GPIAA AirTransat 236
GPIAA AirTransat 236
GPIAA AirTransat 236
S. R.
Government of Portugal
Air Transat
Airbus A330-243 marks C-GITS
Lajes, Azores, Portugal
24 August 2001
On August 24, 2001, Air Transat Flight TSC236, an Airbus 330-243 aircraft, was on a scheduled
flight from Toronto Lester B Pearson Airport, Ontario (CYYZ), Canada to Lisbon Airport
(LPPT), Portugal with 13 crew and 293 passengers on board. At 05:33, the aircraft was at
4244N/2305W when the crew noted a fuel imbalance.
At 05:45, the crew initiated a diversion from the flight-planned route for a landing at the Lajes
Airport (LPLA), Terceira Island in the Azores. At 05:48, the crew advised Santa Maria Oceanic
Control that the flight was diverting due to a fuel shortage.
At 06:13, the crew notified air traffic control that the right engine (Rolls-Royce RB211 Trent
772B) had flamed out. At 06:26, when the aircraft was about 65 nautical miles from the Lajes
airport and at an altitude of about FL 345, the crew reported that the left engine had also flamed
out and that a ditching at sea was possible.
Assisted by radar vectors from Lajes air traffic control, the crew carried out an engines-out, vis-
ual approach, at night and in good visual weather conditions.
The aircraft landed on runway 33 at the Lajes Airport at 06:45. After the aircraft came to a stop,
small fires started in the area of the left main-gear wheels, but these fires were immediately ex-
tinguished by the crash rescue response vehicles that were in position for the landing.
The Captain ordered an emergency evacuation; 16 passengers and 2 cabin-crew members re-
ceived injuries during the emergency evacuation.
The aircraft suffered structural damage to the fuselage and to the main landing gear.
APPENDIX E - GLOSSARY..................................................................................................................................101
1
All times are Coordinated Universal Time unless otherwise noted.
2
All fuel quantities are in metric tons, unless otherwise noted.
3
Analysis of the DFDR data indicates that a higher-than-normal rate of reduction in aircraft gross weight
started at 04:38, the time that the fuel leak started.
4
Air Transat’s MCC is manned by the company’s dispatcher and maintenance manager.
5
The cabin preparations for the possible ditching and eventual engines-out landing are detailed in section
“1.15 Passenger Safety and Survival” of the report.
Final Investigation Report 22 / ACCID / 2001 Pag 7 of 103
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The crew then contacted MCC on HF, advising the dispatcher of the inexplicable low fuel quan-
tity readings. At this time, fuel on board was 4.8 tons, or 12 tons below the planned quantity. The
crew reported that they could not determine what the problem was, that the fuel indication was
continuing to reduce, and that the apparent fuel leak was happening in the right-wing inner tanks.
At 05:59, during the dialog with MCC, the crew reported that the fuel quantity had further re-
duced to 1.0 tons in the right tanks and 3.2 tons in the left tanks. MCC asked whether the fuel
loss might be a leak in the left engine. In reaction to this suggestion, the Captain momentarily re-
selected cross feed from the left tanks. The crew stated that all fuel pumps were selected ON
when the fuel remaining was 1.1 tons.
At 06:13, when the aircraft was at FL390 and 150 miles from Lajes, the right engine flamed out.
The crew notified Santa Maria control that the engine had flamed out and that the flight was de-
scending. At 06:15, the crew reported to air traffic control that the fuel on board had reduced to
600 kilograms. At 06:23, the First Officer declared a “Mayday” with Santa Maria Oceanic Con-
trol, and at 06:26, when the aircraft was 65 nautical miles from the Lajes airport and at an alti-
tude of about FL 345, the left engine flamed out. The ALL ENG FLAME OUT procedure was
completed by the crew and an engines-out descent profile was flown towards Lajes.
At 06:31, the flight was transferred to Lajes Approach Control. Assisted by radar vectors and
flashing of the runway lights, the aircraft arrived about 8 miles off the approach end of runway
33 at approximately 13 000 feet on a track of about 270°. The Captain advised Lajes that he was
conducting a left 360-degree turn in order to lose altitude. During the turn, the aircraft was con-
figured with leading-edge slats out and landing gear down for the landing. S-turns were con-
ducted on final to lose additional altitude.
At 06:45, the aircraft crossed the threshold of
runway 33 at about 200 knots, touched down
hard 1 030 feet down the runway, and
bounced back into the air. The second touch-
down was at 2 800 feet from the approach
end of the runway, and maximum braking
was applied. The aircraft came to a stop 7
600 feet from the approach end of the 10
000-foot runway. After the aircraft came to a
stop, small fires started in the area of the left
main-gear wheels, but these fires were im-
mediately extinguished by the crash rescue
response vehicles that were in position for Figure 1 - Aircraft After Landing
the landing6. The Captain ordered an emer-
gency evacuation. Fourteen passengers and two cabin-crew members received minor injuries,
and two persons received serious injuries during the emergency evacuation. The aircraft suffered
structural damage to the fuselage and to the main landing gear.
6
The response of crash file rescue services to this emergency landing are detailed in section “1.14 Crash Fire
Rescue and Survival” of the report.
Final Investigation Report 22 / ACCID / 2001 Pag 8 of 103
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The First Officer subsequently made a public address announcement that the flight would be
landing on or near the runway in 5 to 7 minutes and to prepare for a land evacuation. Just prior to
the landing the First Officer issued a “Brace, Brace, Brace” command. The flight attendant
shouted the prescribed brace commands to the passengers.
Immediately after the landing, the passengers began cheering and clapping. Concerned those fol-
low-on instructions from the flight deck would not be heard, the flight attendants shouted to the
passengers to be quiet; the passengers complied. About 10 to 20 seconds after the aircraft came
to a stop, the Captain made the “EASY VICTOR” evacuation command.
The evacuation was attempted using all emergency exits and evacuation slides. All doors and
slides functioned normally, except for exit L3, which only opened approximately 20 to 25 centi-
metres. The passengers in the area of L3 were redirected to other exit doors.
The only other problems noted with the evacuation from the cabin were the following:
• Some passengers were reluctant to leave the aircraft and had to be aggressively encour-
aged to do so;
• Many passengers attempted to leave with carry-on baggage; and
• One paraplegic passenger located in row 1 in the forward cabin and an elderly man in
row 39 in the aft-cabin, who could not walk without his cane, had to be physically as-
sisted to reach the exit and to get onto the escape slide.
The evacuation reportedly was completed in approximately 90 seconds. Following the evacua-
tion, the passengers were marshalled away from the aircraft.
Upon completion of the engine replacement, inspections were conducted by both the lead techni-
cian and another technician and no discrepancies were noted. The engine was successfully
ground run and the aircraft was released for flight with a post-SB RB.211-29-C664, hydraulic
pump (P/N: 974800), a post-SB C625 fuel tube (P/N: FK30383), and a pre-SB C625 hydraulic
line (P/N: LJ51006).
An examination of the aircraft following the occurrence determined that both engines stopped
due to fuel exhaustion, which was precipitated by a rupture of the high-pressure fuel pump inlet
fuel tube on the right engine, which failed as a result of hard contact with the hydraulic line. The
engine had accumulated 67.5 flight hours since the engine installation.
All the injuries to the passengers were as the result of the evacuation from the aircraft. Although
most injuries were of a very minor nature, two passengers required hospitalization for treatment
of their injuries.
Shedding of brake and wheel components during the landing run also resulted in a combination
of punctures and impact damage to the airframe and left engine nacelle.
The Captain passed his initial Pilot Proficiency Check as an A330 Captain on 11 May 2000, and
his final Route Check was performed on 22 June 2000. Company training records indicated that
he had successfully completed all required recurrent training. No shortcomings in performance
were recorded on his file. The Captain successfully completed his most recent check ride on
29April 2001.
7
Flight Director is the lead flight attendant in charge of the passenger-cabin crew.
Final Investigation Report 22 / ACCID / 2001 Pag 13 of 103
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The Trent Engine Controller worked Monday to Friday, and was on call during the weekend that
the engine was being replaced.
The lease status of the aircraft had no bearing on the control of the aircraft. The operation and
maintenance of the aircraft was the responsibility of the air operator.
The aircraft was registered to Air Transat AT, Inc. on 28 April 1999 and had a valid Certificate
of Airworthiness issued on the same date. The aircraft was configured with 362 passenger seats.
The actual fuel on board at take-off as calculated from the DFDR data was 46 900 kg.
As requested by Rolls-Royce, the engine was stored in a restricted area to ensure its integrity in
the event that it urgently was required by another airline, because this was the only available
spare loaned engine in North America. Access to the engine required notifying the in-house
Rolls-Royce representative. Because the engine had to remain available to other user’s world
wide, it was kept in an "as received" status.
9
Note from Bureau d´Enquêtes et d´Analyses pour la Sécurité de l´Aviation Civile (BEA) – Ministére de l´Equipement ,
des Transports, de l´Aménagemement du Territoire, du Tourisme et de la Mer- REPUBLIQUE FRANÇAISE
Final Investigation Report 22 / ACCID / 2001 Pag 16 of 103
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cluded that the scratches and scores were directionally aligned and that they could have been
caused from repeated contact from a blunt instrument, such as a screwdriver being inserted be-
tween the tubes in order to force a clearance between them. There were no cracks initiated from
the score or scratch marks.
Engine No 1 Engine No 2
Oil temperature 110°C 65°C
Oil pressure 80 psi 150 psi
Oil quantity 17 litres 14 litres
Rolls-Royce conducted a technical review of the oil parameters. Technical Report Number
FSG44035 in part determined that, because the position of the leak was downstream of the
fuel/oil heat exchanger, the high fuel-flow through the heat exchanger would have cooled the oil
resulting in the oil parameters shown. A characteristic of the Mobil Jet oil II used for engine lu-
brication is that the viscosity increases rapidly when the temperature decreases. The higher vis-
cosity resulted in an increase in oil pump outlet pressure, and in a low flow rate of oil back to the
reservoir. Because the oil quantity is measured at the reservoir, a lower quantity of oil would
have resulted.
Post occurrence verification of the oil reservoir sight gauge showed the oil level to be 1.5 litres
below the full line. Assuming that the oil reservoir was full at departure, the oil used was less
than the normal oil consumption after 5 hours of operation.
A trim tank is located in the THS. The trim tank transfer system is a fully automatic mode sys-
tem that controls the center of gravity of the aircraft. When the aircraft is in cruise, the primary
Fuel Control and Management Computer (FCMC) calculates the C of G and compares the result
to a target value that depends on the aircraft actual weight. From this calculation, the FCMC op-
timizes the C of G by deciding to transfer fuel to or from the trim tank. There is normally only
one aft transfer at the beginning of the flight. During the flight, there is a series of small forward
transfers. If the actual C of G is different from the target C of G by more than 0.5% and the air-
craft is above Flight Level 255, an appropri-
ate transfer occurs. If an inner tank quantity
drops below 4 000 kg, forward transfer also
occurs to maintain the fuel in the inner tanks
between 4 000 kg and 5 000 kg until the trim
tank is empty. If during a forward transfer the
inner tanks are out of balance by more than
500 kg, the transfer is automatically stopped
on the heaviest side until the fuel balance is
achieved. A final forward transfer occurs
when the time to destination is less than 35
minutes, when either set of wing tanks is be-
low 4.0 tons, or when the aircraft descends
through FL245. When fuel is being trans-
ferred, a “TRIM TANK XFR” message ap-
pears on the ECAM Memo screen; when the
trim tank is empty, a “TRIM TANK XFRD”
message appears on the ECAM Memo por-
tion of the E/WD screen. Figure 5 - E/WD & Trim Tank Transferred Memo
The Fuel ECAM page displays the following:
• Layout of the fuel tanks,
• Fuel tank quantities,
• Fuel used by each engine, and the total fuel used,
• Fuel on Board quantity
• The status of the eight fuel pumps,
• The low-pressure valves, crossfeed valve, and the trim tank isolation and inlet valves po-
sitions, and
• Anomalies to the system in amber colour.
The fuel panels, located on the overhead panel, incorporate selectors and switches to control the
fuel pumps, crossfeed valve, inner tank split valves, trim tank isolation valve, center tank valve,
and outer tank to inner tanks transfer valves.
The fuel system incorporates a fuel/oil heat exchanger that uses fuel flowing to the engine to cool
engine oil and to pre-heat the fuel.
A crossfeed valve is fitted in the fuel system to connect or isolate the left and right engine feeds.
The valve position is controlled by a push-button switch. The primary purpose of the crossfeed
switch is to provide a capability to correct fuel imbalance situations, in particular to allow both
engines to be fed from either the right-hand or left-hand wing tanks. In normal operation, the
switch lights are out, and the crossfeed valve is in the CLOSED position10. To connect the left
and right hand sides of the fuel system, the pilot pushes the WING X FEED switch to open the
crossfeed valve: the ON light illuminates “white” to indicate that the valve is opening; and, the
OPEN light illuminates “green” when the valve is fully open. With the crossfeed valve selected
to the AUTO position, the valve automatically opens in the emergency electrical configuration.
10
In some parts of the manufacturer’s documentation, the CLOSED position is sometimes referred to as the
AUTO position.[The valve (cross feed) automatically opens in emergency configuration]
Final Investigation Report 22 / ACCID / 2001 Pag 20 of 103
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The only fuel quantity recorded on the DFDR was the quantity in the trim tank. The following
table represents, for each fuel-related event, the aircraft position and the trim tank fuel (TTF) as
recorded on the DFDR, as well as the fuel on board (FOB) and leak rate (Leak/R tons per hour)
as calculated by subtracting the zero fuel weight from gross weight recorded on the DFDR.
When a more serious fault occurs, the ECAM system alerts the crew aurally by a single chime,
and visually by an amber MASTER CAUTION light. The ECAM system informs the crew by
displaying an amber failure message on the E/WD, the crew action items (procedure) required
for the abnormal situation, and the relevant system synoptic page on the SD. The affected system
on the SD will be displayed in amber.
For ECAM Caution messages, the first action required by the crew is to ensure that the aircraft is
on a safe flight path. Although the flight crew needs to be aware of the configuration or failure,
immediate action is not required. Depending on the fault, a related FAULT light may be illumi-
nated as well.
When there is a serious failure that requires immediate action, the ECAM system alerts the crew
with a continuous repetitive chime and a flashing red MASTER WARNING light. The ECAM
system informs the crew by displaying a red failure message on the E/WD, the crew action items
(procedure) required for the abnormal situation, and the relevant system synoptic page on the
SD. The affected system on the SD will be displayed in red.
For ECAM Warning messages, the first action required by the crew is to ensure that the aircraft
is on a safe flight path, and that the required crew actions depicted on the warning/message por-
tion of the E/WD are completed in a timely manner.
At 04:38, the DFDR recorded an increased rate of reduction in the fuel quantity. Analysis of this
DFDR data determined that this anomaly was the start of the fuel leak in the right (#2) engine,
low-pressure fuel line. The increased rate of reduction in fuel quantity would have been indicated
in lower-than-anticipated FOB quantity figure on the E/WD.
At 04:44, the DFDR recorded a decrease in oil quantity on the right engine; however, because
the oil parameters were within operating limits an ECAM message was not generated.
At 04:56, the DFDR recorded the commencement of a two-minute forward transfer of fuel from
the trim tank to the main wing tanks. Total transfer was about 0.3 tons. During this transfer, a
green TRIM TANK XFR ECAM message would have been displayed in the memo section of the
E/WD. The occurrence crew did not recall seeing this message.
According to the crew, at 04:58, shortly after the aircraft crossed 030W, a routine check of the
aircraft instrument indications was commenced. It was at this time that the crew noticed that the
oil quantity on the right engine was markedly lower than the quantity on the left engine. At
05:04, the crew selected the ENGINE status page on the SD to verify other engine readings.
11
Oil quantity is recorded on the DFDR in imperial quarts; whereas, oil quantity is displayed in the cockpit in
litres.
Final Investigation Report 22 / ACCID / 2001 Pag 23 of 103
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At 05:11, the DFDR recorded the commencement of a 19-minute forward transfer of the remain-
ing 3.2 tons of fuel in the trim tank commenced. During this transfer, a green ECAM message
TRIM TANK XFR would have been displayed.
AT 05:21, the crew notified the company operations centre that, although at the beginning of the
flight the right engine had 18.5 litres of oil, the oil quantity was now only 14.5 litres, the oil tem-
perature was 65 degrees Celsius, and the oil pressure was 150 pounds per square inch (psi); these
readings were significantly different from the readings on the left engine, which were 18.2 litres,
110 degrees Celsius, and 80 psi. MCC advised the crew that the problem would be analysed and
that the flight would be contacted with the results12. The readings were within the parameters
specified in the Engine Oil Consumption Airbus A330 chart.
At 05:30, the trim tank forward fuel transfer was completed and a TRIM TANK XFRD message
would have appeared in the memo section of the E/WD; this message would remain displayed
for the duration of the flight. The complete forward transfer of the trim tank fuel is not scheduled
to occur until 35 minutes from the destination airport, until the wing tanks are below 4.0 tons, or
until the aircraft descends below FL 245.
At 05:33, a pulsing, white ECAM advisory ADV message was generated and displayed in the
memo area of the E/WD, indicating a 3 000 kg fuel imbalance between the right and left wing
tanks. Under normal conditions, this ECAM advisory brings up the FUEL system page on the
SD. However, the manual selection of ENGINE systems page by the crew inhibited the display
of the fuel page. A 3 000 kg fuel imbalance is an abnormal condition that does not result in a
display of the corrective action required to correct the imbalance. To ascertain the required cor-
rective action, the crew must view the fuel page, diagnose the pulsing fuel quantity indications,
and then refer to the appropriate page in the Quick Reference Handbook (QRH).
At 05:34, the crew deselected the ENGINE page, and the FUEL page was displayed in the SD.
At 05:36, having noted the fuel imbalance, the crew opened the crossfeed valve and turned off
the right-wing fuel pumps, establishing a crossfeed from the left wing tank to the right engine.
An amber FUEL R WING PUMPS LO PR message13 would have appeared on the left side of the
message area of the E/WD and a green WING X FEED memo would have appeared on the right
side. Shortly afterward, the crew also noted that the remaining fuel on board was significantly
below the planned quantity. Fuel losses or leaks themselves cannot be identified as such by the
ECAM system; consequently, a specific ECAM warning is not generated for these conditions,
although related system messages would be generated as normal parameters were approached or
exceeded.
At 05:52, the caution message ENG 2 FUEL FILTER CLOG appeared on the E/WD. This mes-
sage indicated an abnormal (and sometimes temporary) pressure loss across the fuel filter of the
right engine. This type of message does not require action by the crew; it is only generated for
crew awareness and monitoring, if necessary.
12
Prior to MCC re-contacting the flight on the unusual oil readings, the fuel loss problem occurred and com-
munications on this problem took precedence.
13
Amber messages are accompanied by an amber CAUTION and a single chime caution.
Final Investigation Report 22 / ACCID / 2001 Pag 24 of 103
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At 05:54, the crew established crossfeed from the right-wing tank to the left engine by selecting
the right-wing pumps ON and the left-wing fuel pumps OFF. A FUEL L WING PUMPS LO PR
message appeared on the left portion of the E/WD message screen and the WING X FEED
memo would have continued to appear on the right portion.
At 05:58, the FUEL R WING TK LO LVL message appeared, indicating less than 1 640 kg of
fuel remaining in the right inner tank for more than 60 seconds.
At 06:08, the FUEL L+R WING TK LO LVL message appeared, indicating that inner tanks on
both wings were now below 1 640 kg for more than 60 seconds.
At 06:13, the ENG 2 STALL and ENG 2 FAIL messages were displayed indicating that the right
engine had flamed-out. The RPM decay resulted in the ENG 2 STALL message; the ENG 2
FAIL message indicated that core speed had decelerated to below idle with the master switch
‘on’ and the fire pushbutton ‘in’ (not pushed).
At 06:21, the FUEL TRIM TK PUMP LO PR message was displayed indicating that the trim
tank transfer pump switch had been selected to FWD and no fuel remained in the trim tank.
At 06:26, the ENG 1 STALL and ENG 1 FAIL messages were generated as the left engine
flamed-out. As the associated generator decelerated, the aircraft would have automatically re-
verted to the emergency electrical configuration, with power supplied by the automatic extension
of the ram air turbine. The EMER ELEC CONFIG warning may have been inhibited by the ENG
ALL ENG FLAMEOUT warning; neither warning was recorded on the Post Flight Report.
The containers containing the slides were shipped back to Canada. When the containers arrived,
the L3 slide was identified by checking serial number against aircraft logs. The L3 slide was
forwarded for examination to the Aircraft Evacuation Systems Division of the Goodrich Corpo-
ration, the manufacturer, located in Phoenix, Arizona, United States of America. The examina-
tion was carried out under the supervision of an investigator from National Transportation Safety
Board (NTSB) Survival Factors Group.
When the shipping container was received at the Goodrich facility, it contained the slide/raft, its
girt bar, and the packboard with the decorative cover. However, the crate did not contain the two
release rails, rail adapters, rail release pins, or girt panel sleeve. An additional search did not lo-
cate the missing items or identify specifically the ones installed at the L3 location.
The NTSB, Survival Factors Group Report, dated 19 November 2001, detailed the condition of
the slide. Specifically, the inflation bottle gauge reading of “0" and the detached firing line were
consistent with the firing of the inflation valve; and, an “L” shaped tear, measuring 7 by 19
inches, of the fabric was the reason for incomplete inflation of the slide. The other abrasion
marks on the slide attachments were probably caused by the attempts by the fire-fighters to open
the door and to release the chute.
Conclusive finding as to the cause of the door jam could not be made, primarily because of the
missing components. Notwithstanding, interviews and photos confirm that the slide had not re-
leased completely from the door, and that the bustle rails/rail adapters may have jammed.
There have been at least two, previously documented cases where the slide rails have jammed
preventing opening of the door in the emergency mode. Studies of these previous occurrences by
Goodrich indicated that the jamming might have been caused by incomplete installation of a pin
forming part of the assembly. On 30 July 2001, to mitigate risks of improper installation, Good-
rich published Service Bulletin Number 25-306, introducing a rework of the rail-associated com-
ponents. Goodrich recommended compliance with the SB at the next scheduled unit mainte-
nance. In conjunction with the Goodrich SB, Airbus issued SB’s A330-25-3126 and A340-25-
4152 (for the A330 and A340 respectively) dated 07 August 2001. Airbus also recommends
compliance, but with no time frame specified. At the time of the accident (two weeks later), the
Airbus non-mandatory bulletins had not been yet received by Air Transat.
In 17 October 2001, France’s aviation regulator, Direction Générale de l’Aviation Civile
(DGAC), upgraded compliance with these SB’s by issuing Airworthiness Directive (AD) num-
bers AD 2001-465 (B) R1, for the A330; and, AD 2001-464 (B) R1 for the A340, both dated 17
October 2001. Compliance with these AD’s was required no later than 13 October 2004. AD
2001-465 (B) R1 applies to the occurrence aircraft.
about 17 000 feet. Based on these calculations, the passengers would have been exposed to a
maximum cabin altitude above 13 500 for about 1 minute. 15
15
Appendix A details the calculation of cabin pressures.
Final Investigation Report 22 / ACCID / 2001 Pag 29 of 103
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A review of the Transport Canada and the Federal Aviation Authority Service Difficult Report-
ing (SDR) system confirmed a number of previous similar instances where there have been prob-
lems with emergency mask deployment involving a wide range of different models of aircraft.
16
P/N AF5L32-25 S/N 90631; P/N AF5R32-25 S/N 90637; P/N AF5R32-25 S/N 90658;
P/N AF5L33-25 S/N 91049; and P/N AF5L34-24 S/N 00112
Final Investigation Report 22 / ACCID / 2001 Pag 30 of 103
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The reasons given for these failures, in part, included doors failing to open due to an electrical
fault or for no apparent technical reason.
The number (14) of masks that failed for undetermined reason was within the 10 percent bound-
ary assumed by the design standard.
• WARNING - MUST OPEN DOOR THEN REMOVE RING AND THIS FLAG
FROM THIS GENERATOR PRIOR TO PLACING THIS UNIT IN SERVICE
This oxygen unit had been installed at the time the aircraft was manufactured.
1.9 Communications
1.9.1 Communications Equipment
During the portion of the flight subsequent to the initial recognition of engine reading anomalies,
the flight crew used the aircraft’s HF radio to communicate with Santa Maria air traffic control
and the company MCC; the very high frequency (VHF) radio was used to communicate with La-
jes Approach Control. No anomalies were reported regarding the operation of these radios.
Final Investigation Report 22 / ACCID / 2001 Pag 32 of 103
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Santa Maria Oceanic Control is responsible for air traffic control in an area bounded on the west
(40°W) by New York Oceanic Flight Information Region (FIR), on the north (45°N) by Gander
and Shanwick FIRs, on the south by Sal and Canarias FIRs, and on the east by Canarias, Lisboa
and Madrid FIRs. Control relies on flight plans, position reports, track predictions, and HF com-
munications. Santa Maria Oceanic Control does not have radar. The occurrence flight was in
communications with Santa Maria Oceanic Control from approximately 04:10 until 06:31 when
control of the aircraft was passed to Lajes Approach Control.
Santa Maria Approach control is responsible for air traffic control in the area around the Azores
islands (approximately 240 wide by 540 miles long) between 1 000 feet and FL 285. Control re-
lies on flight plans, position reports, track predictions, and VHF communications. Although
Santa Maria Approach was involved in passing situation information to Lajes, it was not in-
volved in the direct control of the aircraft.
Lajes Approach Control is a military terminal area control facility that is responsible for control-
ling air traffic arriving and departing Lajes. The control area is bounded by a 45 nm arc com-
mencing from the 270° clockwise to 150°, and then from 150°/45nm to 270°/45nm point; and
between 700 feet above mean sea level (msl) to FL155. Control relies on flight plans, position
17
Appendix B details an overview of the cockpit communications activity level.
18
These times are based solely on utterance times, and do not include the entire time occupied with communi-
cating. Specifically, times not included are the following: the periods before speaking, planning the commu-
nication; waiting time between communications where a response is expected; and, the periods following the
communication, recognizing and analyzing the meaning of the communication.
Final Investigation Report 22 / ACCID / 2001 Pag 33 of 103
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reports, track predictions, radar, and VHF communications. Lajes Approach provided control for
the flight from 06:31 until the aircraft landed. Radar data is not recorded.
Lajes Tower is a military facility that is responsible for air traffic control within its 5nm zone.
Control relies on flight plans, aircraft position reports, radar information from Lajes Approach,
and VHF communications. Although Lajes Tower was not directly involved in controlling the
aircraft, it did provide landing clearance and did coordinate the response of airfield facilities.
At 06:31, Air Transat 236 checked in on Lajes Approach Control frequency and declared a
MAYDAY; at this time, the aircraft was descending through FL273 and at 33 miles northeast
from Lajes. On a number of occasions, the crew requested that the all runway lights be flashed to
aid in the visual acquisition of the runway; each time the approach controller relayed the request
to the tower controller, and the approach controller responded to the flight that the lights were
being flashed.
At 06:36, when the aircraft was passing through approximately FL220 and 14 miles from the air-
port, the crew confirmed the runway in sight. The crew also requested confirmation that the
Crash Fire Rescue (CFR) vehicles were standing by, and prepared for an aircraft evacuation; this
transmission was acknowledged by the controller.
AT 06:43, the tower controller advised the approach controller that the flight was cleared to land.
19
Appendix A contains the Terceira airport and approach charts.
20
The TRM TACAN is a military navigation system that incorporates distance-measuring equipment that can
be used by civilian operators.
Final Investigation Report 22 / ACCID / 2001 Pag 34 of 103
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At 06:45, just after landing, the crew requested that fire crews go to the area of the tires, and at
06:46, advised that an evacuation was in progress.
At 06:46, the tower controller suspended runway operations due to the disabled aircraft.
The aircraft was equipped with an Allied Signal Model 6022 solid state Cockpit Voice Recorder
(CVR), part number 980-6022-001 and serial number S/N 0327, and an Allied Signal Model
4700 Digital Flight Data Recorder (DFDR), part number 980-4700-003 and serial number 5636.
The two recorders were sent to the Bureau d’Enquêtes et d’Analyses pour la Sécurité de
l’Aviation Civile (BEA) in France for read out and analysis.
The First Officer was not familiar with the layout of the circuit breaker panel in the avionics bay,
nor was he knowledgeable about the location and number of circuit breakers associated with the
recorders.
The aircraft was equipped with a digital access recorder (DAR), P/N 2248000-61, S/N 00548.
Following the occurrence, the optical cartridge (S/N 009) installed in the DAR was sent to the
Flight Recorder Playback Centre of the National Research Council (NRC) of Canada for data
retrieval. The NRC examination determined that the cartridge was properly formatted and had a
root directory; however, the cartridge did not have any recorded data.
To determine the reason for the lack of data, the airline was requested to provide the cartridges
previously installed on the aircraft DAR. These cartridges (S/N 5, 14, and 3) were in the airline’s
queue for download/analysis and had not yet been analyzed. The cartridges were examined by
Flight Recorder Playback Centre, with the following results:
The analysis of these cartridges concluded that the DAR failed on or immediately after 31 July
2001. It was also concluded that Air Transat was unaware of the failure of the DAR.
A similar situation occurred during the Transportation Safety Board (TSB) of Canada’s investi-
gation into the Swissair Flight 111 in-flight fire and loss-of-control accident that occurred off the
coast of Nova Scotia, Canada, on 2 September 1998. On 9 March 1999, TSB issued the follow-
ing recorder, power-supply related recommendations based on its determination that “A lack of
recorded voice and other aural information can inhibit safety investigations and delay or prevent
the identification of safety deficiencies”:
As of 01 January 2005, for all aircraft equipped with CVR’s having a recording capacity
of at least two hours, a dedicated independent power supply be required to be installed
adjacent or integral to the CVR, to power the CVR and the cockpit area microphone for a
period of 10 minutes whenever normal aircraft power sources to the CVR are interrupted.
A99-03
Aircraft required to have two flight recorders be required to have those recorders pow-
ered from separate generator buses.
A99-04
In its response to TSB Recommendation A99-04, Transport Canada stated that it supported this
TSB recommendation with the provision that the U.S. and Canadian requirements are harmo-
nized. The Federal Aviation Administration of the United States of America (FAA) response to a
similar recommendation from the NTSB, indicated that the FAA would be introducing a Notice
of Proposed Rulemaking to amend Technical Standard Order (TSO) 123 (a) to address the re-
quirement for a 10 minute independent power supply for CVR’s. This TSO is based on a stan-
dard developed by the European Organisation for Civil Aviation Equipment (EUROCAE), of
which Transport Canada is a participating member. Transport Canada will monitor the progress
of this standard and, when appropriate, consider introducing the requirement into Canadian legis-
lation.
In its response to TSB Recommendation A99-03, Transport Canada stated that Canadian Avia-
tion Regulations subsections 551.01 and 605.33, as well as Airworthiness Manual 551.00, al-
ready require the use of separate busses. Furthermore, the Transport Canada requirement is har-
monized with the EUROCAE-ED-56A.
The life jackets have an inspection cycle of two years. Each bag contains an inspection tag that
indicates a “REINSPECTION DATE” for the vest, and an additional, red colour sticker affixed
to the outside of the bag indicates the “DUE TO BE CHANGED” date.
Most of the life jackets on board the aircraft had been packed in 1998 and had a “REINSPEC-
TION DATE” of OCT 2002. One of the inspection tags had an overhaul inspection date of 16
DEC 98, and another, 21 JAN 99.
The passenger life jackets found on the aircraft after the occurrence were of two types: a single-
strap type similar to the one described on the passenger safety card and the cabin safety demon-
stration video; and, a two-strap version.
While donning the vests, some of the passengers had difficulty in finding the bound waist straps.
The reported donning problems were associated with the single-strap jackets.
The Cabin Attendant Operations Manual specifies that the occurrence aircraft was equipped with
only the single-strap type of life jacket. On the occurrence flight, the pre-flight passenger safety
briefing and the demonstration of the donning of the life jackets during the preparation for the
anticipated ditching were based on the single-strap type life jacket.
There is no CAR’s specifying that there should only be one type of life jacket on an aircraft.
However, CAR’s subpart 705.43 (1) requires that the air operator ensure that passengers are
given a safety briefing in accordance with the Commercial Air Service Standards, and CAR’s
Subpart 705.44 requires that the air operator provide each passenger, at the passenger's seat, with
a safety features card containing, in pictographic form, the information required by the Commer-
cial Air Service Standards (CASS).
CASS subpart 725.43 requires that the standard passenger safety briefing consist of an oral brief-
ing provided by a crew member or by audio or audio-visual means in both official languages
which includes the location, and use of life preservers, including how to remove from stow-
age/packaging and a demonstration of their location, method of donning and inflation, and when
to inflate life preservers.
CASS subpart 725.44 (vii) requires that the safety features card contain the location of life pre-
servers and correct procedures for removal from stowage/packaging; donning and use of the life
jacket for adult, child and infant users including when to inflate; and that the safety information
provided by the card be accurate for the aeroplane type and configuration in which it is carried
and in respect of the equipment carried.
The Emergency Equipment Section of the Air Transat Cabin Attendant Operations Manual states
that all life jackets on board must be of the same type, and states that, during the pre-flight check,
flight attendants must verify the presence of a life jacket at each seat. Although this section of the
manual also refers to the fact all life jackets on board are to be of the same type, verifying that
the type of life jacket during the pre-flight check is not a flight attendant responsibility. Accord-
ing to the flight attendants on the occurrence flight, the presence of lifejackets at each seat was
verified before the passengers boarded the aircraft.
The installation and verification of the status of life jackets is a maintenance function. All life
jackets are verified on installation and at every “C” check of the aircraft for compliance in re-
gards to the “re-inspect due date” to ensure that each vest has sufficient time remaining until the
next “C” check. The aircraft had not undergone a “C” check since it was acquired by Air
Transat.
Final Investigation Report 22 / ACCID / 2001 Pag 39 of 103
Released copy
21
AOC 6727 in force on the day of the occurrence was approved on 10 October 1996.
22
Operations Specification 61 in force on the day of the occurrence was approved on 15 June 2001.
23
TP 6327, Safety Criteria for Approval of Extended Range Twin-engine Operations (ETOPS) Manual, dated
1996 Edition, is published by Transport Canada Safety and Security under the authority of the Director gen-
eral, Civil aviation by the Director, Commercial and Business Aviation in coordination with the Director,
Airworthiness.
Final Investigation Report 22 / ACCID / 2001 Pag 41 of 103
Released copy
Chapter 4 of Transport Canada publication TP 6327 E specifies the standards and necessary
guidance that must be contained in the maintenance program to qualify for ETOPS. The Air
Transat MCM, containing the maintenance procedures for it’s A330 aircraft involved in ETOPS,
was approved by Transport Canada. The MCM specifies the qualification required for mainte-
nance personnel involved on ETOPS aircraft. This ETOPS qualification is provided as an ele-
ment in the company’s training that provides its technicians with a technical maintenance rating
on the A330. Other than a requirement to maintain an ETOPS reliability program, which in-
cludes reporting to Transport Canada, there are no additional maintenance actions or record
keeping required, other than maintaining compliance with the provisions in the company’s
MCM.
Section 6.13 of the company Operations Manual provides direction as to the conduct of ETOPS
flights. Section 6.13. H) specifies the following conditions that would mandate an en-route diver-
sion to an ETOPS alternate airport:
• Engine failure;
• Multiple system failures that would make it impossible for safe flight continuation to destina-
tion;
• When a LAND ASAP message is displayed on the ECAM; and
• When an immediate landing is indicated in an emergency or abnormal procedure checklist.
Section 6.13 H) also specifies that some failures, such as a fuel leak, depressurization, or higher-
than-normal fuel consumption, may warrant a diversion.
The Airbus A330 IPC, also referred to as ADRES (Airbus Documentation Retrieval System), is
presented on a series of CD-ROMs. It specifies the configuration status of each aircraft by serial
number. It lists both the current aircraft parts applicability and includes a note informing the
reader of the embodied SB.
Concerning the engine dressing and the hydraulic pump modification, Airbus published its own
SB’s (A330-29-3068). Although the Airbus IPC referenced the applicable Rolls-Royce SB’s, a
direct hyperlink to the Rolls-Royce SB’s is not a design feature of the Airbus IPC.
The Rolls-Royce EIPC for the Trent 772B engine series is available on a single CD-ROM. The
CD-ROM also contains relevant SB’s, which are accessible through a number of different meth-
ods, one of which is via hyperlinks from the IPC portion of the CD-ROM.
The Airbus IPC, Rolls-Royce IPC and associated SB’s are available on the company computer
network. These documents are also available on standalone PC’s and CD’s at the MCC station
and in the Air Transat Technical library. Additionally, a paper copy of each SB is held in the Air
Transat Technical Library, under controlled access, in order to preserve its integrity. Technicians
rarely, if ever, access either the library’s hard copy or the standalone CD’s; maintenance man-
agement more commonly uses them.
Neither the Airbus IPC, nor Rolls-Royce EIPC was referenced at the time of engine receipt, nor
during review by engineering prior to the engine installation. The Airbus IPC was referenced by
the lead technician during the engine installation.
24
Although an SB may be designated as “Mandatory” by the manufacturer, the embodiment of the SB only be-
comes mandatory if the civil aviation authority issues an airworthiness directive directing the embodiment of
the SB.
Final Investigation Report 22 / ACCID / 2001 Pag 44 of 103
Released copy
In cases, when an airframe manufacturer-controlled system interacts with an engine system, both
manufacturers will publish their own separate SB. In such cases, embodiment of the SB would
normally be found in both the airframe log under the airframe manufacturer's designation and in
the engine log under the engine manufacturer's designation. When a modification associated with
an SB is embodied during production, the annotation provided in log book by Airbus will be the
modification number with a brief description of the modification; the description does not refer-
ence the SB number.
Rolls-Royce SB’s for the RB211-700 and 800 series are listed together in a 75-page index. At
the time of the occurrence, there were a total of 908 Service Bulletins published, of which 545
concerned the 700 series. Out of those 545 SB’s, a total of 295 were relevant to the condition of
the engine. Review of the loaned engine logbook showed that out of the remaining 250 SB’s, 167
had been carried out or embodied. These were documented on 10 different pages throughout the
engine logbook.
In this regard, the Air Transat MCM contains a procedure that requires incoming parts and mate-
rials be subjected to a receiving inspection in order to verify that the subject items are acceptable
for use on company aircraft. In order to verify acceptability of items, the receiving inspector’s
responsibilities include ensuring that:
• The delivered goods match the items on the respective purchase order with regard to part
number specification and quantity;
• The B757, A310 and A330 components critical to ETOP’s meet the requirements for
ETOP’s capability;
• The visual inspection ensure that the received goods have not suffered damage in transit;
and
• The paperwork accompanying the goods provides data substantiating that airworthiness
requirements have been met by the supplier.
As per CARs 571.08 (1) (a), the above requirements do not apply for serviceable, used parts that
are removed from an aircraft and are immediately installed on another aircraft.
When the engine RB211 Trent 772-60 SN 41055 arrived at Air Transat's facility, the engine con-
troller compared the status of the engine to the Rework Summary Sheet and the Carry Forward
Items List. He was satisfied that the components on the carry-forward item list were available
either in stock, or off any engine that might require replacement.
The review of the documentation and receiving inspection of the engine did not detect that the
engine condition was in the pre-mod (SB RB.211-29-C625) configuration.
The use of the EIPC CDs was not considered by the lead technician because he was not aware of
this capability in the MCC. The use of the CDs by the MCC technicians was not considered be-
cause their role in providing technical assistance to maintenance crews was to locate resources
and not to provide technical assistance in searching for technical references."
When the Trent Engine Controller called back, he readily recalled the rationale for the pump
modification as being excess vibration. He also recalled that the modified pump interfered with
the fuel lines, and that these would need to be replaced. He further advised the lead technician to
confirm that, when the pump and lines were installed, adequate clearances existed between lines
and components. The lead technician queried the possibilities of using a pre-mod pump to save
time, because the work was already running late. Based on his knowledge that all Air Transat
aircraft were of post-mod status, as were all other Roll Royce powered A330's flown in Canada
by other operators, the Engine Controller informed the lead technician that such a pump was not
available on short notice. Both agreed that there was no choice other than to replace the fuel
tubes. In discussing the estimated time required to complete the transfer of the tubes, the control-
ler suggested that the time outlined in the SB should be used. At this time, the controller was
told, in passing, that the crew had not been able to access the SB. While the difficulty in access-
ing the SB initially was a concern, the discussion quickly reverted to the time required to com-
plete the work, without further discussion of the SB. The controller was advised that he would be
kept informed of the situation.
Both segments of the post-SB fuel tube assembly (P/N’s: FK30382 & FK30383) were taken
from the removed engine and installed on the replacement engine. The different shape and rout-
ing of the new fuel line overcame the earlier difficulties encountered in installing the hydraulic
pump. The pre-SB hydraulic tube LJ51006, received with the loaned engine, was retained. The
installing technician recalled that, during the installation of the hydraulic line when trying to
achieve the required separation between the fuel and hydraulic line, the hydraulic line had a ten-
dency to spring back. Notwithstanding, according to the technician who did the installation,
clearance between components was easily obtained by positioning and holding the hydraulic
tube, while applying torque to the “B“ nut. He also stated that a tool was not used to force the
separation between the fuel and hydraulic tubes. There was no additional installation difficulties
reported.
The Rolls-Royce representative telephoned MCC during the engine installation on Sunday to in-
quire about the work progress and to offer help if required. He was informed that the pre-mod
status of the loaned (right) engine did not permit installation of the hydraulic pump and was in-
formed that the fuel tube was being changed over from the removed engine to the loaned (right)
engine to allow the pump installation. The Rolls-Royce representative was unaware of the engine
dressing SB modification status of the loaned engine and of the status of the Air Transat engine
fleet. The Rolls-Royce representative was not specifically told of the difficulties in accessing the
SB's nor was he specifically asked to consult his documentation. His offer to attend on-site if re-
quired was not taken up.
The installation of the post-mod hydraulic pump, the pre-mod hydraulic tube and the post-mod
fuel tube assembly resulted in a mismatch between the fuel and hydraulic tubes.
When the engine change was completed, the lead technician arranged for an independent inspec-
tion.
Another inspection called “the independent inspection” was done by a qualified technician, who
had not been involved with the work being inspected. The independent inspection was done to
ensure that engine controls are properly connected and secured. This scope of this inspection
was not intended to include the fuel or hydraulic system components.
Following these inspections, the engine was ground run, without problems, and was released for
flight.
The company MCM specifies a requirement for a quality control inspection of the documenta-
tion after an engine installation; however, company manuals do not specify a time frame for this
inspection. There was no QC representative on site on the weekend of the engine installation.
The company plan was to do the document verification when preparing the removed engine for
shipment for repair. As of the occurrence date, 24 August 2001, the engine change documenta-
tion had not yet been reviewed by the quality control staff.
27
A review of other airline training programs indicated a similar deficiency in that there was no specific, ini-
tial, recurrent, or line oriented flight training on fuel leaks.
The crew stated that, although indications of a lower-than-expected fuel quantity were recog-
nised shortly after receiving the fuel imbalance ADV, they did not consider the FUEL LEAK
procedure, until later in the flight28.
28
The crew’s consideration of the FUEL LEAK procedure occurred at a time prior to the commencement of
the CVR recording.
Final Investigation Report 22 / ACCID / 2001 Pag 54 of 103
Released copy
“CRUISE C/L”
ENROUTE WIND … INSERT
The flight plan log entries indicated that, up to the time that aircraft passed 30º West, the crew
had recorded the times, fuel on board, and surplus fuel over the flight planned waypoints. The
DFDR indicated that the ECAM system pages were manually selected by the crew only once
during the cruise portion of the flight, at 01:15:38, just after the aircraft reached the initial cruis-
ing altitude of FL 370.
According to the crew, the flight and fuel consumption progressed normally through to 04:57
when the aircraft passed 30º West. The flight log indicates that the fuel surplus quantity was
maintaining within the range of 7.0 ±0.2 tons. The fuel quantity data on the DFDR also indicated
normal fuel consumption up to 04:38, the onset of the increased rate of reduction in the fuel
quantity. At 04:56, a two-minute, 0.3-ton forward transfer of fuel from the trim tank occurred,
and the green TRIM TANK XFR ECAM message would have been displayed: the crew did not
mention seeing this message
As part of routine procedures, when the aircraft crossed 030º W at 05:00, the crew would have
made a position report, should have reviewed system indications and made the flight plan log
entries. DFDR data indicates that, at 05:04, the Engine Page was manually selected, and that, at
05:10, the SD was returned to the Cruise Page.
It was during the check of engine parameters that the low oil quantity was noticed. DFDR data
indicates that the Engine Page on the SD was manually selected again at 05:15, and company
logs and a HF recording indicate that the crew were in a 3-minute conversation with MCC re-
garding the oil problem at 05:21. The crew indicated that the sudden change in oil parameters
plus the unexplained combination of low oil temperature, low oil quantity and high oil pressure
led them to believe that there was a problem with the indications. This opinion was supported by
the fact that the crew’s review of the aircraft manuals did not discover any reference to this type
of system anomaly.
While the trouble-shooting of the engine oil problem was taking place, at 05:11, a 19-minute for-
ward transfer of the remaining 3.2 tons of fuel in the trim tank commenced and a green ECAM
memo TRIM TANK XFR would have been displayed. At 05:30, the fuel transfer was complete
and a TRIM TANK XFRD message would have appeared in the memo section of the E/WD. The
crew did not recall seeing these messages.
The first signs noted by the crew concerning a fuel problem were at 05:33, when the fuel-related
ADV message was displayed on the Engine/Warning Display29. The crew’s de-selection of the
Engine ECAM page resulted in the Fuel ECAM page being displayed and the crew becoming
aware of a fuel imbalance between the left and right inner-wing tanks. The initial crew action at
05:36 was to address the Fuel Imbalance message by selecting the crossfeed valve OPEN and the
right-wing fuel pumps OFF in order to feed the right engine from the left-wing tanks.
Shortly thereafter, the crew became aware that the fuel remaining on board was only 11 tons, or
8.5 tons below the expected amount of fuel. According to the crew, both the imbalance and fuel
quantity indications were unusual and unexplainable. Neither of the pilots had ever encountered
a fuel leak or an unexplained low fuel quantity either in training or in flight.
29
The generation of the fuel imbalance-related advisory message was delayed by about 25 minutes by the 3.5-
ton forward transfer of the trim tank fuel.
Final Investigation Report 22 / ACCID / 2001 Pag 56 of 103
Released copy
Because the total fuel quantity was still reducing at an unexplainable high rate, the Captain de-
cided to use up the fuel from the right tank before it was lost, and selected the right wing boost
pumps ON and the left-wing boost pumps OFF to establish a crossfeed from the right wing tank
to the left (#1) engine, specifically to counter the possibility that the fuel loss was the result of a
leak in the right wing tanks. The Post Flight Report printout indicates that the left-wing boost
pumps were turned OFF at 05:54, when 5.9 tons of fuel remained on board.
Starting at 05:57, the crew was in a 5.5-minute conversation with MCC to seek advice on the
situation. MCC’s question whether the fuel loss might be a leak in the left engine, resulted in the
Captain to momentarily re-select crossfeed from the left tanks. At 06:05, the crew still estimated
that the flight would arrive at Terceira with 1 ton of fuel. However, by 06:08, the crew deter-
mined that insufficient fuel remained on board to reach the island.
30
Appendix C details the calculation of the fuel quantities in the aircraft fuel tanks.
Final Investigation Report 22 / ACCID / 2001 Pag 57 of 103
Released copy
31
Based on DFDR data a fuel quantity of 7 tons occurred at approximately 0550Z, or just after the crew initi-
ated the diversion and the aircraft was 376 nm from Lajes.
Final Investigation Report 22 / ACCID / 2001 Pag 58 of 103
Released copy
• coordinating the diversion to Lajes, which included planning for the diversion, undertak-
ing the diversion, and HF communications with ATS and MCC;
• preparing the cockpit and the cabin for a possible ditching;
• managing the engine failures; and
• carrying out the engines-out landing.
32
Kahneman and Tversky, 1986
Final Investigation Report 22 / ACCID / 2001 Pag 59 of 103
Released copy
value, potentially disconfirming information is subjected to a more critical and sceptical scrutiny.
Several studies have shown that preliminary hypotheses formed on the basis of ambiguous data
interfere with the later interpretation of better, more abundant data33.
An individual’s mental model of a situation is likely to correspond to a large part to the reality,
even though it may be wrong in some respects. Having expectations frequently confirmed re-
duces the sensitivity of the error detection mechanism. Confirmation bias is a selective process
that favours information relevant to the presently held view. In essence it is a bias towards rele-
vant-appearing information. Additionally acting upon one’s beliefs can also increase the psycho-
logical costs or “dissonance” involved in changing one’s beliefs34.
Confirmation bias can have such a strong impact that once individuals have developed a mental
model of a problem space, and they have confirmed their model, it becomes very difficult to let
go of the model, even in the light of contradictory information. The need for a realignment of
one’s mental model becomes apparent only in the light of one or more extraordinary events that
do not fit the model.
33
Lewis and Normal, 1986
34
Festinger, 1957
35
Ross and Anderson, 1982
36
Billing, 1997.
Final Investigation Report 22 / ACCID / 2001 Pag 60 of 103
Released copy
The A330 FCMC system was not designed to consider the type of fuel leak that occurred during
this flight. As a result, after the FCMC did what it could do to maintain a fuel level of 4 tons in
the right tank and when it was no longer able to maintain that level, it advised the crew that there
was an imbalance. Specifically, the FCMC, no longer able to deal with the fuel leak through its
pre-programmed fuel balancing, shed the task to the crew. This shedding took the form of a fuel
imbalance ADV.
With Management by exception, it is not uncommon to have what have been referred to as
“automation surprises”. Although information may be available to crews, this information is not
necessarily observable. Observability, in this context, refers to the cognitive work that is required
to extract useful information. It results from the interplay between a human user knowing when
to look for what information, at what point in time, and the structure of the automated system
and how it supports attention guidance.
The challenge is for automation to not merely provide additional data but to reduce the cognitive
effort required to locate, integrate, and interpret those data. For this occurrence, the low level of
system observability was manifested in two ways:
• The sudden presentation of apparently anomalous and incredulous information; and
• A representation of the system state that does not readily lead the crew to identify and
rectify the problem.
The following table depicts the flight profile as determined from the ATS transcript:
The Captain reported that he had the flashing runway lights visually from a long way out and
that he was confident that he had more than enough altitude to glide to the airport.
Consequently, during the initial glide, he was attempting to fly the aircraft at a speed, between
the recommended glide speed and the stall-warning speed, in order to keep the aircraft airborne
for the longest time. Other considerations taken into account during the glide were that the air-
craft speed could not be higher than 200 knots for gear lowering, the recommended approach
speed was 170 knots, the minimum speed to ensure RAT operations was 140 knots, and that he
had to adjust the aircraft pitch angle to achieve a glide descent angle to reach the runway. Al-
though he had never received formal training on gliding approaches, he had experienced doing
power-off approaches to landing in a number of aircraft types that he had flown.
The Captain reported that during the glide that he did not use manual trim, because he was very
busy concentrating on maintaining the correct vertical profile to the runway. In addition, al-
though he knew that the aircraft response to stick inputs would be sluggish, during the flare he
did not want to be too aggressive. Following the initial bounce, the nose of the aircraft rose sig-
nificantly. Because he did not want to become airborne a second time, on the second touchdown,
he did not flare and he applied and held maximum braking.
Outer Tank Left Inner Tank Left Inner Tank Right Outer Tank Right
1 800 kg 4 000 kg 4 000 kg 1 800 kg
37
Appendix C Fuel Consumption Calculations contains the conditions, bases, and assumptions for these fuel
calculations.
Final Investigation Report 22 / ACCID / 2001 Pag 63 of 103
Released copy
Outer Tank Left Inner Tank Left Inner Tank Right Outer Tank Right TOTAL
680 kg 1 420 kg 3 030 kg 690 kg 5 820 kg
The QRH procedure related to the fault required that the fuel be balanced. Specifically, the crew
opened the crossfeed valve and selected the left fuel pumps OFF. The crew also noted that the
fuel-on-board was significantly less than expected. Hypotheses considered by the crew for the
fuel anomalies were the following:
• An anomaly at the re-fuelling coupling;
• A possible erroneous fuel indication, (the crew was aware of a number of such previous
incidents);
• Incorrect fuel load; or
• A fuel leak.
To help determine if there were any visual signs of a fuel leak, the Captain asked a deadheading
company pilot, who was previously qualified on the A-320, to examine the wings for signs of a
leak. Because it was now nighttime, the inspection was done with the cabin lights turned off and
with the aid of a flashlight. No signs of a fuel leak were observed.
At 20:02 hours, the fuel in the left and right tanks became balanced, and the left wing tank
pumps were selected ON and the crossfeed was selected to OFF. The descent was initiated, and
the fuel load at 20:04, was as follows:
Outer Tank Left Inner Tank Left Inner Tank Right Outer Tank Right TOTAL
0 1 160 kg 1 120 kg 0 2 280 kg
There was subsequent fuel warning of L WING TK LO LVL. In accordance with the ECAM
procedure, the crossfeed was opened. However, the crew believing this action to be not appropri-
ate for the situation turned the crossfeed OFF after about 90 seconds.
38
The aircraft had been loaded with 8.5 tons of fuel because it had been a backup aircraft for a flight between
Paris and Rome. In accordance with the company’s procedures, the fuel required for the trip, including re-
serves, was 6.4 tons.
Final Investigation Report 22 / ACCID / 2001 Pag 64 of 103
Released copy
Outer Tank Left Inner Tank Left Inner Tank Right Outer Tank Right TOTAL
0 580 kg 1 080 kg 0 1 660 kg
At 20:12 hours, the left engine flamed out, and at 20:19 hours the aircraft landed at its destina-
tion with approximately 900 kg of fuel on board.
39
Kenya had investigated one of the previous occurrences in 1995 involving an A310 aircraft. The other occur-
rence involved a United Kingdom A340 aircraft; this occurrence was reported to the Accidents Investigation
Branch of the United Kingdom.
Final Investigation Report 22 / ACCID / 2001 Pag 65 of 103
Released copy
The letter stated that, in its review of proposed corrective actions to recent A320 and A340 fuel-
leak events, the DGAC identified two areas of possible improvements, technical and operational.
For improvement related to crew procedures, the letter included proposed revisions to FCOM
procedures. The letter reminded that a fuel imbalance triggers an Advisory on the ECAM with an
automatic display of the FUEL page; and, that there is no ECAM crew procedure. The letter,
highlighting that there currently was neither a fuel imbalance nor a fuel leak procedure, re-
quested that recipients review the proposal and provide DGAC with its comments. The proposal
also contained a proposed revision to SOPs, in part, to include in the FLIGHT PROGRESS
CHECK a requirement to check that the sum of the fuel on board and the fuel used is consistent
with the fuel on board on departure; if the sum is unusually smaller than the fuel on board at de-
parture, the crews were to suspect a fuel leak.
On 25 September 1997, Airbus Flight Operation Telex (FOT) AI/ST-F 999.103/97 was issued to
all known operators of Airbus A320 aircraft. The Operational Recommendation section of the
FOT, stated, in part, the following:
• before opening the Fuel X-FEED valve(s) for any unexpected fuel distribution, it is nec-
essary to check if either the fuel imbalance or the fuel low-level warning is not caused by
a fuel leak;
• If a fuel leak is confirmed by a significant inconsistency between the sum of fuel on
board (FOB) and fuel used compared to the FOB at engine start, the fuel leak procedure
applies.
Airbus fleet FCOM Abnormal Procedures were amended to include a FUEL IMBALANCE
checklist, including a Caution that the procedure should not be done if a fuel leak is suspected.
Airbus fleet FCOM Abnormal Procedures were amended to include a FUEL LEAK checklist,
including notes as to how fuel leaks could be detected.
Airbus fleet FCOM Abnormal Procedure FUEL L(R) WING TK LO LVL was amended to in-
clude a Caution that this procedure not be applied if a fuel leak is suspected.
Airbus fleet FCOM Standard Operating Procedures were amended to include in the FLIGHT
PROGRESS CHECK a requirement to check that the sum of the fuel on board and the fuel used
is consistent with the fuel on board on departure. Crews are directed to suspect a fuel leak if the
sum is unusually smaller than the fuel on board.
fuel filter on one of the left engines. The flight crew performed the fuel leak procedure in accor-
dance with the published QRD.
A United Kingdom Air Accidents Investigation Branch investigation into this occurrence was
not conducted and a report was not published on this occurrence. Reportedly, the only safety de-
ficiencies associated with this occurrence were related to a known technical fuel filter installation
fault.
Neither the Air Transat Training Manual, nor the CASS, specifically requires training on fuel
leaks. In addition, prior to this fuel exhaustion occurrence, few airlines, if any, conducted train-
ing on fuel leak situations.
2.0 Analysis
2.1 General
The investigation determined that the double-engine flameout was caused by fuel exhaustion,
which was precipitated by a fuel leak developing in the right engine as the result of the use of
mismatched fuel and hydraulic lines during the installation of the hydraulic pump. Facilitating
the fuel exhaustion was the fact that the crew did not perform the FUEL LEAK procedure that
was specifically designed by the manufacturer to reduce the consequences of an in-flight fuel
leak.
The maintenance managers, supervisors and technicians responsible for the receipt, planning,
installation and associated inspections were qualified to do their assigned responsibilities. The
Captain and the First Officer had the proper licences, endorsements and qualifications for their
assigned flight-crew duties, and had successfully completed all the required training and check
rides. The flight attendants all had the required qualifications and had successfully completed all
the required training for their assigned duties.
Up to the point that the crew became aware of the fuel quantity anomaly, the flight was prepared
and conducted in accordance with existing regulations and operational directives.
• Why the aircraft maintenance organisation did not detect the mismatch in engine configu-
rations prior to starting the engine change; then why, once the configuration difference
was detected during the engine change, the installation of the hydraulic pump and hy-
draulic and fuel lines was not completed in accordance with manufacturer’s specifica-
tions; and
• Why a qualified flight crew trained in accordance with approved training programs, while
attempting to analyse the situation and taking actions in reaction to the situation, did not
take the actions prescribed by the manufacturer to mitigate the consequences of a fuel
leak situation, and took action that exacerbated the situation.
This check was based on a comparison of the spare engine against the Rework Summary Sheet
and the Carry Forward Items List provided by the company that had completed the last shop visit
of the engine. Based on the available information and a visual inspection of the condition of the
engine, it was assessed that the required parts were available if and when an engine change to
one of the company’s A330 became necessary. Of importance to this occurrence, the engine re-
ceiving process did not identify that the configuration of the loaned engine did not match the
configuration of the other A330 engines at the company.
The following factors may have influenced this incorrect assessment:
• Because all the A330 engines in use at the company were in the post-SB configuration and
the company personnel had never been involved with pre-SB configured engines, there was
no information that would have caused a heightened concern regarding the configuration of
the loaned engine.
• The physical appearance of the pre-SB and post-SB configurations are similar and cannot be
identified through a cursory inspection such as is conducted during engine receipt.
• The part number of the hydraulic pump, as documented in the carry-forward list, was incor-
rectly identified as a post-SB hydraulic pump, Part Number 974976; and
• Hydraulic pump, Part Number 974976 was installed on other company A330 aircraft.
There was also the time-pressure factor to complete the work in time for a scheduled flight and
to clear the hangar for an upcoming event. This pressure also may have played a role in reliance
on direct and personal information about the SB, rather than trying to resolve the existing prob-
lem of not being able to access the SB’s.
With the solution at hand, being behind schedule, and having spoken to the Engine Controller,
the lead technician felt confident that the fuel tube replacement was the only remaining require-
ment to complete the hydraulic pump installation.
situation of high oil pressure, low oil quantity and low oil temperature created a level of uncer-
tainty in the cockpit. The facts that there were no other unusual engine readings, there were no
other system anomalies, and MCC could not explain or provide advice on the unusual readings
contributed to this uncertainty.
Because the oil parameters were within specified operating limits, a diversion to an ETOPS al-
ternate airport, based solely on these parameters, would not have been required by regulations,
by the company Operations Manual, or by the company’s standard operating procedure.
All of the fuel-related information and messages were provided in the form of text-type status
messages and digital counter displays, none of which conveyed a sense of urgency to cause the
crew to abandon activities associated with resolving the oil reading anomalies, and none of
which conveyed the critical nature of the fuel leak.
Of importance is that during this time, the forward transfer caused the fuel in the trim tank to be
loaded into the right wing, delaying the generation of the fuel ADV message, masking the fuel
leak problem from the crew. By the time that the fuel imbalance advisory was generated at
05:33, fuel on board had reduced to 12.2 tons and 6.65 tons of fuel had been lost.
In summary, it was highly unlikely that the crew would have become aware of the fuel anomaly
during this time frame, given the subtleties of the available indications. The fact that this could
occur highlights the limitations of the warning and alert system in this kind of situation.
When the ECAM ADV alerted the crew to the fuel imbalance, there was a large disparity be-
tween the actual fuel system state and the crew’s understanding of it. Although there were other
indications that the situation was more serious than a fuel imbalance, the crew initially reacted by
doing the FUEL IMBALANCE procedure because that was the only anomaly that was exposed
by the ECAM system. The crew did the procedure from memory because the crew was familiar
with it, having been frequently required to monitor fuel balance during simulator training ses-
sions.
The cockpit activity level during this 12-minute period would have been high, and the crew’s
attention would have been focused on the perceived ambiguity of the fuel situation and activities
involved with the diversion to Lajes. Consequently, the crew would have had little time and lim-
ited mental capacity to re-examine its mental model of the situation and to question actions al-
ready taken in response to the fuel ADV. Doing the FUEL IMBALANCE procedure fulfilled the
immediate, perceived goal of managing the fuel imbalance.
Neither of the crewmembers had ever experienced a fuel imbalance of any magnitude during fly-
ing operations, nor been exposed to a fuel leak situation during training or operations.
On 24 August 1997, an Air France A320 aircraft experienced a fuel leak. The crew involved in
this event took similar action to balance the fuel.
Once the EFOB at destination reduced below minimums, the Captain made an appropriate deci-
sion to divert to the ETOPS alternate of Lajes.
In summary, the crew was presented with an ADV that did not require immediate action. The
FCOM required that the crew refer to the QRH before taking action, and CRM principles suggest
that, before taking action in response to the Fuel ADV, the crew should have taken into account
all available information about the fuel system. Such a review would have revealed that over 6
tons of fuel had been lost. The combination of the fuel-loss indications and the substance of the
Caution note in the FUEL IMBALANCE procedure in the QRH should have led the crew to the
FUEL LEAK procedure. The FUEL LEAK, LEAK FROM ENGINE procedure requires that the
leaking engine be shut down; the FUEL LEAK NOT FROM ENGINE OR LEAK NOT LO-
CATED requires that the crossfeed must remain closed. Either of these actions would have con-
served the fuel in the left wing tanks and allowed for a landing at Lajes with the left engine oper-
ating. Opening the crossfeed valve put the fuel in the left tank at risk, and initiated a worsening
of the serious fuel-leak situation that existed.
At 05:54, the Captain’s reconfiguring the fuel pumps to establish the crossfeed from the right
tanks resulted in the fuel in the right wing tank feeding the left engine, thereby isolating fuel in
the left tank from the leak in the right engine and conserving the fuel in the left tank that would
be normally feeding the left engine. The momentary configuration of crossfeed from the left
tanks at 06:02 in reaction to a suggestion from MCC had little consequence on the fuel situation.
From 05:45, the time that the diversion was initiated, to 05:51, when the FD left the cockpit to do
the visual inspection for signs of a fuel leak, the level of activity in the cockpit would have been
very high. In particular, much of the crew’s efforts would have been occupied with preparing the
aircraft systems for the diversion and approach to Lajes, and crew’s requirement to advise ATC
and the FD about the decision to divert, all tasks required by the diversion.
Between 05:57, the start of HF communications with MCC, and 06:13, the time when the right
engine flamed out, much of the crew’s efforts were involved with communications with MCC
totalling over 10 minutes. The workload was sufficiently high that the crew did not have time to
action the ECAM action items associated with the FUEL R WING TK LO LVL and the FUEL
L+R WING TK LO LVL messages that appeared at 05:58 and 06:08 respectively.
Although not actioning these checklists did not adversely affect the flight, the crew’s involve-
ment in non-critical communication with MCC reduced the time available for them to more ac-
curately assess the situation.
Notwithstanding indications that there had been a massive loss of fuel, the crew did not believe
that there was an actual fuel leak. The following factors supported this mental model of the situa-
tion:
• The combination of the suddenness and the magnitude of the indicated fuel loss were
such that it could not be linked to any explainable reason.
• The earlier problem with the oil indications had established a level of uncertainty.
• There was no ECAM warning or caution message indicating a severe problem.
• No other indication of an engine problem was discovered.
• Some information, like the cabin crew confirming that there were no visible signs of a
leak, countered the possibility of a leak.
The crew, realizing that the situation was continuing to deteriorate, hypothesized that a computer
malfunction would account for the ambiguous indications. The lack of training for a fuel leak
situation, never having experienced a fuel leak, and having no knowledge of similar events
meant that the crew had no relevant information to counter the basis for their hypothesis.
At 06:21, the crew, attempting to ensure that all usable fuel from the trim tank was available to
the remaining left engine, selected the trim tank transfer pump switch to FWD, which resulted in
the display of the FUEL TRIM TK PUMP LO PR message, indicating that no fuel remained in
the trim tank.
Based on recorder data available, the crew’s reaction to the engine failures and actioning of the
required checklist procedures were in accordance with procedures specified in the FCOM. The
performance of cockpit duties, interface with cabin crew, and communications with air traffic
were professional and highly effective.
• The conditions that should be used to assess if a fuel leak exists are not located on the FUEL
IMBALANCE checklist.
• The exposure of A330 crews to fuel imbalance situations is limited to situations that only re-
quire a monitoring of fuel balance, and not to situations that require an active response to a
FUEL IMBALANCE advisory.
Even the last TRIM TANK XFR message that lasted 19 minutes and the TRIM TANK XFRD
message for remainder of the flight did not alert the crew to an urgent situation, in part because
they were occupied in higher priority cockpit tasks such as completing flight documentation,
communicating, analyzing the unusual engine oil parameter anomalies, and then attempting to
resolve the fuel imbalance and ambiguity of the fuel quantity.
Of importance is that the forward transfer caused the fuel in the trim tank to be loaded into the
right wing, feeding the leak in the right engine and masking the fuel leak problem from the crew.
This masking contributed to an unnoticed loss of 3.5 tons of fuel.
Some regulatory agencies (e.g. FAA and DGAC - France) already require that aircraft flight
manuals include procedures that will enable flight crews to identify fuel system leaks, and pro-
cedures for crews to follow to prevent further fuel loss. However, there are a number of commer-
cial aircraft that do not have identification procedures or fuel leak checklists.
There are also no specific regulatory requirements for training on fuel leak scenarios, and prior to
this occurrence little if any training on this type of aircraft malfunction was conducted by any
airline.
Had this particular crew been trained in the symptoms of fuel leak situations and strategies to
identify and counter such a situation, they would have been better prepared to take appropriate
actions.
3.0 Conclusions
3.1 Findings as to Causes and Contributing Factors
1. The replacement engine was received in an unexpected pre-SB configuration to which the
operator had not previously been exposed.
2. Neither the engine-receipt nor the engine-change planning process identified the differ-
ences in configuration between the engine being removed and the engine being installed,
leaving complete reliance for detecting the differences upon the technicians doing the en-
gine change.
3. The lead technician relied on verbal advice during the engine change procedure rather than
acquiring access to the relevant SB, which was necessary to properly complete the installa-
tion of the post-mod hydraulic pump.
4. The installation of the post-mod hydraulic pump and the post-mod fuel tube with the pre-
mod hydraulic tube assembly resulted in a mismatch between the fuel and hydraulic tubes.
5. The mismatched installation of the pre-mod hydraulic tube and the post-mod fuel tube re-
sulted in the tubes coming into contact with each other, which resulted in the fracture of the
fuel tube and the fuel leak, the initiating event that led to fuel exhaustion.
6. Although the existence of the optional Rolls-Royce SB RB.211-29-C625 became known
during the engine change, the SB was not reviewed during or following the installation of
the hydraulic pump, which negated a safety defence that should have prevented the mis-
matched installation.
7. Although a clearance between the fuel tube and hydraulic tube was achieved during installa-
tion by applying some force, the pressurization of the hydraulic line forced the hydraulic
tube back to its natural position and eliminated the clearance.
8. The flight crew did not detect that a fuel problem existed until the Fuel ADV advisory was
displayed and the fuel imbalance was noted on the Fuel ECAM page.
9. The crew did not correctly evaluate the situation before taking action.
10. The flight crew did not recognize that a fuel leak situation existed and carried out
the fuel imbalance procedure from memory, which resulted in the fuel from the left tanks
being fed to the leak in the right engine.
11. Conducting the FUEL IMBALANCE procedure by memory negated the defence of the
Caution note in the FUEL IMBALANCE checklist that may have caused the crew to con-
sider timely actioning of the FUEL LEAK procedure.
12. Although there were a number of other indications that a significant fuel loss was occur-
ring, the crew did not conclude that a fuel leak situation existed – not actioning the FUEL
LEAK procedure was the key factor that led to the fuel exhaustion.
15. The overwriting of 90 minutes of the CVR recording deprived the investigation of data that
could have resulted in a clearer understanding of the underlying factors to this occurrence.
16. There was no documentation readily available to the crew regarding the deactivation of the
flight recorders; consequently, only two of the three recorder circuit breakers were pulled,
which allowed the inadvertent overwriting of the CVR recording.
17. Jamming of the L3 emergency exit somewhat hampered the evacuation of the aircraft.
18. Having three Portuguese-speaking flight attendants enhanced passengers’ understanding of
the safety briefings being given in preparation for the anticipated emergency ditching and
actual land evacuation
Historically, fuel leaks were considered to be rare events, and although consequences could be
significant, the overall risk was evaluated as being low. It was also considered that routine fuel
quantity monitoring and common sense would drive a crew to a prompt precise determination of
the cause of the symptoms and to take the required action. The historical occurrence records in-
dicate that, although in-flight fuel leaks are infrequent events, these events continue to occur.
Recent occurrences have revealed that crews have had difficulty in diagnosing fuel leak situa-
tions, and that the consequences can be significant.
Analyses of past events have resulted in the design and implementation of systems capable of
detecting fuel loss events and of alerting crews, and in the creation specific fuel leak checklist
procedures. Some civil aviation authorities have mandated the implementation of these capabili-
ties and checklist procedures.
In this occurrence, the crew’s routine monitoring did not detect that a fuel leak was occurring
until over 6 tons of fuel had been lost. Also, the low-level nature of the Fuel ADV, on its own,
did neither clearly indicate the cause of the imbalance nor the severity of the situation that ex-
isted.
Although the Airbus A-330 Flight Warning Computer has a FUEL FU/FOB DISCREPANCY
Caution alert capability, the implementation of this system capability has neither been mandated
for all Airbus A-330 aircraft nor for other Airbus aircraft of similar fuel system design.
• Mandate the implementation of the FUEL FU/FOB DISCREPANCY Caution alert for all
A-330 aircraft; and
• Mandate the incorporation of a fuel loss alert for other Airbus aircraft with similar fuel
system design.
SAFETY RECOMMENDATION AA/2004
It is also recommended that the civil aviation authorities of other transport aircraft categories
manufacturing states, such as Canada, United States of America, and United Kingdom, as
well as the European Aviation Safety Authority:
• Review the adequacy of aircraft indications and warning systems and procedures to de-
tect fuel-used/fuel-loss discrepancy situations;
• Review the capability of these systems to provide clear indications as to the causes of
these situations; and
• Review the capability of these systems to provide alerts at a level commensurate with the
criticality of a fuel-loss situation.
As a result of previous similar occurrences, fuel leak checklists had been created or improved,
and some limited documentation had been added to flight manuals regarding the criteria to be
used to determine if a fuel leak exists. Notwithstanding, prior to this occurrence, no or very little
training was provided to crews on fuel leak situations. This deficiency is not unique to this A330
operator or to other Airbus operators having similar fuel and flight management systems. For this
particular occurrence, had the flight crew members been trained in the symptoms of fuel leak
situations and strategies to identify and counter such a situation, they would have been better
prepared to take appropriate actions.
Although since this occurrence, some civil aviation authorities and aircraft manufacturers have
taken action to improve related checklists and to improve crew awareness of the critical nature of
fuel leaks, there are a number of commercial aircraft that do not have identification procedures or
fuel leak checklists. There are also no specific regulatory requirements for training on fuel leak
scenarios.
The historical occurrence records indicate that, although in-flight fuel leaks are infrequent
events, these events continue to occur. The dissemination of information related to this occur-
rence will enhance safety by increasing crew awareness of the fuel leaks in the short term. Not-
withstanding, ensuring safety in the longer term will require other sustained action to ensure that
crews are better prepared for these events.
Therefore, its is recommended that Direction Genérale de l’Aviation Civile of France, Transport
Canada, Civil Aviation Authority of the United Kingdom, the Joint Aviation Authority, European
Aviation Safety Authority, and the civil aviation authorities of other states:
• Review flight crew operating manuals and checklist procedures to ensure that they con-
tain adequate information related to fuel leak situations;
• Review flight crew training programs to ensure that they adequately prepare crews to di-
agnose and take appropriate actions to mitigate the consequences of fuel leak events; and
• Amend regulations and standards to require crew training on fuel leak events.
SAFETY RECOMMENDATION AC/2004
It is also recommended that, as an interim safety measure, all civil aviation authorities:
• Promulgate the circumstances of this fuel leak event to all air operators, aircraft manu-
facturers and flight crew training organizations.
Therefore, it is recommended that Direction Genérale de l’Aviation Civile of France and EASA:
• Review Airbus aircraft indication and warning systems and abnormal procedures to en-
sure that, in situations of major fuel imbalances, actioning of appropriate fuel leak pro-
cedures becomes a priority for flight crews; and
• Consider merging the Airbus FUEL IMBALANCE and FUEL LEAK checklist proce-
dures into one procedure, containing, at the top of the procedure, the conditions that
would suggest the presence of a fuel leak.
It is also recommended that the civil aviation authorities of other aircraft manufacturing states,
such as Canada, United States of America, and United Kingdom, as well as the European Avia-
tion Safety Authority:
• Review the adequacy of the fuel indications and warning systems, as well as procedures
associated with fuel imbalance situations to ensure that the possibility of a fuel leak is
adequately considered.
SAFETY RECOMMENDATION AG/2004
It is also recommended that the civil aviation authorities of other states, as well as the European
Aviation Safety Authority:
• Review the adequacy of their regulations related to the safeguarding of on-board air-
craft recordings.
SAFETY RECOMMENDATION AI/2004
Therefore, it is recommended that the European Organization for Civil Aviation Equipment,
ICAO, all civil aviation authorities and safety investigation authorities:
• Take into account the circumstances of this particular occurrence in their deliberations
on the requirements for independent power supplies for on-board aircraft recordings.
SAFETY RECOMMENDATION AJ/2004
Current regulations and industry standards do not mandate that the configuration of major com-
ponents, such as an engine, be determined prior to the components being installed on the aircraft.
In particular, the current method used for assigning a part number to an engine results in a part
number that does not reflect which service bulletins have and which service bulletins have not
been embodied. The overall number of involved service bulletins complicates the task of deter-
mining parity between similar major components. Because there is not a requirement for a major
component-change planning process, nor a requirement to determine the precise configuration of
the component during such a process, the responsibility for detecting differences in configuration
is deferred to subsequent stages of the maintenance process.
For this occurrence, the differences in configuration between the engine being removed and the
engine being installed were not detected prior to the start of the engine change. As a result, de-
termining part parity and ensuring integrity of the installation of the right engine rested solely
with the level of the technician responsible for the engine change. Effectively, there was only
one defence layer that could ensure the safety of the installation. The integrity of the engine
changed hinged on using the Illustrated Parts Catalogue and the referenced service bulletins to
verify the compatibility of each part being changed with associated/adjacent lines and compo-
nents. The incompatibility of the hydraulic pump with the adjacent fuel pipe was eventually de-
tected and lead to reference being made to the catalogue. However, difficulty in accessing the
SB’s, time pressures, prime focus on completing the installation, and other factors caused this
one-level of defence to be ineffective in preventing an improper installation.
Frederico J F Serra
The Investigator in Charge
GPIAA- Portuguese Aviation Accidents Investigation Department
43
The cabin leakage rates versus aircraft cruise altitude are based an assumption of maximum admissible pro-
duction aircraft leakage. The realistic leakage in production is on average approximately 25-30% less than
the maximum value. The leakage rate will increase depending on aircraft age and maintenance quality. The
values are only valid for the moment where the double pack shut down takes place. The leakage rate de-
creases constantly afterwards as the cabin depressurizes.
44
Cabin altitude based on the average 665 ft/min leak rate and 9.3 minutes between these events.
45
Time estimated based on the start of the communications at 0617:16 and time estimated for the communica-
tions that took place.
46
Cabin altitude based on the average 700 ft/min leak rate for 2 minutes. This is the worst-case scenario. The
leak rate would have been lower given that the cabin altitude at the aircraft altitude of FL 250 was most likely
above the scheduled cabin altitude of 3000 feet.
47
Time estimated using the 700 ft/min leak rate to reach a cabin altitude of 13 500 feet, which is the lowest
cabin altitude (14 000 –500/+0 feet) that an oxygen mask deployment should have occurred.
48
Calculated based on the average rate of decent between FL 185 and 13 000 feet.
49
The worst case scenario based on the knowledge that the O2 masks did deploy.
Final Investigation Report 22 / ACCID / 2001 Pag 96 of 103
Appendix - 97
Time Left tank Trim tank Right tank Total FOB Events
05:54:34 3 20051 2 600 5 800 Fuel left wing pumps LO PFR support that X-Feed is in the Open
pressure position and X-Feeding from right to left
05:57:00 3 200 1 600 4 800 0.0 20.0 Right wing tank LO level 1 600 kg is based on the fact that the
t/hr t/hr low-level warning is displayed within 60
seconds after the fuel quantity falls
below 1 640 kg
Crew reported that X-feed from left
momentarily during this timeframe.
05:59:24 3 2002 1 0002 4 2002
10.4 4.3 From this time onward, the positions of
t/hr t/hr fuel tank pump switches uncertain.
06:04:00 2 80052
06:08:34 1 600 350 1 950 L+R tank LO level 1 600 kg is based on the fact that the
low-level warning is displayed within 60
12.7 4.7 seconds after the fuel quantity falls
t/hr t/hr below 1 640 kg
06:10:03 1 30053 All fuel switches reportedly selected
ON.
06:13:07 650 0.0 650 3.0 Eng 2 fail
t/hr
06:26:19 0.0 Eng 1 fail
50 Fuel balance was calculated based on the assumptions that the cross-feed valve is open, left wing tank pumps are ON and right wing
tanks are OFF.
51 This quantity is supported by the facts that the crew was crossfeeding from right to left between time 0554Z and time 0559Z, and that
on the CVR, at 0559Z, the crew reported the quantities as being 3 200, 1 000, and 4 200 kg.
52 This quantity is supported by the fact that on the CVR at 06:04Z, the crew reported the total fuel quantity as being 2 800 kg
53 This quantity is supported by the fact that on the CVR at 06:10Z, the crew reported the total fuel quantity as being 1 300 kg
Appendix E - Glossary