Takniki Darpan - Issue 18
Takniki Darpan - Issue 18
Takniki Darpan - Issue 18
lekeâveerkeâer ohe&Ce
TAKNIKI DARPAN
Reflection of the achievements…..
Sh. B. Swain
Sh. S.Mandal INSIDE
Sh. Rajib Chakraborty
TITLE PAGE
EDITOR
MESSAGE FROM HEAD (TSX) 01
Sh. B. Swain
Email: djawade@bhelpswr.co.in
Mobile: 09423680639
Dear Colleagues,
Wish you and your family members a very happy and
prosperous new year. We have entered into the last quarter of
financial year 2014-15 and when we look at the achievements
and targets for the year, it is very clear that the path ahead is
going to be tough and challenging.
We have nearly 3500MW to be synchronized and around
4000MW capacity addition is to be achieved. Additionally, some
old projects such as GPPC Pipavav, GSEG Hazira and IEPL Belais
going to be re-started. In totality, the asking rate (to use a popular
cricketing parlance) has already become very high and we will
have to give really more than hundred percent to achieve our
targets.
This issue of TaknikiDarpan is an excellent compendium of
feedbacks received from various sites of PSWR. The feedbacks
are a nice collage of experiences and innovations from Power
Sector, Industry Sector as well as IO projects. It is also heartening
to observe that the contributions are from a wide spectrum of
employees ranging from General Managers to Engineer Trainees
who have spared time to write down the feedabacks so that it is
shared with others for betterment of our working. We sincerely
hope, these feedbacks will be useful in problem solving and
reducing time cycle during project execution.
Please give us feedback about this issue and also share with
us your innovations and experiences at site so that others will be
benefited from it.
Once again, best wishes and enjoy working.
B. Swain
AGM, TSX,
BHEL, PSWR, NAGPUR.
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January - 15
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January - 15
unit. It was observed that there was no level built up problem from no load to full load. Max level in LPH1
was +35 mm (min level was -125mm as per remote level transmitter) throughout the operation.
From the above it may be concluded that
1. There was air lock in the inverted U-loop in the drip line of LPH 1 to DC. By providing the continuous air
vent from the top of inverted U-loop, the air locking problem was overcome.
2. Due to high venting of LPH1 to condenser there used to be low DP between LPH1 & DC combination at
low load condition. Once the steam flow to LPH1 increased beyond the threshold limit (> 170MW), the
DP becomes more and the resistance of air locking in the inverted U-loop got overcome and heater
comes to service. By keeping the vent valve in the throttled condition also helps to maintaining
sufficient DP to make the drip flow from start of unit to full load.
NOTE:
As per the heater level control logic, there is no level control valve in the drip line of LPH1 to DC and from DC
to condenser. There is only one level control valve in the cascading drip line from LPH2 to LPH1. Under
condition of high level in LPH1, the same control valve will get close command diverting the drip from LPH2
to condenser directly isolating the LPH 1 from drip side. Condensate line inlet valve to DC will close and
outlet valve of LPH-1 to LPH-2 will close & bypass valve will be opened bypassing the heater from
condensate side. As per the layout and logic there should not be any level built up in LPH1 under any
condition from no load to full load if the isolating valve in the drip line of DC to condenser is kept full open.
Even with the temporary arrangement made at site there is level build up in LPH1 (from -125 to +35 mm).
This is because of the inverted U-loop which still exists because of site condition. This is also not the
intended operation of LPH 1.
SUGGESTION:
To correct the same, it is highly recommended to modify the LPH1 drip line suitably based on site condition
so that there the drain line will always have negative slope towards DC. Otherwise it will have an
unexpected effect of LP turbine last stage blades for which it is not intended or designed.
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Before changing feed back cam After changing feed back cam
Sl no HP sec oil HPCV 1 HPCV 2 HP sec oil HPCV 1 HPCV 2
Press opening opening Press opening opening
ksc mm mm (ksc) mm mm
1 2.4 2 2 2.4 1 1
2 2.78 5.5 6 2.5 2 2
3 2.9 7.5 7.5 2.8 6 6
4 3.4 21 16 3.o 9.5 9
5 3.6 30 26 3.4 21 16
6 3.75 33 29 3.58 25 21
7 4.63 62 64 3.7 30 27
8 5.1 62 64 3.9 37 35
9 4.2 44 44
10 4.6 50 51
11 5.0 51 52
12 5.1 55 55
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EHC PROBLEMS
Sadanand Mandal
AGM, TSX
PSWR- Nagpur
PROBLEM 1:
After adjusting the balance voltage at -1.6 V, it was observed that the balanced voltage was drifting towards
positive side causing disturbance in EHC operation. On investigation it was observed that the amplifier
piston as well as the EHC pilot assembly were not free. So both the assemblies were dismantled and
cleaned thoroughly. Even after that the problem did not get resolved. It was then noticed that-
1. There was leakage at the bottom of the EHC pilot through the threaded cap.
2. There was low trip oil pressure to the EHC block. It was less than 4.5 kg/cm2 instead of 5.0 +0.5 kg/cm2
as per design even after full tightening of pressure converter in the trip oil line.
ACTION TAKEN:
1. A new pilot from spare was assembled. Before assembly no leakage through the thread was ensured.
2. The trip oil supply line orifice size was increased from 3.0 mm dia to 4.0 mm dia. The orifice to EHC pilot
valve was increased from 1.5 mm dia to 1.8 mm dia. With that oil pressure in the trip oil line to EHC
improved to 5.0 kg/cm2.
3. Since there was lot of adjustment trial taken with the old moving coil assembly, a new moving coil
assembly was installed in place of the old one.
With the above changes, the EHC balanced voltage drifting problem got stabilised.
PROBLEM2:
While taking HP & IP secondary oil pressure readings with EHC voltage, it was found that the IP secondary
oil pressure was dropping immediately from 5.3 kg/cm2 to 0 kg/cm2 with EHC opening more than 90 %. It
was also observed that two follow up pistons out of three in the IP secondary oil follow up piston battery
was not responding properly with the adjustment screws. By blocking the oil supply to those two suspected
follow up pistons, IP secondary oil pressure became stable even beyond 90% EHC opening. It increased to
5.6 kg/cm2 with 100 % EHC opening. Repeatability was also found to be matching.
Though no apparent abnormalities were noticed with these two follow up pistons, they were replaced with
new ones. Still the problem of IP secondary oil dropping did not get resolved. So the EHC with follow up
pistons battery and linkages was removed from location for through checking. It was observed that there
was fouling of power piston linkage with IP secondary oil follow up piston battery sleeve. Further it was
noticed that the power piston linkage was of short length than the design. It was 102 mm against 127mm as
per drawing (fig-1). The length of the old linkage was increased at site by adding an extra piece and EHC
block was assembled (fig- 2). The functioning of the block was found to be alright and there was no
dropping of IP secondary oil pressure beyond 90 % opening of EHC even with all three IP follow up pistons in
service. Max IP secondary oil pressure was 5.6 kg/cm2 with 100 % EHC opening.
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Fig.1
Fig.2
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New linkage (fig-3) with correct dimension was brought from BHEL/Hardwar and again assembled in the
EHC block by replacing the old fabricated one. With that calibration of EHC was taken and found to be
satisfactory
Fig.3
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Also, the work on Bottom Ash Hopper (Customer Scope) was not even started. On Discussion along with
the customer it was decided to seal the S Panels temporarily by Castable refractory.
IMPLEMENTATION:
The arrangement is in process and continuously leaks are identified and are being repaired simultaneously.
CONCLUSION:
Since being a continuous process, the leaks are being identified and regularly attended. Also, the blowers
are readily available for ESP Air Tightness Test and the same blowers can be used for the same. The process
has removed the dependency on external factors such as Foundation readiness for Fans, Startup Power,
etc. which are usually in Customers Scope as is the case at OPGS Kutch site. The process has helped in
reducing the time for Furnace Air Tightness Test once the FD Fan is commissioned on receipt of startup
power from the customer. At OPGS Kutch site, instead of cribbing about the non-availability of the fronts,
team has successfully found the alternate solution which has saved approximately 25 days.
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January - 15
CASE STUDIES
Tapas Saha
AGM,
Hindalco Mahan Site
1.0 FAILURE OF BFP IN UNIT-1 AT HINDALCO MAHAN SITE
DESCRIPTION:
On 16/08/2013, when U#1 TG was running on load, BFP 1A suddenly developed very high vibration leading
to shut down of the pump. Prior to the high vibration, there was heavy shaking of suction and discharge
lines of BFP.
ACTION:
It was decided to decouple the BFP shaft and check alignment. While checking alignment it was found that
shaft is very tight in rotation. After much effort it was possible to rotate and alignment was checked. Radial
alignment was found disturbed by about 3mm. It was then decided to open the pump. After opening the
pump, the cartridge was sent to BHEL, Hyderabad for inspection and repair.
ANALYSIS:
It is concluded that the damage in the pump has occurred due to high vibration which was caused by
misalignment of Hydraulic coupling assly. It was also found that Hydraulic Coupling is disturbed from its
original position by several mm as few of the foundation bolts which were assembled during erection were
missing . There is no provision of locating pin in hydraulic coupling assly supplied by Voith.
REMEDIAL ACTION:
It is suggested to provide at least two locating pins in the Hydralic coupling assly. This will prevent physical
movement of the body in case foundation bolts are not in order.
2.0 HIGH VIBRATION AND LP ROTOR BENDING OF U#3 TG AT ADITYA BIRLA PROJECT ATLAPANGA,
ODISSA.
DESCRIPTION:
The Unit was commissioned and was running at 80MW load. Suddenly there was high shaft vibration in brg
no. 4. The vibration exceeded more than 400 micron. Machine was hand tripped but it could not return to
Barring Gear operation. After 3-4 days when machine was cooled , inspection of brg was carried out. During
inspection it was found that journal and coupling run out was on the higher side at 0.10mm.However there
was no damage in the bearing. Heavy rubbing marks were observed in the LP gland area.
ACTION:
LP gland was replaced with a new gland . Since LP rotor run out value was high, it was replaced with a new
rotor as per direction from customer. After replacement of the rotor m/c was rolled again and loaded. All
parameters were found normal.
ANALYSIS:
During first commissioning, the gland steam temperature controller were not commissioned. The gland
steam temperature was being controlled from PRDS. During operation once gland steam temperature shot
up to 370 deg C. During that time high vibration of the rotor was observed. Due to sudden over-heating of
the gland box, the body of the glad box, which is a fabricated one , got deformed and resulted in total loss of
clearance between shaft and seals and led to rubbing of the shaft.
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January - 15
REMARKS:
i) The gland steam controller should be in service before charging steam to shaft glands. The temperature
of initial gland steam should be kept as low as possible.
ii) The bow in the shaft was probably a temporary phenomenon. An attempt of salvaging the situation
could be attempted by putting the rotor on Barring Gear operation for a prolonged time and then low
temperature soaking could have been carried out at 500-600 rpm. But this was not attempted due to
pressure from customer to replace the rotor.
4.0 OIL LEAKAGE IN LPBP CONTROL VALVE ACTUATOR OF UNIT-1 AND UNIT-2 AT HINDALCO, MAHAN
SITE
DESCRIPTION:
The high pr. (150Kg/cm2) LPBP system for 150 MW TG was supplied by M/s HORA, Germany. All the
actuators were supplied in assembled condition to site. In Unit #1 and Unit#2 control valve actuators were
leaking out oil through the spindle. This problem was reported in March 2013 and was conveyed to BHEL,
Hyderabad. Since BHEL,Hyderabad had no expertise on the servo-motors, the specialist from M/s HORA,
Germany was called. The German specialist refused to attend the problem citing scouring marks which
developed at site due to welding splatter, causing the leakage. M/s HORA refused to take any responsibility
for this problem and their representative left site without attending the problem.
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January - 15
ACTION TAKEN:
It was decided at site level to open one servomotor and to inspect the internals. On inspection it was
found that the spindle had some rough surface which caused slight rubbing of the end gaskets ( see
attached drg.). The spindle was polished with fine emery paper (200 gr) and the gaskets were replaced
with new spare. The actuator was put into service in June 2013 and till now there was no leakage found.
Same exercise was carried out for the second actuator in U#2 and was successful.
REMARKS:
The problem which was disowned by the OEM, was resolved by site erection group. In addition, time and
costly foreign exchange also could be saved for the organisation due to affirmative action taken by the site.
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Parameter Value
Seal Oil DP Turbine End 1.41 kg/cm2
Seal Oil DP Exciter End 1.41 kg/cm2
Seal Oil drain temperature H2 TE side 50.26 Deg C
Seal Oil drain temperature H2 EE side 54.30 Deg C
Seal Oil Drain Temp Air TE side 57.02 Deg C
Seal Oil Drain Temp Air EE side 61.0 Deg C
PROBLEM OBSERVED:
After two days, oil level in seal oil vacuum tank started decreasing below minimum level. Level was not
improving.
ACTION TAKEN:
Level in Intermediate Oil Tank was observed for any anomaly. It was found in order. Operation of float in
Intermediate Oil tank and Seal Oil Vacuum tank was observed. For checking, bypass valve of float in
Intermediate Oil Tank was opened for maintaining oil level in seal oil vacuum tank. But still level was not
being maintained. Observation was done from sight glass in seal oil vacuum tank. Very small amount of oil
was seen flowing in the tank.After confirming proper operation of float in Intermediate Oil tank, position of
bypass valve of vacuum pumps was checked. Bypass valve was found in closed condition and vacuum
pumps were also in stopped condition. Bypass valve was opened. After opening of bypass valve, oil level in
vacuum tank started increasing.
Probably by opening of bypass valve, there was release in slight pressurization of vacuum tank.
SUGGESTION:
In seal oil vacuum tank, only level switch is envisaged for indication of level low condition. Seal Oil level not
low condition in vacuum tank is used for start permissive of AC seal oil pump.Continuous monitoring of oil
level of seal oil vacuum tank is not provided. Level transmitter should be provided in seal oil vacuum tank
for continuous monitoring of oil level in seal oil in vacuum tank. Emergency in seal oil system can be
avoided.
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Fig-01
3. Over speed tester valve body was found in damaged condition near bottom (Fig-02).
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Fig-02
4. Radial clearances between OSG fly bolt and rotor shaft measured and found 1.0 mm which was within
limit as its design value is given from 0.8 mm to 1.0 mm.
5. Radial gap in both sides were measured and found 1.0 mm.
6. OSG fly bolt movement checked and found stuck up.
7. OSG dismantled for checking assembly discrepancies, fly bolt vent hole found choked with metal
debris. Trip device vent hole and drain hole found rusted.
8. OSG Tester test oil, control oil and holding oil lines checked for dummy and same found ok.
9. Trip device sliding pilot spindle found rusted and its movement inside liner of trip device was also found
stuck up (Fig-03)
Fig-03
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10. Trip device vent hole and drain hole found rusted.
RECOMMENDATIONS / CONCUSION:
1. Proper cleanliness of individual governing oil pipe to be ensured by air blowing and looping during
flushing.
2. Manufacturing unit should adhere correct assembly and testing of governing console and this should
be done with utmost care and due importance so that missing items can be identified during its testing
and site should not suffer for this.
3. 2 mm dia. orifice should be installed in holding oil line to avoid excessive holding oil leakage from top of
trip device during its remote engagement.
4. OSG servicing/checking must be completed prior to start of commissioning of governing system.
Jitendra Kumar joined BHEL PSWR in Feb 2008 and looking after Turbine-
Generator and aux. commissioning. Presently posted at 2X500 MW NTPC
Mauda having experience of commissioning of 125 MW KN series and
250 MW & 500 MW KWU turbines and aux. commissioning.
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INTRODUCTION:
Boiler Circulating Pump is a glandless (seal less) pump motor unit for boiler water circulation application
with pump and motor being integrated in a pressure-tight casing. The glandless design (no shaft seal)
makes this pump best suited for pumping of high temperature and high pressure liquids without any
leakage at all. The pump is driven by Torishima made high p erformance three phase induction motor filled
with water (wet motor).
In a controlled circulation Boiler, circulating pumps plays an important role in the performance of the
Boiler. For 500 MW/600 MW Units, 3 Nos of circulating pumps are given and these pumps are placed in the
down comer circuits to ensure proper circulation of water through the water walls.
Feed water entering the boiler drum via Economizer, flows from the drum through the down comers (6
Nos) to the pump suction manifold. The boiler circulating pumps takes water from the suction manifold
and discharges via the pump discharge lines in to the furnace lower front inlet header, furnace lower water
wall right and left side headers and rear headers.
In the water wall inlet header, the boiler water passes through strainers and then through orifices, which
feed the furnace wall tubes to drum.
Cooling water is required for BCW pump motor cavity water cooling and Heat barrier cooling.
Fill and purging line is required for motor cavity filling and purging before the BCW pump commissioning
and trial run. This line is taken from BFP common discharge and CEP discharge line as per BCW pump
erection and process and instrumentation drawing.
PROBLEM:
Problem is faced at erection and commissioning stage of systems for initial filling of BCW pump motor
cavity. As per BCW pump scheme motor cavity filling and purging line is given from BFP common discharge
header and CEP discharge line but initially these systemsare generally not ready.
SITE ACTION:
Following site action was done for BCW pump motor cavity filling and purging:
1. Boiler fill pump was commissioned.
2. 25 mm piping tapping was taken from boiler fill pump discharge line near boiler and piping erected up
to HP cooler and filter. Line diagram Scheme shown in figure and approval taken from customer.
3. One no of valve and NRV of 2500 Classwas introduced in the line.
4. Water flushing of temporary pipe line before the HP cooler and filter was carried out.
5. Water flushing of pipe line through HP cooler and filter was carried out.
6. Water flushing of permanent pipe line for CC pumps motor cavity filling line, up to motor inlet and LP
cooler inlet was carried out. Water flushing was declared as per procedure for commissioning of BCW
pump.
7. Filling and purging was done as per commissioning procedure.
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FIG.1
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The HPBP (BP&BPE) Valves are fitted with RSG-10A resistive type Position Transmitter. During
commissioning at various sites, we have come across the following problems:-
PROBLEM:
These transmitters are supplied along with the valve assembly in assembled condition.
1. During the course of project execution, it takes considerable time between receipts of material at site
to actual E&C. During this period, valve assembly is kept at storage yards & these transmitters are
subjected to harsh environmental condition, causing defects.
2. During commissioning of the valves at most of the site, it is very difficult to set the zero position (5mA)
& span position (15mA) of RSG-10A position transmitter, due to improper fitting of position transmitter
on the valve body & associated linkages.
3. RSG-10 position transmitter has bolt & hexagonal nut type terminals for electrical connections. During
Commissioning & calibration of the valves, these connection needs to be removed & frequent
loosening & tightening of terminals make them prone to become loose. This looseness causes the
variation in the position transmitter output & malfunction of the valves.
SOLUTION TO THE PROBLEM:
1. It is advisable to send these transmitters as a separate package with the valve assembly with
appropriate storage instruction on the package, so that defects due to improper storage can be
avoided. During commissioning the same can be mountedat site after erection & necessary
adjustment can be done in situ.
2. To correct the problem of improper fitting of position transmitter on the valve body & associated
linkages, the whole position transmitter assembly needs to be removed & adjusted in situ.
3. It is advisable to provide push-in type or screwed terminals in RSG-10 position transmitter, which are
more reliable instead of bolt & hexagonal nut type.
PROBLEM:
Being a resistive type position transmitter RSG-10A Position transmitter is prone to loose contact
(Chattering), temperatures drift etc. which will ultimately cause the malfunction of the HPBP Valves.
SOLUTION TO THE PROBLEM:
Some Non-Contact type position transmitter can be used for HPBP Valves, like BALLUFF make position
transmitters which are used in EHA of Turbine Valves. Though using Non Contact type position transmitter
is a costly affair, but the HPBP system reliability & availability will be increased.
PROBLEM:
In the control system of HPBP Valves comprises of Valve Position controller module (PROMAX Module DSZ-
OM69229S908A, refer Fig. 2), Normally Auto Bit (P3A-3) is kept at high state for enabling the Blocking
Element & operation of the valve. It has been observed that in case of failure of position transmitter loop,
valve malfunctions.
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Figure1–RSG-10PositionTransmitter
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PROBLEM FACED:
During commissioning of AVT in Amravati U#1it was observed that during CV testing (Quick Opening &
Closing) steps arenot executed & AVT was going in Shutdown Steps. The partial trip logic for control valves
implemented was as follows:-
Partial trip bit will activate when any of this condition is satisfied:-
1. Any of the trip solenoid of that valve combination is OFF (e.g. for HPCV1 partial trip will be active when
any of the TSV of HPSV1/HPCV2 is OFF).
2. LSR Operated
3. Turbine trip operated
On further analysis it was observed that during AVT, stop valve is tested by TSV1 & then TSV2. TSV2 is kept in
OFF condition so that Stop Valve can remain close during Control Valve testing. Keeping TSV2 OFF was
causing partial trip of Control Valve.
MODIFICATION DONE:
Partial trip bit will activate when any of this condition is satisfied:-
1. (Any of the trip solenoid of that valve combination is OFF)A ND (Valve Combination is not selected for
AVT)
2. LSR Operated
3. Turbine trip operated
After this modification, input 1 of partial trip logic for control valve selected for AVT, is disabled during AVT.
After this modification AVT was demonstrated successfully OFFLINE as well as ONLINE.
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RECTIFICATION:
Pump Bearing was replaced.
ROOT CAUSE OF FAILURE:
Failure of ferrule joint of bearing lubrication line lead to failure of pump bearing.
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Annexure-1
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FIG NO.01
FIG NO.02
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FIG.NO.03
Om Prakash Singh completed his B. Tech from BIT Sindri and joined BHEL
PSWR in Feb 2011. Presently posted at 2X600 MW DAINIK BHASKAR TPP
and looking after Turbine-Generator and aux. commissioning.
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PROBLEM:
Tendaho U#1 20MW Turbine was running continuously, parameters were as follows.
· Turbine load between 2 MW to 5MW
· Aux. steam pressure 13.0 kg/cm2
· Gland steam header pressure between 200mmwc– 400mmwc,
· Condenser vacuum 0.170 ata.
After some time it was observed that condenser vacuum is deteriorating continuously from 0.170 ata to
0.390 ata. Aux. steam pressure was seen to be same as earlier but gland steam header pressure went to
negative side (-100 to -250mmwc).
All possibilities to improve the vacuum were checked as turbine tripping value on vacuum was 0.400 ata.
By increasing the aux. steam pressure to 15 kg/cm2 instead of 13 kg/cm2 unit was allowed to run. But
vacuum could not be improved and turbine tripped on low vacuum.
OBSERVATIONS:
After turbine shut down the strainers provided in the steam supply line of ejectors and steam supply line of
gland seal steam header were checked and all strainers were found in heavily choked condition. This was
the only reason for improper supply of steam to ejectors and low gland seal steam header. This strainer
choking was due to following reasons.
· Improper quality of steam supplied.
· Improper mixing of chemical into water at boiler end. Poor DM water quality
· Improper steam blowing of steam pipe line.
ACTION TAKEN:
As there are 2 no. of steam ejectors (one in service and one stand by) whenever one steam ejector's
strainer gets choked, 2nd steam ejector is taken in service and then the previous ejector is isolated for
cleaning its strainer.
But such provision is not available in gland seal steam header. Original scheme was as below.
G S Supply To Turbine
Y- strainer
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As shown above it has only one strainer before its supply header it cannot be isolated. The steam pipe line
for gland seal steam header was modified by providing 2 nos. of strainers - one in main supply line and
other in its bypass line as shown below.
G S Supply To Turbine
Y-strainer
This modification was very necessary because this strainer choking problem was coming frequently.
PRESENT STATUS & CONCLUSION:
Now whenever gland seal steam supply header pressure falls down, bypass line is taken in service and
main line strainer is cleaned and vice versa. With that there is no low vacuum problem.
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Dear Reader,
Here is an opportunity to share your experience with us. If you have solved any problem, carried out any
modification or effected improvements in the past, on any power station equipment or system leading to its
improved performance, you can share your experience with others by contributing an article on it for
publication in the TAKNIKI DARPAN Journal. The article can pertain to design, engineering, commissioning,
operation, maintenance or R&M function.
Your feedback, in the form of article, would certainly play a pivotal role in the perpetual endeavours of BHEL
and its customers towards effecting improvement in the performance of the equipment supplied by BHEL.
Thanking you,
Yourstruly,
Editorial Committee
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