Imcadpe 01 19
Imcadpe 01 19
Imcadpe 01 19
The following case studies and observations have been compiled from information received by IMCA during 2019. To
ensure anonymity all vessel, client and operational data has been removed from the narrative.
Vessel managers, DP operators and DP technical crew should consider if these case studies are relevant to their own vessel
DP operation so that they can be used to assess and assist the safe operation of the vessel.
Any queries regarding this bulletin should be directed to Andy Goldsmith (andy.goldsmith@imca-int.com), IMCA Technical
Adviser – Marine. Members and non-members alike are welcome to contact Andy if they have experienced DP events which
can be securely analysed and then shared anonymously with the DP industry.
Divers informed to
Verifying thruster
return to bell clump
performance
weight
1525 Thruster
1509 Both divers on
confirmed fully
clump weight
operational
During diving operations in open water, tunnel thruster No. 1 tripped offline. Investigation showed that the cause
was due to tripping of the thruster hydraulic pump because of voltage instability. The voltage instability was caused
by a spike load on an unrelated circuit breaker on the same switchboard which tripped. Because of the voltage
drop on starboard 690V switchboard during the event some of the equipment breakers opened on under voltage:
Tunnel Thruster No. 1 due to power drop to hydraulic pump and signal command “External Shutdown” from
controller to frequency converter drive.
Starboard ER fans.
Thrusters remained on
A series of 10m moves high load, low speed
were made in ‘Move was selected and stop
up mode’ on track request
confirmed
Position setpoint
changed 140m and
heading setpoint
changed dramatically
A planned controlled
All thrusters
shutdown of the Total excursion
operational DP status
starboard switchboard approximately 100m
returned to green
was initiated
Technical team
DP status changed continue reinstating
Vessel on location
from advisory to breakers resulting from
on DP
yellow initial switchboard
blackout
Drilling operations
Vessel drifting
ceased
An AVR problem in diesel generator No. 1 engine caused an over voltage in the system. Due to increased voltage,
the standby machine could not be brought online, and the switchboard required a controlled blackout. After this,
many alarms from Network B were observed due to the supply being interrupted. An hour later, there was a total
loss of network communication affecting many field stations together with loss of DP communication to all
thrusters, which caused the vessel to drift off. The probable cause was accidentally resetting network A, when
trouble shooting of network B was taking place.
Further investigation of the overvoltage issue found a 3-phase breaker was faulty to engine No.1; the breaker was
replaced by an onboard spare. The DP system manufacturer concluded that the vessel was operational as designed,
indicating a possible human mistake by rebooting network A.
The vessel instigated a DP yellow alert whilst a fault was investigated. Considering the weather conditions and
nature of investigation the vessel should have either abandoned operations or been fully prepared to do so.
Given the circumstances, it is evident the vessel returned to normal operations too quickly and whilst reinstatement
of the system was still in progress. The root cause of the incident was not given in the report, but it is evident that
work involving the resetting of the network caused the loss of DP communication with the thrusters and subsequent
position excursion. While total network failure and subsequent drift off represents a DP incident, the initial failure
of the AVR only represents an undesired event.
Event 4: Loss of One Redundant Group – DP Undesired Event
11:03:57 – High
winding temperature 11:04:23 – ME No. 1
alarm No. 2 centre centre start requested
generator
A partial blackout of the centre high voltage (HV) switchboard at 11.04am caused by No. 2 generator. This caused
the loss of the 440V distribution board and thrusters No. 3 & 6. The centre generator No. 1 started and connected
onto the switchboard, there was no loss of power to the drill floor as this is fed from both port and starboard HV
switchboards. The power management system worked as expected, investigation found a poor connection to the
temperature sensor of No. 2 generator causing the temperature fluctuation.