Customized aMDEA Process For Acid Gas Removal
Customized aMDEA Process For Acid Gas Removal
Customized aMDEA Process For Acid Gas Removal
Gas Removal
The operational experience with aMDEA gas scrubbing units shows that they contribute substantially
to both the reliability and the economy of the ammonia plant.
T
he CO2 removal system represents a major The development of the aMDEA process was started
energy consumer in an ammonia plant. An in the late 1960s. The first aMDEA unit went on-
energy-efficient gas scrubbing process is thus stream in 1971 with the commissioning of the No. HI
sine qua non for economic production. On the other ammonia plant in Ludwigshafen, Germany. In the fol-
hand, the economics of the ammonia plant also require lowing years, eight more BASF plants were fitted with
high on-stream times. Each extra plant shutdown due aMDEA gas scrubbing units.
to a failure of the CO2 removal unit causes a consider- The operational experience with these aMDEA units
able loss of production and adversely affects plant provided the incentive to license the process from
safety. For these reasons, the selection of BASF's 1982 onward. To date, the aMDEA process has been
aMDEA process can make a substantial contribution operated successfully in a total of 66 reference plants
to both the reliability and the economy of the whole worldwide, with some 20 additional units currently
ammonia plant. being under design or construction.
Assuming that U.S. ammonia producers are already
well acquainted with aMDEA, this article will briefly Applications
recapitulate the applications and process features,
which will subsequently be illustrated by a detailed The aMDEA process is suitable for a wide range of
consideration of two examples of retrofitting existing applications (Figure 1). Besides removing CO2 from
CO2 removal units (with all the inherent system con- ammonia synthesis gas, aMDEA units can be used to
straints this task implies. purify CO/H2 synthesis gas, to sweeten natural gas,
The aMDEA solvent systems are aqueous solutions For the "grassroots" design of a new plant, the sol-
of the effectively nonvolatile methyldiethanolamine vent, the configuration, and the process parameters
plus a small amount of an activator to enhance the can be customized to meet all production and site
CO2 absorption rate (Figure 2). requirements. For a revamp, however, the design
Generic MDEA reacts with water and CO2 to yield needs considerable process flexibility to conform to a
the corresponding protonated species and bicarbonate given application. Many additional constraints result
(Figure 3). The overall rate of conversion is very low. from the equipment already installed and the integra-
The absorption can be accelerated by the fast reaction tion of the unit in the ammonia plant. The following
between CO2 and the activator, a secondary amine, examples illustrate such situations.
which together form a carbamate. The carbamate in The first example involves typical conditions for the
turn reacts with the bulk solvent (aqueous MDEA) U.S. reference plants, all of which entailed conver-
transferring its CO2 and thereby being regenerated for sions of ammonia synthesis gas scrubbing units to
further reaction. The activator therefore behaves in a aMDEA (Figure 7). The second example describes the
similar manner to a homogeneous liquid catalyst with revamp of a hot potassium plant in Australia.
no net consumption, but rather several reaction-regen-
eration cycles along the length of the absorber. Conversion from an amine-based solvent
The high loading capacity of MDEA results in low
The U.S. references are all ammonia plants with a
solvent circulation rates, while the activator keeps the
capacity in the range 650-1,500 mtpd, and all have a
absorber height to a minimum. The solvent regenera-
tion can be carried out to a large extent simply by background similar to that of the unit portrayed in the
flashing the aMDEA solution. following example. The gas scrubbing unit comprises
An extra degree of flexibility is achieved by varying a single-stage absorption and stripper regeneration
the activator concentration (Figure 4). This has the (see Figure 6) and was originally operated with
effect of tuning solvent behavior to either a more monoethanolamine (MEA).
This unit has been converted to another amine based
"chemical" or a more "physical" character. The highly
system in the context of a capacity increase. The alter-
activated MDEA 06 has more of a chemical solvent
nature, that is, good absorption efficiency but energy native of achieving a higher plant capacity by an
increase of the MEA concentration was ruled out by
intensive regeneration, while the weakly activated
the operational experience regarding the corrosivity of
MDEA 01 has only a moderate absorption efficiency
the MEA solution, especially at higher concentration.
but benefits from an energy efficient regeneration,
Understandably, the corrosivity of the solution was
similar to that for a physical solvent.
investigated extensively. Following the swap, solvent
Typical application criteria for CO2 removal from
analyses showed no untoward heavy metal content in
ammonia synthesis gas are:
the solution for the first year. Thereafter, some weight
• aMDEA types 02 thru 04 in a standard two-stage
loss was observed on the corrosion coupons and sub-
unit, characterized by low energy consumption values,
sequently a steep increase in the concentration of
high gas purities, and good recovery rates (Figure 5);
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pump were installed parallel to the existing reflux cir- tified as very fine rust particles (probably iron/arsenic
cuit in order to provide a moderate temperature of the complex) in the size range 5-50 urn; the foam test with
CO2 off-gas stream, thus limiting the vapor phase sol- aMDEA indicated a significant foaming tendency.
vent losses. • A further water flushing step was not carried out in
order to limit the amount of arsenic contaminated
Cleaning of the Unit flushing water. It was decided to allow for the higher
foaming tendency by running the mechanical filter (5-
The unit had been operated with a hot-pot solution 10 u,m cartridges) at its maximum throughput from the
since 1969 using arsenic salts as corrosion inhibitor very beginning of the solvent circulation and employ-
and activator. It was therefore to be expected that con- ing an appropriate defoamer dosage rate.
siderable amounts of precipitated corrosion products
(deposit of iron/arsenic complex) were deposited on Startup
equipment surfaces. There were some concerns
regarding the fact that aMDEA is known to dissolve The unit was filled with aMDEA premix and the
such deposits quite well, which might have increased water content and column levels adjusted by adding
foaming susceptibility and carryover of the solution condensate.
from the regenerator into the condensate reboiler. The solvent circulation was commenced at about
The cleaning procedure was carried out as follows: 50% of the design flow rate. After 12 h of circulation,
« Three consecutive flushing steps using NaOH the solution had a reddish-brown color and a foam test
solution at 194°F (90°C), each of which was broken indicated formation of very stable foam (collapse time
off after the arsenic content had attained its maximum more than 5 min). After filtering the aMDEA sample,
are shown in Table 2. the color turned light yellow and the foam activity was
• Two consecutive water flushing steps were at reduced to the normal values.
194°F (90°C); the water analysis after the second An extra dose of defoamer was introduced into the
flushing step gave 60 wppm iron, 7 wppm arsenic, 80 solution loop and the circulation rate increased to 95%
wppm NaOH and 100 wppm solids and the sample of the design figure: the column levels became unsta-
exhibited a dark brownish color. The solids were iden- ble and hence a further shot of defoamer was added.