failure occurred in excess of 103,700 rpm. individual data points in Figure 356 were eval-
The overall results confirmed that a measura- uated relative to sintering process, it was
ble increase in hub strength resulted from determined that the smaller pores (high burst
HIPping. speed group), corresponded to the HIPped
rotors; whereas the larger pores (low burst
Analysis of RM-20 Spin Pit Tested Rotors speed group), were found in the pressureless
sintered rotors.
A porosity analysis was conducted on both
pressureless sintered and HIPped RM-20 rotors The flexural strength data obtained from
as a means of explaining the higher burst test bars cut from pressureless sintered and
speeds of HIPped rotors. HIPped rotors further substantiate these re-
sults. As shown in Table 64, the average
The spin-to-failure tests resulted in the strength of the HIPped rotor material was 111
rotors bursting into many small fragments. ksi versus 75 ksi for pressureless sintered
These pieces were too small to be accurately RM-20 material. Clearly, the overall results
traced to their original position in the pre- of porosity size determination, fracture
failed rotors. Consequently, nine fragments strength evaluation and spin testing demon-
(3 x 20 mm), one from each rotor, were chosen strate the need to reduce pore size in the
randomly. The nine pieces were cut and RM-20 rotor material.
polished to permit microscopic examination of
the porosity. The porosity evaluation was f) The Effect of Heat Treatment on the
performed using DIMA (Digital Imaging Analy- Flexural Strength of RM-20 Rotor Material
sis). Both the percent of overall porosity and
the largest pore dimension and its area were The effects of heat treatment on the
measured on five consecutive 'fields' (0.62 x HIPped RM-20 rotor material were studied in
0.96 mm each) per sample at 180X magnifica- terms of flexural strength and secondary
tion. phases. Modulus of rupture was measured at
room temperature and in some cases at 1200C.
Noticeable variations in porosity were seen Speciman size was 1.25 x 0.25 x 0.125 inch,
when scanning across the rotor samples. In upper span 0.375 inch, lower span 0.75 inch
one sample, total porosity ranged from 0.5 and the loading rate was 0.02 in/min. Table 65
percent to 9.6 percent. The smallest variation summarizes these results,indicating the type
per sample was 0.2 to 0.7 percent. No corre- of heat treatment, specimen (rotor versus test
lation could be established between total bar), secondary phases present and strength
porosity of the pressureless sintered versus the resultsat room temperature and 1200C.
HIPped rotor material. There was, however,
considerable range (1 to 200 microns) in the The flexural strength of the as-HIPped
size of pores found in the nine rotor samples. RM-20 material cut from a rotor was 111.3
316
RPM @ FAILURE VS. MAX. PORE SIZE
105,000
[]
100,000
A
95,000 V
=Z
o,,,
1
90,O00
am A
85,0O0 I W
80,000
Figure 356. Rotor Pore Size Versus Spin Test Rotor Speed.
Table 64. Flexural Strength Of Pressureless Sintered and HIPped RM-20 Rotor Material.
317
ksi. X-ray diffraction analysis indicated a B- this slightly diminished high temperature
silicon nitride crystalline primary phase with strength due to the small sample size.
an amorphous secondary phase. When heat
treated as a half-section rotor (Heat Schedule An interesting phenomena associated with
C), the RT strength was reduced by approxi- these heat treat studies was the pronounced
mately I0 percent- not totally unexpected in affect of heat treatment on the smaller speci-
view of the reduced secondary phase glass men (in this case, the MOR test bar) versus
content and formation of H-phase the previously discussed rotor subsequently cut
(Y5Si3OI2N) and Y2Si207. The 1200C MOR into MOR bars. This can be seen in the last
was 71.5 ksi for this heat treated rotor three tests reported in Table 65. In heat treat
material. schedule B + D, MOR test bars were heat
treated for 96 hours at 1450C. This treatment
Heat Treatment B, with a complete rotor resulted in a severe room temperature
and a shorter total heat treat time, resulted in strength reduction to 73 ksi. Secondary phases
very little difference in room temperature were H-phase and glass. Schedule B + F, using
flexural strength when compared to non-heat a shorter time but higher heat treat tempera-
treated material. X-ray diffraction of this ture of 1700C, resulted in a further strength
material revealed the presence of H-phase but reduction. As expected, this higher tempera-
no glassy secondary phase. The 1200C MOR ture produced more glassy secondary phase
was 59 ksi. No significance was attached to material. On the other hand, when small
A G 111.3(5)
A+C H_Yi g 99.3(5) 71.5(I)
B H lO4.9(3) 58.7(2)
B+D H+g 73.2(3)
B+E Yi+K 117.1(3) 69.1(1)
B+F G 66.o(3)
* Notations:
1. Heat Treatments
A = As HIPped rotor (No H.T.)
B = Complete rotor, 96 hours at 1450C
C = One half rotor, 16 hours at 1450C followed by 36 hours at 1450C, followed
by 96 hours at 1450C
D = Test bar, 96 hours at 1450C
E = Test bar, 96 hours at 1450C with packing powder
F = Test bar, 36 hours at 1700C
2. Secondary Phases
G = Glass (major); g = glass (minor)
H : YsSi3012N; K : YSiO2N; Yi = Y2Si207
3. Strength
Loading Rate: 0.5 ram/rain
Sample size is shown in ( ) following the strength value (average)
318
specimens were packed in powder and heat the glass recrystallized as H-phase. With
treated using schedule B + E, reduction in either heat treatment, however, stress rupture
strength did not occur• In fact, the highest was not improved at the 1200C temperature
strength of 117 ksi was obtained• Phases and 20-30 ksi stress level. In all probability
produced by this schedule were B-silicon sufficient residual glass, although not detected
nitride, K phase and Y2Si20 7. by x-ray analysis, was present to cause sample
deformation and oxidation.
g) Stress Rupture of RM-2O Rotor Material
In the previously described MOR experi-
The stress rupture characteristics of ments, heat treatment of the test specimens
RM-20 rotor material are shown in Table 66. in packing powder resulted in conversion of
Stress rupture, as in previously described MOR the glassy phase to K-phase (YSiO2N). Unfor-
tests, was measured in 4-point bending• Stress tunately, program timing did not permit these
levels evaluated were 30, 40 and 50 ksi and experiments to be extended to stress rupture
temperature levels were 800, 1000 and 1200C. evaluation. Future testing should address this
Measurements were made on RM-20 material form of heat treatment as a possible means of
prepared as follows: extending the capability of RM-20 silicon
nitride.
Group 1 - Test specimens cut from "as-
HIPped" rotor h) Development of Improved RM-20 Rotor
Material
Group 2 -Same as above but test specimens
heat treated 96 hours at 1450C Failure of the HIPped RM-20 material to
adequately address the AGT rotor stress rup-
Group 3 -Test specimens cut from a rotor
ture requirements initiated a search for other
that was previously heat treated 96
hours at 1450C possible compositions. The short time remain-
ing on the contract, however, discouraged any
As shown in Table 66, the as-HIPped mate- drastic modifications of our present approach
rial sustained over 200 hours without failure at or material. Recent information cited in the
a stress of 50 ksi and test temperature of literature (13, 14) pointed to ZrO 2 additions as
800C. At 1000C under the same load, speci- sintering aids capable of improving the
men failure occurred in 1.1 hours, however, at strength of silicon nitride. Zirconia seemed an
the lower load of 40 ksi, this RM-20 material ideal candidate for investigation--it has the
again sustained over 200 hours of testing at potential for overcoming RM-20's limitations
1000C without failure• At 1200C, the mate- while being relatively easy to test and imple-
rial failed in 1.3 hours at the 40 ksi load. ment.
Failure analysis of the specimens showed evi-
Hot pressing was chosen as the initial
dence of slow crack growth, as well as oxida- means of consolidating the powder mixtures of
tion. At 1200C and 30 ksi, the material did
partially-stabilized zirconia (PSZ) and RM-20.
not fail up to 140 hours of testing• However,
It permitted more rapid assessment of the
visual inspection of the specimen during the
composition's potential properties and, to
test revealed bending• X-ray analysis of this
some extent, the sinterability of the material•
as-HIPped material confirmed the presence of
Hot pressing time can be a measure of the
glass in the secondary phases, accounting for
amount of liquid phase present- the more
the deformation.
liquid, the shorter the time required to hot
The Group 2 and 3 heat treatment experi- press- and the amount present generally cor-
ments were designed to eliminate this sec- relates well with sinterability. However, if a
ondary glass phase. X-ray analysis in both particular composition emerged as a likely
cases disclosed recrystallization of the glass. candidate, a parallel study, undertaken to
In the Group 2 heat treatment of the test evaluate its slip-casting potential, would also
specimen, Y2Si207 was formed. In Group 3, be used to evaluate sinterability.
319
Table 66. Stress Rupture Test Results RM-20 Rotor Material.
* X-RAY DATA: B + G
* X-RAY DATA: B + Yi
* X-RAY DATA: B + H
.320
Various PSZ and RM-20 powder batches of transformation. The presence of both silicon
200 grams each were mixed for 2 hours in nitride phases in these samples may account
half-liter polyethylene bottles with absolute for their total deterioration during oxidation.
alcohol as a vehicle. A dozen hot pressed In the other samples, oxidation was directly
silicon nitride milling media (1/2 in long x 1/2 proportional to the amount of PSZ present.
in diameter) were included to facilitate mix- The only exception occurred between samples
ing. The powder mixtures were ready for hot IV and V, where the additional alumina in V
pressing after removal of the milling media appeared to alter the effects of the additional
and evaporation of the alcohol. PSZ.
The mixtures were hot pressed in a graph- Although additions of PSZ to the RM-20
ite die lined with molybedenum foil at 4000 material might ultimately have improved room
psi. The cycle time required to hot press was temperature rotor performance, the oxidation
defined to be from the time the die punches test clearly revealed its "Achilles heel" and
started to move until the motion was less than further testing was discontinued.
0.001 in./15 min. The resulting hot pressed
TASK 2.7 - STATOR - FORD
billets were 6.67 mm in diameter by approxi-
mately 1.75 mm in thickness.
Introduction
The compositions and the initial results of The stator configuration selected for the
these experiments are summarized in Table AGTI01 engine was of a 19-vane, radial flow
67. Also included in this table are three
design. Nominal overall dimensions were:
samples of the same composition which were
slip cast and sintered. All of the hot pressed Outside diameter 7.0 inches
samples achieved greater than 99 percent of Inside diameter 5.2 inches
their theoretical density. It should also be Total thickness 0.6 inch
noted that the PSZ containing samples were
hot pressed in much shorter time than the base Design alternatives considered were (a) a
RM-20 material. This suggested the likelihood stator assembled from individual vane seg-
of good sinterability. Indeed, the first slip ments and (b) a monolithic configuration hav-
casting and sintering attempt achieved densi- ing one solid and one segmented shroud. The
ties as high as.98.5 percent of theoretical. latter configuration was designed to reduce
thermal gradients which could result in exces-
Both the hot pressed and sintered samples sive stresses during transients.
were sectioned for further study. Test speci-
mens were cut from each of the billets for use Several potential advantages were inherent
in a static oxidation test and other evalua- in the monolithic construction:
tions, such as MOR, creep, thermal expansion,
o Ease of Handlin[_- One large part versus 19
etc. The static oxidation results (Figure 357),
discouraged any hopes that PSZ additions pieces would be processed through all
could overcome RM-20's limitations. All of stages of fabrication and assembly.
the ZrO 2 containing samples exhibited poor
O Reduced Machinin_ Costs- There would be
oxidation resistance, as evidenced by the dis-
a maximum of four surfaces and no critical
coloration of their initial dark appearance.
circumferential stack-up tolerances requir-
The dramatically different results obtained in
ing machining.
samples of similar composition warrants fur-
ther comment. The abbreviated hot pressing o Reduced Leakage- Leak paths through the
cycle used to achieve full density in composi- shrouds would be reduced by one half.
tions Ai, Bi and Ci (where unreacted raw
materials were used in place of RM-20), was o Experience- Ford had already demon-
too short to complete the alpha-to-beta phase strated the capability of monolithic axial
321
Table 67. The Effect of PSZ Addition to RM-20 Si3N 4 Material.
Hot Pressed
Weight Percent
(*) (A) Alpha Si3N4, (B) Beta Si3N4, (Z) ZrO2, (Y) Y2Si207, (H) Y5Si3012N ,
(K) YSiO2N , (G) Glass (major), (g) glass (minor)
322
1000°C - 100 hrs.
stator molding for the 820 engine program. location. Both can influence melt front weld
(1,15) Molding and forming this component lines and significantly affect component
of individual vane segments was readily strength. For the AGT stator, a diaphragm
supported by existing inhouse technology gate along the inside diameter of the solid
and that of other suppliers. shroud would prevent weld lines in the shroud.
However, the vanes and segmented shrouds
Based on these advantages and seeking to
would be filled in parallel, constricting the
advance the technology of complex shape
flow through each vane to 5 percent (1/19) of
forming, Ford elected the challenge of a mon-
the machine maximum flow rate. Conversely,
olithic stator and worked on this design until
a single point gate (at any location) would
February, 1984 when lack of funding caused
produce a shroud weld ]ine but permit a flow
elimination of this effort.
rate through each vane of 50 percent machine
Flow Modelinl_ maximum by filling paired vanes sequentially.
Among the many important parameters for Cornell University was contracted to con-
injection molding tool design are gate type and duct computer flow modeling studies to ex-
323
amine the influence of flow rate, material lation and operational check out. Several
temperature and die temperature on the vane deficiencies were related to installation and
fill pattern (16). Of primary concern was the construction. The platens of the vertical
possibility of inadequate fill or the formation molding machine were bowing, transmitting
of weld lines in the thin trailing edge of the the clamping forces at the tool perimeter,
vane. leaving the central section completely unsup-
ported. The platen deflection pattern was
Their studies indicated that, for the ideal-
measured and circular shims installed at the
ized isothermal case and projecting flow rates
tool/platen interfaces to correct the problem.
<50 percent of those anticipated through a
Dimensional measurements of molded stators,
diaphragm gate, good vane fillwould occur as
however, suggested that internal tool compo-
shown in Figure 358. In this case, the melt
nents were deflecting. Specific ares of de-
front at the trailing edge advances to the
flection were measured during molding trials
segmented shroud before the shroud fills.
and locations which required internal stiffen-
However, projecting an unheated tool and the
ing were identified. Also, cold weld lines were
expected flow rates for a diaphragm gate, the
occurring in the trailing edge of the vane. The
model predicted complete freezing of the melt tool was returned to the vendor for correction
front along the trailing edge before reaching
of the internal deflection problems and en-
the shroud. Only back flow from the shroud
largement of the cavity to increase the vane
would complete the vane trailing edge, result-
trailing edge thickness from 0.030 to 0.040
ing in a cold weld line. As the flow rate was inch.
increased to that predicted for a point gate,
the melt front approached that of the isother-
Molding Development - Diaphragm Gate
mal case. Thus the study emphasized the need
for precise die temperature control and flex-
Stator molding was initiated using the
ibility in design of the gate region to facilitate
0.010 inch thick gate; 12 full and six short
changes in gate configuration.
shots were made. The fillpattern observed on
Tooling Design the short shots was non-uniform as shown in
Figure 360, Views (a) and (b). Complete cavity
The stator tool design (Figure 359) incorpo-
fill was achieved as indicated in Figure 360
rates three independent water temperature
View (c).
control circuits. Five cavity pressure trans-
ducers and four thermocouples are included to
Measurements of the gate material at the
monitor and control molding parameters.
inside diameter of the solid shroud revealed
Removable die inserts enable rapid changes in
that the actual gate size varied from 0.006 to
gat ing.
0.014 inch. This variation was the result of
Previous experience in the injection mold- eccentricity between the tool details which
ing of complex-shaped components related the form the gate. The direction of eccentricity
occurrence of cracks in the molded part to the matched the fill pattern seen in the short
sequencing of insert removal and parting of shots. This is, the cavity area first to fill was
the die. Consequently, considerable effort at the larger gate dimension. Full shots had a
was spent in designing flexibility into the tool. weld line in the solid shroud opposite the
This included independent sequencing of the larger gate area.
two sets of 19 inserts forming the vane con-
tour. In addition, the die was designed to Seven of the full shots were visually in-
independently sequence the gate parting line spected for defects in the vane trailing edges.
before opening the die and ejecting the stator. In general, the trailing edges were sound with
over half the vanes in each stator having no
Tool DeveloPment
observable defect. Trailing edge knit lines, or
Initial development work on molding the signs of cold packing, were found in the re-
AGT stator was directed toward tool instal- mainder of the vanes. Three types of typical
324
Vi EW xx
VANE
SEGMENTED
SHROUD
! I
VIEW zz
325
g
I
Figure 359. Stator Tool.
trailing edge conditions are shown in Figure thick and an extensive parametric study was
361. The relative frequency of each type of conducted. Stators were molded at material
vane was: temperatures of 200, 250 and 275F and tool
temperatures of 90 and IIOF. Several shots
Vane Average Vanes
were also made at varied injection pressures.
Appearance per Stator
No defect I0.7
The first series of shots was made at
Knit lines 1.3 material and tool temperatures of 200 and
90F, respectively. These stators were visually
Cold packing _. 1
inspected and compared with stators molded
The tool insert forming the gate was re- using the eccentric gate and identical temper-
worked to make a concentric gate 0.015-inch atures. The data are summarized below:
ORIGINAL PAC!,_ Ig
326
10]_ _OOR QUALITY
_GOl_ QUALITZ
327
Gate Knit Cold No
t_
Configuration Lines Packing Defect 2O
t_ 18
Eccentric 1.3 7.0 10.7 ae
w
(0.006 - 0.014 n 16
inch) 14 _
Z __" 90*F
_
12
Concentric 6.0 17.0 0.6
u.
0
(0.015 inch) I0
0_
8
The overall condition of the stators had z 6 _
obviously degenerated significantly and vanes w
4
appeared which had both knit lines and cold ¢Y Z _
packing flaws. u.I
I I I I
0
The effects of material and tool temper- 2oo 225 250 275 300
328
,0_, i:O.i)i :, QJAI,YI'_
(a) (b)
uJ
temperatures ranging from 225 to 275F at a z
14
constant tool temperature of 80F. The results
Q IlO°F
indicated that with the thick gate: W 12 (
I0
o Uniform radial fill occurred at all temper-
atures. 8
0
6 90°F
o Virtually t no cold packing appeared in the TOOL TEMP.
/
vane trailing edges. 4 -
Z
2 -
o Knit lines were evident in all vanes. W
0
W 2O0 225 250 275 500
Knit lines became "tighter" and less ob-
vious with increasing materifil tempera- MATERIAL TEMPERATURE (OF)
ture.
Figure 365. Relative Frequency of
o Vane or vane/shroud fillet cracks were Vane Cracks as a Function of Material
329
Parametric studies with the diaphragm original gate at the solid shroud inside diam-
gate configuration revealed that no combi- eter.
nation of conditions was likely to produce
flaw-free parts. However, it was clearly evi- Short shots disclosed that a circumferen-
dent that all three defects (knit lines, cold tial fill pattern developed with a uniformly
packing and cracks) could be significantly thick melt front (Figure 366). When full shots
altered. were made, there were no signs of trailing
edge knit lines or cold packing. The fullshots,
Cracks in the vane trailing edge or the however, revealed a localized "hot spot" in the
vane/shroud fillets were attributed primarily shroud near the gate. Changing the injection
to tensile loads on the stator during die open- hold times before tool opening and ejection
ing. The entire conical runner section usuall_ resulted in stators with either "pull-out" of the
adhered to the upper half of the tool, breaking shroud material or shroud cracks (Figure 367).
off at the gate during opening. The most
frequent cracks occurred when using the Fourteen full shots were made during a
thicker gate which developed higher loads. study of the effect of gate size, flow rate and
The thin gate shots at lower tool and material tool temperature on the pull-out and cracking.
temperatures were not cracked as shown The material temperature and injection pres-
earlier in Figure 361. At higher temperatures sure were held constant at 250F and 1800 psi
cracks appeared, believed to result from ad- (9000 psi equivalent cavity pressure). The
herence of the part to the tool. Crack preven- gate size, flow rates and tool temperatures
tion appeared to be a function of the loads investigated were:
borne by the stator during tool opening.
Gate size - 0.015 x 0.5 - 0.015 x 1.0
Molding Development - Single Point Gate (inch)
Flow rate - 4.4 - 8.8
Improvements in tool gating could resolve (in3/sec)
all three problem areas. Switching from the Tool temp (F) - 70 - 90
diaphragm gate to a single point gate had the
advantage of: All 14 stators had either pull-out or cracks,
but no strong correlation between any of the
O Sequentially fillingvanes; effectively in- above parameters and flaw type was evident.
creasing the flow rate and eliminating Since the machine was being operated man-
trailingedge knit lines. ually during the study, significant variations
occurred in the injection molding sequence
o Developing a thick melt front while filling times (injection hold, tool open and ejection).
the vanes and eliminating the cold packing. The timing of these events was available from
analog instrumentation recordings of cavity
o Reducing the gate cross-sectional area, pressures for each shot.
I minimizing the load required to break off
the gate runner during tool opening. The flaw types were quantified and plotted
as a function of time as shown in Figures 368
One potential disadvantage was expected. and 369. Pull-out was quantified by measuring
The circumferential fill pattern would result the length of chord of the affected area.
in one solid shroud weld line 180 degrees from Cracks were quantified as the number of op-
the gate. ticallydetectable cracks in the stator shroud.
A cone-shaped metal insert was fabricated At a tool temperature of 70F, pull-out was
to fillthe original runner cavity. A one-half reduced to zero when the tool opening time
inch wide radial slot was then cut into the exceeded 14 seconds from the start of injec-
insert, running from the central sprue to the tion. Cracks appeared only when ejection
330
_ ii_ _ i i_ _ _ _
Figure 366. Short Hot Fill Pattern When Using Single Point Gate.
(a) (b)
331
Seventeen additional stators were modeled
z
o
F
0 I0 20
i
30
I
4O
utilizing
the
tures,
size,
time
an
the point
higher
window,
overflow
injeetion
at the
gate
lower
to
pressures,
solid
further
material
shroud
larger
weld
investigate
tempera-
gate
line
TIME BEFORE TOOL OPENING (sac.) and use of a hot sprue bushing. Preeise
control of hold times for tool opening and part
• GATE O.OI5 x 0.5 IN.
ejeetion. Effeetively prevented pull-out and
o GATE O.OI5 x I.O IN.
solid shroud eracks. None of the other vari-
°iF f
ables had a significant effect on molded part
=5 quality.
OO
332
were re-inspected: 23 of the batch intended Leading edge cracks were found in all of
for further testing and 10 others molded the test candidate stators,averaging 7.5 vanes
during development studies. A summary of per stator and ranging from 1 to 13. Trailing
the inspection findings relative to leading and edge cracks appeared in an average of 2.8
trailingedge cracks ispresented in Table 68. vanes per stator; and ranged from 0 to 12 in
Stator
" Serial LE TE Total
Number Cracks Cracks Craeks
S 1206201 12 4 16
H 02 7 1 8
I 02 8 0 8
P 04 3 0 3
P 05 4 1 5
E 06 6 16 18
R 07 u_
08 4 8 12
1208201 9 2 11
C 02 11 0 11
A 03 11 0 11
N 04 5 0 5
D 05 5 7 12
I 06 6 0 6
D 07 9 6 • 15
A 08 1 0 1
T 1209201 13 4 17
E 02 4 8 12
S 03 9 1 10
04 8 0 8
05 11 1 12
06 7 3 10
07 13 1 14
08 7 5 12
D 0113201 0 0
E 027206 0 0
V S 1129203 18 18
E T 04 17 17
L U 1130203 4 4
O D 1202202 5 5
P I 1203201 5 5
M E 04 5 5
E S 05 3 5
N 06 4 4
T
333
number. Six stators had no trailing edge
cracks. The ten experimental stators had a
B
significantly different crack distribution; two 24
had fillet cracks and none had the typical _20
trailing edge cracks. (These ten stators, how-
w[ 8 m
ever, had other defects).
z
-;16
Although 23 stators were molded under
14
nominally identical conditions, some process _-
variability occurred. Size parameters were _n 12
identified which showed significant shot-to- _ I0 m
17 191 2 4 6 8 I0 12 14 16 18191
front to rear, at to
VANE NUMBER
Figures 370 and 371 show the frequency of Figure 371. Frequency of Cracks Relative
cracks relative to vane numbers. Leading to Vane Number (Trailing Edge).
edge cracks occurred I00 percent of the time
where no cracks occurred (vanes 14 through
24 - 17).
-- Z2
LJ
Plots of vane cracks versus injection times
zo
144 (tI, to and tE) are shown in Figures 372 and
373. No clear pattern or trend appears for
leading edge "cracks. For the trailing edge
..I
cracks, however, die open time (to) appears to
(n influence crack frequency where increasing to
•." 12
U reduces cracks. No cracks appear when this
variable is greater than 16.1 seconds. Cavity
U.
o
e_
u_
i1o
z
8
0 I
_7 le
I I
2 4 6 _ i_ i_
/I
14 is
I I
_igl
I I
pressure did not correlate with either type of
crack.
Significant differences
frequency
batch and the 10 experimental
were found
of fillet cracks between
in the
24-stator
stators which
were inspected (Table 68). Two of the latter
I VANE NUMBER
were crack-free. All ten had no trailing edge
Figure 3?0. Frequency of Cracks Relative cracks. In addition, the frequency of leading
to Vane Numbers (Leading Edge). edge cracks in these stators could be sum-
marized in three categories: no vanes cracked,
at vane number 19 in the center of the gate all vanes cracked or approximately 25 percent
region. Vanes 8, I0 and 12- opposite the of the vanes had cracks.
gate- had no cracks in any of these stators.
Trailing edge cracks were more randomly dis- Ten variables were identified which could
tributed, but a four-vane segment existed be used to compare the two batches of stators
334
16
14
I Q
Q•
z
I0
$ m
= 8
_0
6 QO
OOQ
• QO
4
I 1 I I I I I I I I I I I I I I _ I I I t i 1
2 4 6 8 I0 12 14 16 18 20 :)2 z4
0
SHOTTIMES(SECONDS)
_ 12 $ • •
_ 10
00 • •
= 8
w
z
6
_ 4
z 2 Q •
2 4 6 8 10 12 M 16 i8 20 22 24
SHOTTIMES(SECONDS)
335
relative to leading edge cracks. The variables Table 69 shows the value or range for these
were: variables for the best and worst shots of the
24-batch stators and the three groupings for
o Gate type (full 360 degrees versus arc the developmental shots. Three variables
segment) stand out as being unique to the best develop-
mental shots: gate type, sprue type and injec-
o Sprue type (standard tapered versus hot tion pressure. The eccentric, full 360 degree
sprue) gate had previously produced a fill pattern
essentially the same as an arc-segment gate.
o Injection pressure (hydraulic pressure set- Therefore this variable was considered insig-
ting) nifieant in the development of leading edge
cracks. However, sprue type and injection
o Melt temperature setting pressures were potentially important param-
eters influencing leading edge cracks.
Mold temperature
top half In summary, a review of all available data
bottom half regarding the leading and trailingedge cracks
in the vane-to-segmented-shroud fillet sug-
Injection times gested that four variables had influenced the
cracks:
inject and hold
time to die open o Gate location - allpoint gate (arc segment)
time to ejection shots were made with the gate in the same
location which may have masked another
o Cavity pressures (residualat to) tool problem.
No. of Variables
Leading
Edge Gate Sprue lnj. Melt Mold, Temp. Inieetion Times PCAV at
Cracks Type Type Press.
TemP. (Top) [ (Bot.) (lnj.) I (Open)I (Ejet.) topen
0.015
Shipper X
600 -
Best (1) 3.0 Hot 1980 225 90 90 5.5 16.5 21.5 800
0.015
Shipper X
800 -
Worst (1) 13 3.0 Hot 1980 225 90 90 4.5 15.3 21.3 1600
Full
Eccentric
Other 0.015/ 900 - 225 - 80 - 80 - 5.5
Best (2) 0.025 Taper 1500 240 95 95 8.1
0.015
Other X 1800 - 200 - 70 - 70 - 5.2 12.4 15.6 500 -
Fair (6) 3-5 3.0 Hot 1980 250 90 90 8.1 20.8 30.6 2500
0.015
Other X 5.9 - 14.1 - 20.0 - 600 -
Worst (2) 17 - 18 3.0 Hot 1800 250 75 75 8.6 14.5 21.6 1000
336
O Sprue type- the only stators without lead- Each of the three other variables showed
ing edge cracks were made with a standard an improvement over the repeat shots in terms
tapered sprue. of filletcracks. However, at lower injection
pressure, the parts experienced solid-shroud
o Injeetion pressure- developmental shots pull-out and cracking at the edges of the gate,
made with reduced pressures had no lead- due to localized overheating. This problem
ing edge cracks. persisted when all three variables were com-
bined. A similar pattern was observed to a
o Die open time- trailingedge cracks were lesser degree in the 24-batch stators. Again,
reduced with longer times and none ap- the difference might have been a function of
peared for to >16.1 seconds. material batch inconsistency. This investiga-
tion indicated that the variables identified
Molding Investigations and Development significantly influenced the development of
leading and trailingedge filletcracks.
Molding studies investigated each signif-
icant variable. Stators were molded repeating In order to reduce localized overheating in
the same conditions as used for the 24-stator the gate region, and to continue stator mold-
batch. Several shots were made, changing ing development, the gate size was increased.
only one variable from the baseline conditions. An insert was installed which increased the
Finally, shots were made combining all three gate width to 0.065 inch, maintaining an arc
variable changes. All of the stators were then length of 3.0 inches. Preliminary shots showed
inspected with particular attention given to that the overheating problem was corrected.
the leading and trailing edge fillets at the
segmented shrouds. The inspection results are A parametric study was initiated to ex-
summarized in Table 70, along with compara- amine the effects of material melt temper-
tive data from the baseline. ature. Ten shots were made over the temper-
ature range of 225 to 270F. These stators
The six shots replicating the 24-batch con- were visually inspected for all types of flaws.
ditions generally repeated the baseline results. The inspection results are summarized in
The variance in the number of leading edge Table 71. The total number of flaws should be
cracks may reflect material batch incon- compared to 10.3 flaws per stator observed in
sistency. When the gate was rotated during the batch of 24.
these shots, the crack pattern followed the
gate, indicating a flow-related phenomenon Further molding process improvements and
rather than a localized tool problem. tool temperature measurements indicated that
Number of Shots 24 6 4 4 4 3
337
Table 71. Material Temperature Investigation 0.065 X 3.0 Gate.
Number of Shots 2
Notes:
trailing edge cracks could be related to the Table 72. Stators Delivered to Garrett.
temperature of the inner inserts which form
the vane trailing edge. As no water temper- Number of Cracks
ature control circuits were available in that Stator
region of the tool,-auxiliary electrical heaters _N LE TE
were installed. However, because of budget
cut-back, no funding was allocated to continue 1215202 1 0
the investigation. 1221306 0 2
1110308 1 4
Lack of funding for stator molding devel- 1130306 1 0
opment and the concurrent availability of 0125408 0 3
single stator vanes, caused this effort on a 0221406 1 2
monolithic, 19-vane stator to be dropped in 1206203 9 0
February 1984. As of that time, twelve 1206206 8 13
stators were delivered to Garrett for evalu- 1020307 1 4
ation. Two of those delivered had only one 1206308 2 1
crack each. Table 72 summarizes leading and 1208205 5 7
trailingedge cracks of these stators. 1209206 7 3
TASK 2.7 - FLOW SEPARATOR HOUSING ture for hot flow path components and pro-
vides a sealing surface for the rotating heat
Introduction exchanger.
The flow separator housing is a ceramic The material selected for this component
component that channels the gas flow through is a low thermal expansion lithium aluminum
the heat exchanger, acts as a support struc- silicate(LAS) ceramic, made by Corning Glass
338
Works as their Code 9458 LAS. The process
for making the flow separator housing consists
of slip casting an aqueous suspension of
crushed glass into the desired shape in Plaster
of Paris molds. The component then is re-
moved from the mold, dried, sintered, and
diamond-machined, as required.
.S
N_ 14 .0209 _
1.0196 .,_
Z= 13
.o,87
_.0181 _.
"_.0173
-".0164
o
...1
_ 9 <¢
n,-
_,J
I 1 I I I I I I I "I"
w I--
z 0 400 800 I?,.00 1600 2000
I..-
TEMPERATURE ('F)
Figure 375. Thermal Conductivity of Corning Code 9458 Lithium Aluminum Silicate.
339
The thermal expansion of 9458 shown in subjecting them to temperatures varying from
Figure 374 is characteristic of beta spodu- 1800F to 2200F (in increments of 100F) for
mene-type ceramics. The material undergoes 500 hours at each temperature. Measurements
negative expansion from room temperature to were made on cube faces prior to the test and
approximately 300C, followed by a much at 250-hour intervals during exposure, with an
sharper positive expansion up to 900C. optical comparator and a series gage block to
measure dimensional changes. This technique
The flexural strength data in Figure 374 was accurate to _10 ppm. Results of this test
shows a slight decrease in strength over the are shown in Figure 377. The Corning 9458
range from room temperature to 500C. Above LAS material retained 100 ppm stability up to
500C the strength increases, indicating the 210OF. Above 2100F, additional contraction
possibilityof microcrack healing. occurred, and the material fell below the
lower limit of- 100 ppm.
Thermal conductivity, based on measure-
ments of specific heat and thermal diffusivity, Meehanieal Testing
was averaged using two different techniques
(Figure 375). Unlike most ceramics, there is The flow separator housing is subjected to
an increase in conductivity with temperature. thermal and mechanical loads in the engine.
In order to provide some assurance that this
Figure 376 shows the modulus of elasticity component will sustain the mechanical loads
of 9458 LAS. The MOE is approximately and to eliminate defective housings early in
processing, a test fixture was designed and
fabricated to duplicate the engine static oper-
TEMPERATURE ('F) ating pressures on the housing.
- 592 752 1112 1472 1832
x 11.5 The test fixture, assembled with a wooden
model of the flow separator housing is shown
in Figure 378. The fixture is designed to
__ II.O support the housing, simulating engine mount-
ing conditions and sealing the housing to the
fixture with rubber gaskets. Hydrostatic
_. 10.5 pressure loads could be applied within a con-
tainment vessel available at Corning. Lifting
ua I0.0 eyes assist in moving the assembly in and out
of the vessel. The upper plate is provided with
fittings for a pressure line and an air bleed
valve.
_ 9.5
/
340
"'--'-1800
OF 1900°F =I= 2000OF'--"_ 2100'F--_ 2200°F-'"
, _mi .
100
5O
A
E
0
e_
v
,- -50
._J
-I00
z
-150
-200 - O0
I I I I I I I I I I I I I I I I I
I I I I I I I I I I I
0 0 5OO 0 5O0
TIME (HOURS)
Figure 377. Dimensional Stability of Coming 9458 LAS Material at Various Times and
Temperatures.
Figure 378. Flow Separator Housing Pressure Test Fixture Shown Assembled to Wooden
Model of the Housing.
341
duct, the turbine shroud and the flow sepa- rejected due to very large casting voids in
rator housing. Thus the high pressure cavity is areas where mechanical and thermal stresses
sealed and loads can be applied to simulate were highest. During this period, a number of
engineoperating pressures. process modifications and mold changes were
effected. These improvements, coupled with
Each flow separator housing was tested at an acceptance specification that permitted
a pressure 25 percent greater than the maxi- casting voids in non-critical areas of the hous-
mum mechanical load exerted on the compo- ing, resulted in additional acceptable compo-
nent at full engine speed. All components met nents for delivery to Garrett. In summary, for
the 65 psi mechanical load specification. a period of five years up to April 1985, the
accept/reject ratio for flow separator housing
was approximately 1:2. At this point in the
Strain Gage Measurements
AGTI01 program, the decision was made that
housing quality permitted housings to be
The flow separator housing mechanical test
shipped directly from Corning, and the Ford
ratus but also permitted the correlation of 3D
inspection technology was transferred to
stress analysis with mechanical stresses en- Garrett.
countered in engine operation. Fourteen uni-
axial and 17 triaxial strain gages were
CONCLUSIONS AND RECOMMENDATIONS
attached to SN-8 in critical areas, as shown in
Figures 379 and 380. Strain gage data were
This report covers material and process
recorded up to 60 psi in increments of 4 psi in
developments by the Ford Motor Company on
both air and water environments.
three key components of the AGTI01 gas
turbine. These components are the i) silicon
Component Fabrication nitride turbine rotor 2) reaction-bonded silicon
nitride one-piece stator, and 3) lithium alum-
The initial phase of component fabrication inum silicate flow separator housing. The
consisted of wooden model machining, pattern following are conclusive remarks and recom-
design, pattern fabrication and Piaster of mendations for future work on each of these
Paris mold construction. A series of slip activities.
casting experiments was designed to test the
feasibility of casting a relatively flaw-free Rotor Development
flow separator housing. These experiments
revealed the need for a number of design o Two materials - sintered, reaction-bonded
modifications, particularly a double bulkhead silicon nitride (SRBSN) and sintered silicon
wall (Figure 381). With this double wall, nitride (SSN) - were investigated using the
casting could be achieved without the inci- fugitive wax slip casting process to form
dence of very large voids at the junction of AGT rotors.
the outer wall/bulkhead and bore/bulkhead.
342
Figure 379. Ceramic Flow Separator Housing Showing Strain Gages In Place.
o Test bars cut from RM-20 rotors did not ondary phase which affected the stress
have the same material quallity as mater- rupture properties of RM-20.
ial cut from a billet. These findings
o The glassy secondary phase was reduced,
emphasized the importance of developing
but not eliminated, through heat treat-
and fabricating components of test bar
ment. This heat treatment, when done in
quality.
the absence of packing powder, also re-
sulted in reduced flexural strength. It is
O HIPping of RM-20 rotors versus pressure- recommended that future heat treatment
less sintering resulted in material closest
by accomplished in packing powder.
to billet/test bar quality.
o Crack-free rotors were produced and cold
o Both pressureless sintered and HIPped sil- spin tested to failure speeds in excess of
icon nitride rotors showed a glassy sec- 1009000 rpm.
343
Figure 380. Ceramic Flow Separator Housing Mounted to Mechanical Test Fixture.
O Pore size in the rotor material was most wax process. Successes in this area will
important as related to ultimate failure require improved injection molding binder
speed. Future work should focus on reduc- systems permitting binder burnout of thick
ing pore size as well as total porosity. section ceramic components.
o Slip casting using the fugitive wax proce- Reaction Bonded Silicon Nitride Stator
dure is a viable process for making proto-
type rotor components. Future work using O Injection molding of the complex shaped,
this process should address: monolithic, radial stator was shown to be
feasible.
1) Shorter casting time
2) Increased slip suspension time Lack of funding during th AGT program
3) Reduction of pore size in the finished and concurrent availabilityof single stator
rotor vanes caused the effort on a monolithic,
19-vane stator to be dropped. At that
o For the long range, and particularlyfor low time, twelve stators were delivered for
cost, high volume production, the injection evaluation.
molding process and SRBSN is recom-
mended as a rotor material and forming o The molding development efforts revealed
porcess over slipcast SSN and the fugitive complex interaction of many molding
344
ORIGINAL PAGE IS
_01_ P.OOR QUALITY.
0RIG!NAU PA-GNIg
OE POORQUALITY
Figure 381. Ceramic Flow Separator Housing with Double Wall Bulkhead.
Table 74. AGT Flow Separator Housing Quality (Period 1980 - 1985).
FSH FSH
(No.) Quality/Co m ments (No.) Quality/Com ments
345
variables influencing several different complex components such as the flow sepa-
fabrication defects. As such, more exten- rator housing used in the AGT101 gas tur-
sive use of statistical experimental design bine program.
should be applied to resolve the relation-
ship to, and significance of each of the o The double bulkhead configuration of the
variables to specific flaw types. flow separator housing demonstrated the
importance of component design, not only
Computer flow modeling was shown to be a in meeting performance criteria, but criti-
very useful tool for providing direction in cal fabrication criteria as well. This de-
injection molding tool design and in estab- sign modification eliminated the incidence
lishing material flow rate requirements. of very large voids at the junction of the
Efforts should be continued to explore outer wall/bulkhead as well as the bore/
modeling techniques with specific emphasis bulkhead.
on the nonisothermal modeling of simple
shapes and experimental verification. o Although the components produced were
not totally flaw-free, nondestructive test-
Tool deflection and temperature control ing and proof test procedures that permit-
were shown to be critical considerations in ted casting voids in non-critical areas of
injection molding die design. These should the housing are feasible.
be evaluated analytically during die design
to reduce time consuming delays during This program demonstrated that slip cast-
tool tryout. ing is the correct process choice for fabri-
cating large complex components such as
Lithium Aluminum Silicate Flow Separator the flow separator housing in prototype
Housinff form. On a long range basis, however, it is
felt that a glass ceramic process will be
o Lithium aluminum silicate is a suitable required to attain cost competitiveness in
ceramic material for fabricating large high volume production.
346
REFERENCES
1) McLean, A.F. and Fisher, E.A., "Brittle 9)Govila, R.K., Mangels, J.A., Baer, J.R.,
Materials Design, High Temperature Gas "Fracture of Yttria-Doped, Sintered Reac-
Turbine," Final Report AMMRC Contract tion Bonded Silicon Nltride," J. Am.
No. DAAG 46-71-C-0162, (AMMRC TR Ceram. Soc., 68 (7),413-41 (1985).
81-14), March, 1981.
2) Mangels, J.A., Tennenhouse, G.J., "Densifi- i0) Govila, R.K., "Fracture of Flash Oxidized,
cation of Reaction Bonded Silicon Nitride," Yttria-Doped Sintered Reaction-Bonded
Bull. Amer. Ceram. Sot., Vol. 59, No. 12, Silicon Nitride," accepted for publication
(1980), p. 1216. in J. Mater. Sci. (1986).
6)Benn, K.W., Carruthers, W.D., "3500 Hour 14) Dutta, S. and Buzek, B., "Microstructure,
Durability Testing of Commercial Ceramic Strength and Oxidation of a I0 wt. Percent
Materials," Third Quarterly Progress Re- Zyttrite-Si3N 4 Ceramic," 67 [2], 89-92
port, DOE/NASA Contract DEN 3-27, (1984).
1978.
7) Hinsolt, G., Knoch, H., Huebner, H., 15)Arnon, N. and Trela, W., "Evaluation of
Kleinlein, F.W., "Mechanical Properties of Ceramics for Stator Applications- Gas
Hot Pressed Silicon Nitride with Different Turbine Engines," Final Report DOE/NASA
Grain Structures," J. Amer. Ceram. Soc., Contract No. 0019-83/1 (NASA
Vol. 62, No. 1-2, 1979, p. 29-32. CR-168140), March, 1983.
347
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348
APPENDIX C
349
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350
APPENDIX D
Acronym Definition
351
APPENDIX D
Acronym Definition
352
APPENDIX D
Acronym Definition
353
This Page Intentionally Left Blank
354
APPENDIX E
REFERENCES
I) Garrett Turbine Engine Company, "Ad- 7) Garrett Turbine Engine Company, "Ad-
vanced Gas Turbine (AGT) Powertrain Sys- vanced Gas Turbine (AGT) Powertrain Sys-
tem Development for Automotive Applica- tem Development for Automotive Applica-
tions," Semiannual Progress Report tions," Semiannual Progress Report Num-
Number 1 (October 1979 through June ber 7 (January 1983 through June 1983),
1980), NASA Report CR-165175, November NASA Report CR-174694, December 1983,
1980, Contract DEN3-167. Contract DEN3-167.
355
1 Report No 2 Government Acc_sion No 3 Recipient's Catalog No
CR-180891
4 Title and Subtitle 5 Report Date
15 _pptementary Notes
16 Abstract
This report is the final in a series of Technical Summary Reports for the Ad-
vanced Gas Turbine (AGT) Technology Development Project, authorized under NASA
Contract DEN3-167 and sponsored by the DOE. The project was administered by Mr.
Thomas N. Strom, Project Manager, NASA-Lewis Research Center, Cleveland, Ohio. This
report summarizes plans and progress from October 1979 through June 1987.
Project effort conducted under this contract is part of the DOE Gas Turbine
Highway Vehicle Systems Program. This program is directed at providing the United
States automotive industry the high-risk, long range technology necessary to produce
gas turbine engines for automobiles that will have reduced fuel consumption and red-
uced environmental impact. The intent is that this technology will be capable of
reaching the marketplace by the 1990s.
The Garrett/Ford automotive Advanced Gas Turbine has been designated the AGTI01
The AGTI01 nominally is a 74.5 kw (100 shp) engine r capable of speeds to 100,000 rpm
and operating at turbine inlet temperatures to 1370C(2500F) with a specific fuel
consumption level of 0.18 kg/kw-hr(0.3 ibs/hp-hr) over most of the operating range.
This final report summarizes the powertrain design, power section development,
and component/ceramic technology development. Appendices include summary reports of
progress from Ford Motor Company, AiResearch Casting Company and Pure Carbon, acting
as major subcontractors and suppliers of ceramic materials and components. Standard
Oil Company's Unique and Common work accomplished under this program is published
in topical report (TBD).
19 Security Cla_if (of this report) 20 SecurityClassif (of this _) 21 No of Pages 22 Price"
Unclassified Unclassified 384 A.]7
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NASA-C-168(Rev I0-75)