5 KK Pillar
5 KK Pillar
5 KK Pillar
Activities
Presented By : KK Pillar Chairman
Date :
Presentation contents
Sr.
1 Background status
Contents
AIM - KK Pillar
Target - KK Pillar
Approach
Trend Graphs
Kaizen Status
2. AIM KK Pillar
KK PILLAR TARGETS
Parameter
Target Criteria
30 % up
Reduction by 50 % in
Minutes./Occ.
Reduction by 50 % in
Minutes./Occ.
Reduction by 50 % in
Minutes./Occ.
Reduction by 50 %
30%UP
variable conversion
cost - Model wise
1) Labour
2) Tool
3) Consumable
4) Power
5) Fuel & water
6) Material Yield
KAIZENS /MAN/YEAR
2 KAIZENS / MAN / YR
BM-DEC 05
Target
( 31.10.07)
ACTUAL
(31.07.07)
Master Plan
KK Activity
Approach
Cost Loss
OEE Loss
Cost Loss Tree
Define loss
Loss Tree
Kaizens
A v g M in s /M o n th
40000
30000
19530
20000
12349
10000
6269
5024
3822
Mar-07
Apr-07
2154
0
Bench Mark- JAN 06 TO
DEC 05
DEC 06
Jan-07
Feb-07
May-08
Month
Loss Details
S.N.
Bench JAN 06
MarkTO
Jan-07 Feb-07
DEC
DEC
05
06
Loss Desc
Tool change
KK
Setup
KK
Startup
KK
Measure / Adj
KK
Logistisc loss
KK
KK
Breakdown
PM
OT
Mar-07
Apr-07
May-08
Jun-07
Tool Change
Start up
Measurement
& Adjustment
-Quick change
-Elimination of setup
-Series to parallel
-Elimination
-Auto adjustment
-Internal to external
-Speed up
-Frequency reduction
-Elimination
-Auto Adjustment
-Auto start
-Improvement in 1S/2S
-Early start
-Method change
-Improvement in 1S / 2S
-Series to parallel
-Speedup
-Series to parallel
-Improvement in 1S /
2S
-Presetting
-Reducing occurrences by
increasing Tool Life
-Presetting
-Measurement
elimination
2000
7703
1800
7000
1600
5897
6000
1400
1200
4599
mins
5000
1000
4000
3000
2087
2000
316
1000
316
280
270
Bench
MarkDEC 05
Jan-06
Feb-06
Mar-06
2307
600
1534
950
248
11
800
2416
188
186
166
134
Oct-06
Month
Cell detail
S.N.
1 Cell No1
Total
4546- Gear Shaping min/occ
Target(min/occ)
Total
4- Cell no2
5039- Press min/occ
Target(min/occ)
Total
4- Cell no3
3927- Keyway min/occ
Target(min/occ)
Total
4- Cell no 4
5260- Keyway min/occ
Target(min/occ)
Total
Cell no 5
5411- Murata min/occ
Target(min/occ)
Cell no 6
Total
5359 - Gundrill min/occ
Target(min/occ)
Total
Total
min/occ
Target(min/occ)
Bench
MarkDEC 05
300
26
15
120
60
60
1666
36
36
1036
30
30
4680
40
40
7802
192
100
Jan-06
280
20
15
Feb-06
Mar-06
Oct-06
400
1054
768
131
95.5
200
0
M ins/O cc
8000
KAIZEN IDEAS :
1)
2)
3)
4)
Combination of Tools
Speed up of activities
Inside acivities changed to outside
Elimination of activities
Activity
Time in minutes
4.0
4.5
2.0
5.5
6
3.0
1.0
26 mins
BEFORE :
Gear to be cut
Cutter Adaptor
Cutter locating Diameter. Only one
cutter can be loaded
12 mm
AF TER :
Idea:
Cutter Adaptor
Modified Cutter locating
step to accommodate
spacer.
20 mm
Activity
Time in minutes
4.0
4.5
2.0
5.5
3.0
1.0
20 mins
RESULTS:
BENIFITS:
8%
Dec-05
Aug -07
Cell No 1
Cell No 2
Cell No3
Cell No 4
RESULTS
Summary of the Results Plant Tool Change time reduction
2000
BM-Feb01
BM Dec 05
Actual Jun 07
Mar.05
1800
Total time
BM-Feb01 1800
1500 Mar.05
620
68 %
6.3 %
1000
237
620
223
500
0
Total time
Production / hour
250
200
150
100
50
0
Nos.
Pressing
19
Machining
Fabrication
Painting
113
11
191
13
Total 42 Kaizens
11
Cell No-1
Cell No-2
Cell No-2
9
Cell No-4
120
200
10
REMOVE
Last produce componant
Take press on micro inch
Take Ram at BDC on inch
Unclamp blank holder & bed.Ensure it
Removing blank feeding conveyor
Take ram at TDC.
Take blank holder up by 130 mm
Take ram at BDC.
Unclamp punch manually
Take ram at TDC.
Lift moving bolster
Take moving bolster out
FIX
Take second moving bolster in
Position outer/ inner slide for new die
Take moving bolster down
Take ram at BDC.
Check gap between punch & inner slide
Take ram at TDC.
Position Inner slide shut height
Position centering of Die
Take ram to BDC
Clamp punch manually.
Take ram to TDC.
Position shut height of Outer slide.
Take ram at BDC.
Center adoptor plate.
Clamp blank holder / Outer plate
Clamp Inner slide & ensure
Clamp Outer slide & ensure
Take ram at TDC.
9 10 11 12 13 14 15 16 17 18 19 20
21
22
23
24
25
26
27
28
29
30 31
32
33
ADJUST
34 Run one stroke idle.
45.15
Minutes
45.15
Minutes - - 36
36 Activities
Activ ities
40.75 Minutes (4.4 Minutes Reduction)
39.5 Minutes (1.25 Minutes Reduction)
09.05 M inutes (30.45 Minutes Reduction) - 15 Activities
34
43
44
45
Element
ACTIVITY
Kaizens for set up & adjustment time reduction
Process : Pressing
Kaizen - Inside to Outside
BEFORE
ACTIVITY
Kaizen - Speed Up
BEFORE
AFTER
ACTIVITY
Kaizen : Speed up
BEFORE
AFTER
RESULTS
BEFORE
Minutes
50
45.15
80 %
40
Remove
30
BEFORE
AFTER
48 %
20
10
AFTER
9.8
9.8
5.05
Fix
23.65
23.65
2.9
5.05
Adjust Time/Occ
11.7
45.15
1.1
88 %
9.05
2.9
07 Kaizen
Ideas
Implemented
11.7
91 %
9.05
1.1
Better
0
Remove
Fix
Adjust
Time/Occ
Dec-05
08
Cell No 1
Cell No 2
Cell No3
Cell No 4
RESULTS
Summary of the Results Plant Set time reduction
2000
BM-Feb01
BM Dec 05
Actual Jun 07
Mar.05
1800
Total time
BM-Feb01 1800
1500 Mar.05
620
68 %
6.3 %
1000
237
620
223
500
0
Total time
Production / hour
250
200
150
100
50
0
Nos.
Pressing
19
Machining
Fabrication
Painting
113
11
191
13
Total 42 Kaizens
11
Cell No-1
Cell No-2
Cell No-2
9
Cell No-4
Results
Results
Results
Labour
Tool Cost
Modification of
Tool
Deletion / Combination of
operations
Method change
Reduce movement
Automation
Reduce material handling
Cycle time improvement
Motion loss reduction
Elimination
Standardization
Consumables
Elimination
Energy
Modify Equipment
Method Change
Alternate
Material
Auto Timer
Optimum utilization
Before
CBN Insert CCGW 09T304 BN250 is
used for boring dia.20 Gear Comp
Prim Drivn DK101129, 73117320.
After
High wear resistance PCD insert of
Grade DA2200 from Sumitomo tried and
regularised.
Before condition
After condition
Before condition
Oil carry over with components
Oil waste 0.22 Rs/Veh
After
After condition
Provision of Spinner to avoid oil carry over
with component.
Oil waste 0.05 Rs/Veh
Before
After
Before condition
No provision to turn OFF chilling unit
Power consumption is 174 Kwh/month
After condition
Provision to turn OFF chilling unit
Power consumption is 91 Kwh/month
3
2
Labour
Tools
Consumables
Energy
ACTUAL
BM
Rs/ Veh.
TARGET
BM
ACTUAL
TARGET
ACTUAL
TARGET
THANK YOU