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Analysis of Power Loss and Improved Simulation Method of A High Frequency Dual-Buck Full-Bridge Inverter

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Article

Analysis of Power Loss and Improved Simulation


Method of a High Frequency Dual-Buck Full-Bridge
Inverter
Zhun Meng, Yi-Feng Wang *, Liang Yang and Wei Li
School of Electrical Engineering and Automation, Tianjin University, Tianjin 300072, China;
quakermaster@hotmail.com (Z.M.); zyangliang@tju.edu.cn (L.Y.); liweitju@hotmail.com (W.L.)
* Correspondence: wayif@tju.edu.cn; Tel.: +86-132-0769-7161; Fax: +86-022-2740-1479

Academic Editor: 02 March 2017


Received: 24 January 2017; Accepted: 02 March 2017; Published: 6 March 2017

Abstract: A high frequency dual-buck full-bridge inverter for small power renewable energy
application is proposed in this paper. A switching frequency of 400 kHz is achieved with the
adoption of the SiC power device. A two-pole two-zero (2P2Z) compensator is employed in the
outer voltage loop to generate the current reference for inner current loop. A 3P3Z compensator is
adopted in the inner current loop to track the current reference. A systematic way for calculating
the losses of high frequency inverter is presented, and the losses of the components are thoroughly
analyzed. The turn-on and turn-off procedures of the inverter are discussed in detail. The losses
caused by high frequency are calculated accurately, and the loss distribution is established as well.
The procedure of the loss analysis gives a practical example for calculating the loss of similar type
inverters. Moreover, deviation between pulse width modulation (PWM) control signal and
switching response in high frequency switching is thoroughly analyzed. The influence of deviation
is verified by designed experiment. Hence, a compensation method is proposed in order to
minimize the influence. The compensation effect is validated by experiment and simulation. Finally,
a 1-kW prototype is built to verify the feasibility of the theoretical analyses. The grid-connected
maximum output power experiment is completed at 1 kW with the efficiency of 96.1% and the total
harmonic distortion (THD) of 1.8%. The comparison experiments of power loss between Si and SiC
power devices are carried out. The experiment results confirm the loss calculation method to be
valid.

Keywords: SiC power device; grid-connected generation; dual-buck inverter; high frequency
conversion; loss analysis; simulation

1. Introduction
In order to make the social development less fossil fuel-dependent and more environment-
friendly, renewable energy becomes an important alternative energy source [1,2]. With the
development of distributed renewable energy generation, small-scale inverter becomes a focus of
research. Being able to convert all kinds of distributed energy into a unified AC power, the grid-
connected inverter extensively broadens the application range of renewable energies, and thus acts
as an indispensable role in the renewable energy generation system [3,4].
For the rapid development of the new power devices, the wide band gap power devices, such
as SiC and GaN, begin to replace the traditional Si power devices. Its outstanding performance,
including high switching speed, low switching loss, high stability in high temperature operating and
so on, makes the high frequency inverter a new research hot spot. A three-level SiC inverter is
proposed in [5]. By employing the SiC MOSFET and FPGA control platform, a 100 kHz switching
frequency is achieved. GaN high-electron mobility transistors (HEMT) power devices are adopted in
Energies 2017, 10, 311; doi:10.3390/en10030311 www.mdpi.com/journal/energies
Energies 2017, 10, 311 2 of 18

a single-phase T-Type inverter in [6]. Switching performance and efficiency performance are
analyzed among Si, SiC and GaN HEMT. The results demonstrate the advantage of the wide band
gap power devices in high frequency inverting. It can be seen that all these inverters adopt the wide
band gap power devices and have a working frequency, which is much higher than the traditional
ones. As a result, the THD of the inverters is significantly reduced and the output power quality is
improved obviously. Meanwhile, smaller components can be used and the volume of the inverter is
significantly decreased, which broaden the application range of the inverter. On the other hand, as
frequency increases, the losses of the inverter under high frequency circumstances become a major
problem, which is not discussed in detail in this paper.
With the application of high frequency switching, loss analysis is even more important, because
it can offer a guideline for the system efficiency improvement [7–14]. In [7], a detailed investigation
into loss distribution for diverse components is conducted, which includes losses of switches, diodes,
inductors and capacitors. In [8,9], the switch and diode losses of several inverter topologies are
studied and compared, which gives an evident insight into the loss distribution for each low-
frequency topology. Nevertheless, this comparison may show less accuracy when it comes to high
frequency case, because more details of the switching procedure must be taken into account in the
high frequency operation, which will affect the losses and are not included in this literature. In [10],
the mechanism reflecting the relation between transition characteristics and power losses is
discussed. Diode losses based on traditional Si semi-conductor are analyzed as well. In [11],
comparative experiments of losses between Si and SiC power devices are carried out, which proves
that the SiC devices are superior in switching speed, operating temperature and switching losses than
the traditional Si. Although the loss analyses previously mentioned are very comprehensive and
detailed, all these works are also based on traditional low frequency simplified method, which show
less accuracy for the high frequency loss analysis. This is because some losses, overlooked in low
frequency condition, may become an indispensable part of the total losses in high frequency
implementation. Hence, deviations will be introduced if low frequency loss calculation method is
implanted directly into the high frequency operation.
Moreover, the influence of the high frequency switching is not confined to losses analysis. The
impact of high frequency on the simulation model is also noteworthy. Model of the wide band gap
power devices are established in [15–19]. A compact model of the SiC metal-oxide-semiconductor
field-effect transistor (MOSFET) is built including the carrier-trap influences in [15], the simulation
results is verified by the experiments. Jun Wang et al. [16] discusses a 10-kV 4H-SiC MOSFET and
key characteristics are extensively investigated. A simple behavioral SPICE model for the SiC
MOSFETs is proposed to predict their realistic application prospect. The impact of nonlinear junction
capacitance on switching transient is studied in [17], and a simulation circuit for switching transient
analysis is built. A dynamic model of GaN cascaded current aperture vertical electron transistor
(CAVET) is established in ATLAS-SPICE-integrated simulator. The simulation model successfully
models and projects the switching performance of the GaN CAVET. These simulation models are
very thorough. However, most of the researches concentrate on the component level influence. The
impact of high frequency switching on the output of the converter is not detailed discussed. On the
other hand, the component level model is too complicated and time-consuming for converter
analysis. The influence of high frequency switching on the inverter simulation model is rarely
studied.
In this paper, a high frequency single phase dual-buck full-bridge grid-connect inverter for small
power renewable energy is proposed. The SiC components, as the power devices, are employed to
achieve high switching frequency and to limit the conversion loss simultaneously. For the controller,
the proposed inverter adopts a current voltage dual-loop. The 3P3Z compensator is adopted in the
inner current loop in order to track the current reference which is generated by the 2P2Z compensator.
The 2P2Z compensator is employed in the outer voltage loop in order to regulate the DC bus voltage
by balancing the input and output power. A systematic way for calculating the losses of high
switching frequency inverter is presented. The losses of each component in the inverter are
thoroughly analyzed. The switching procedure and the corresponding losses are discussed in detail.
Energies 2017, 10, 311 3 of 18

The high frequency losses are also taken into account during the analysis. The distribution of the
losses is established based on the presented method. Moreover, the deviation between PWM control
signal and switching response, which emerges in high frequency switching, is thoroughly analyzed.
A designed experiment verifies the influence of deviation. Thus, a compensation method is proposed
in order to minimize the influence of deviation. Experiment and simulation confirm the
compensation effect. Finally, a 1-kW prototype is made and a 400 kHz switching frequency is
achieved. The comparison experiments of the power losses are carried out between Si and SiC power
devices to verify the loss calculation method. The results proved the loss analysis is valid.

2. Circuit Configuration and Control Method

2.1. Operation Principles


The topology of the dual-buck full-bridge inverter is presented in Figure 1a. The inverter can be
regarded as two individual buck converters. Buck 1 consists of S1, S3, D1 and Li1, connecting to the DC
bus positively. Buck 2 consists of S2, S4, D2 and Li2, connecting to the bus negatively. The output
inductors of the buck converters Li1 and Li2 constitute a LCL filter with Cf, Lg1 and Lg2.

(a) (b)
Figure 1. The topology and key waveforms of the proposed inverter: (a) the topology of the inverter;
and (b) the key waveforms of the inverter.

To drive the inverter, the unipolar modulation has been adopted and the waveforms of the
driving signal are shown in Figure 1b. In one AC cycle, both bucks work in their own half cycles
separately. When Buck 1 works, S3 keeps turn-on in the half AC cycle and S1 switches at high
frequency to follow a sinusoidal reference in order to generate the positive half of the grid current ig.
D1 offers the free-wheeling path when S1 turns off. Unlike the H-bridge inverter, no switches are at
the same leg. Accordingly, the dead time is no longer needed. Moreover, the free-wheeling current is
running through D1 instead of the body diode. Because the independent diodes have a better
performance, the total losses of the inverter can be reduced. The operation principle of Buck 2 is
similar to Buck 1 and will not be discussed further.

2.2. Control Theory


The control system structure of the inverter is shown in Figure 2. For the renewable energy
distributed generation application, two-stage system structure is often adopted. The gird-connected
inverter as the post-stage is responsible for transferring the energy into power grid. The inverter can
stabilize the DC bus voltage by balancing the input and output power. A voltage-current dual loop
is employed to fulfill the function which is mentioned above.
A notch filter is used to filter out the ripple in the bus voltage Vbus. By comparing with the bus voltage
reference Vbus_ref, the bus voltage error is acquired and compensated by a 2P2Z compensator. Then, the
current reference amplitude iref is generated by the 2P2Z compensator. The grid voltage signal is injected
into a second-order generalized integrator software phase lock loop (SOGI-SPLL) to generate the phase
reference which is used to synchronize iref with the grid voltage. The instantaneous current reference iref_inst
Energies 2017, 10, 311 4 of 18

is compensated by a 3P3Z compensator. The result goes through a feedback linearization module and
becomes the duty cycle which is used to generate PWM signal to control the inverter. The detail of the
control method is described in another article and will not be discussed further.

Figure 2. Control structure of the inverter.

3. Loss Analysis
The loss analysis is an essential way to improve the system efficiency. For low frequency
inverter, the traditional calculation and approximation method are proven to be effective. However,
when high speed switching is adopted, the losses, which are overlooked in low frequency condition,
may become an indispensable part of the total losses and cause the inaccurate of loss analysis. In this
section, the losses of inverter are systematically analyzed. The switching procedure, including the
miller effect, is discussed in detail. The high frequency loss is thoroughly analyzed, some of which
are not taken into consideration in low frequency applications. Moreover, the loss distribution based
on the new method can offer a more accurate and detailed guide line for the improvement of high
frequency application.
Before the analysis, several assumptions are made in order to simplify the procedure:
1. The influence of some parasitic parameters such as leakage inductance is not considered.
2. The temperature influence on device parameters is not discussed. If the parameter is
temperature dependent, the calibration is only based on the datasheet. The analysis is conducted
considering the inverter operating temperature is 60 °C.
3. The parameters of the symmetry components are same and match the datasheet.
4. The losses of the symmetry components are considered to be the same.

3.1. High Side MOSFET Loss


Basing on operation principles in Section 2, the high side MOSFETs S3, S4 are working at AC
frequency. Comparing with the conduction loss, the switching loss can be ignored for their low
switching frequency. The D-S current of the high side MOSFET S3 ihi_S3 is shown in Figure 3.

Figure 3. The D-S current of the high side MOSFET S3.


Energies 2017, 10, 311 5 of 18

When S3 is turned on, the switching of the low side MOSFET S1 divides ihi_S3 into two parts. When
S1 turns on, ihi_S3 rises, ihi_S3 flows through S1, and the current is in rising period; when S1 turns off, ihi_S3
falls, ihi_S3 flows through D1, and the current is in falling period. The switching of S1 causes the
fluctuation of ihi_S3. Tgrid is the gird period. T(n) is the nth switching period of the low side switch S1
and the duty cycle is d(n), the nth conducting time is d(n)T(n). ihir_S3(n) is the nth rising period of ihi_S3
which is also the turn-on current of S1. ihid_S3(n) is the falling period which is also the free-wheeling
current of D1. Ns is the number of S1 switching period which is contained in one AC period. The
conduction loss of the high side MOSFET S3 Phicon_S3 can be divided into two parts:

1 Ns d (n)T (n ) 2
[ (
Tgrid n =1 0
Phircon_S3 = ihir(n) (t ) RDS_S3dt )] (1)

1 Ns [1-d (n )]T (n ) 2
[ (
Tgrid n =1 0
Phidcon_S3 = ihid(n ) (t ) RDS_S3dt )] (2)

Phicon_S3 = Phircon_S3 + Phidcon_S3 (3)

where Phircon_S3 is the ihi_S3 rising period loss and Phidcon_S3 is the falling period loss, RDS_S3 is the D-S
resistance of S3 which can be obtained from datasheet.

3.2. Low Side MOSFET Loss


The conduction loss of the low side MOSFET S1, Plocon_S1 can be easily deduced from Equation
(1). The conduction current is the same as Phircon_S3 and the only difference is the D-S resistance. RDS_S1
is the D-S resistance of S1. Plocon_S1 can be calculated as:

1 Ns d (n )T (n ) 2
[ (
Tgrid n =1 0
Plocon _ S1 = ihir(n) (t ) RDS_S1dt )] (4)

According to the operation principles, low side MOSFETs S1, S2 are working at 400 kHz. Figure
4a shows the voltage waveforms of S1 during the turn-on transition and the Figure 4b is the simplified
diagram of the transition.

(a) (b)
Figure 4. The waveforms during turn-on transition: (a) the measured waveform during the turn-on
transition; and (b) the simplified diagram of the turn-on transition.

As Figure 4b shows, an approximation is made in order to simplify the analysis. The D-S current
of S1 ion_S1 is considered to be a constant current after ion_S1 is fully turn-on. When a signal starts to turn
on S1, there is a time delay before G-S voltage of S1 vGS_S1 increases to the gate threshold voltage Vth.
Then, the output capacitance of S1, COSS_S1 begins to be charged. The output capacitance loss POSS_S1
can be calculated as:
Energies 2017, 10, 311 6 of 18

VDCBus
POSS_S1 = fSW ×  vDS_S1COSS_S1 (vDS_S1 )dvDS_S1 (5)
0
where fSW is the switching frequency of S1, VDCBus is the input DC bus voltage and vDS_S1 is the D-S
voltage of S1. The output capacitance COSS_S1 is a vDS_S1 related parameter which is provided by the
datasheet.
When vGS_S1 reaches Vth, the ion_S1 starts to rise linearly. After the rising period, ion_S1 turns on
completely, the vGS_S1 reaches the turn-on miller plateau voltage Vmp_on and the voltage vDS_S1 starts to
decrease. The miller plateau is caused by the charging or discharging procedure of the capacitance
between G-D, which is CGD [20]. In actual waveform, as Figure 4a shows, miller plateau have a slope.
The steepness of the slope is depending on the value of CGD and CGS, where CGS is the capacitance
between G-S. Typically, CGD is larger than CGS, the phenomenon appears as a plateau. The duration
time can be considered as the charging time to charge QGD, which is the gate to drain charge.
At the end of the miller plateau, the vGS_S1 reduces to zero and the turn-on procedure is
completed. During the turn-on transition, the turn-on loss Pon can be divided into two parts: Pon1 and
Pon2. The vGS_S1 is constant and iS1 is linearly changed during ton1. Similarly, the iS1 is constant and vGS_S1
is linearly changed within ton2. The turn-on loss of S1 Pon_S1 can be deduced form Equation (6).
1 Ns VDCBus I on_S1(n) 1 Ns VDCBus I on_S1( n ) QGS2 RGon Q R
Pon_S1 =
Tgrid

n =1 2
(ton1 + ton2 ) =
Tgrid

n =1 2
(
Vmp_on + Vth
+ GD Gon )
Vmp_on (6)
2

where Ion_S1(n) is the nth switching period turn-on current of S1. QGS2 represents the corresponding
charge during ton1 which can be calculated according to the transfer characteristic figure of devices,
RGon is the gate loop resistance during turn-on period.
Figure 5a shows the waveforms of S1 during the turn-off transition and the Figure 5b is the
simplified diagram of the transition. A similar approximation is made which considers the D-S turn-
off current of S1 ioff_S1 to be constant before toff2. When the signal starts to turn off S1, vGS_S1 starts to
decrease. The vGS_S1 begins to increases when vGS_S1 reaches the turn-off miller plateau voltage Vmp_off.
At the end of the plateau, vGS_S1 stops increasing and ioff_S1 starts to decrease. The turn-off transition is
completed when vGS_S1 goes down to Vth and ioff_S1 decreases to zero. The turn-off loss Poff_S1 can be
regarded as two parts: Poff1 during toff1 and Poff2 during toff2 which can be calculated by Equation (7).
1 Ns VDCBus I off_S1(n ) 1 Ns VDCBus I off_S1(n ) QGD RGoff Q R
Poff_S1 =
Tgrid

n =1 2
(toff1 + toff2 ) =
Tgrid

n =1 2
(
Vmp_off
+ GS2 Goff )
Vmp_off + Vth (7)
2

where Ioff_S1(n) is the nth switching period turn-off current of S1. RGoff is the gate loop resistance during
turn-off period. The total loss of S1 Ploss_S1 is regarded as:
Ploss_S1 = Plocon_S1 + POSS_S1 + Pon_S1 + Poff_S1
(8)

(a) (b)
Figure 5. The voltage and current waveforms during turn-off transition: (a) the measured waveform
during the turn-off transition; and (b) the simplified diagram of the turn-off transition.
Energies 2017, 10, 311 7 of 18

3.3. Free-Wheeling Diode Loss


The conduction loss of the free-wheeling diode D1, Pdcon_D1 can be deduced from Equation (2),
which is shown in Equation (9):
1 Ns [1-d (n )]T (n )
[ (
Tgrid n =1 0
Pdcon_D1 = ihid (n )U f dt )] (9)

Uf is the forward voltage of the diode. The turn-on loss of the diode Pond_D1 can be represented as
(10):
Ns Ns
1 1 1 1
Pond _ D1 =
Tgrid

n =1 2
U d I don(n)tr ≈
Tgrid
 2U
n =2
I t
DCBus off _ S1(n-1) on1 (10)

where Ud is the voltage on the diode. Idon(n) is the nth diode turn-on current which can be
approximated as the (n − 1)th turn-off current of S1 Ioff_S1(n−1). tr is the rising time of the S1 which can be
approximated as ton1.The turn-on loss of the diode Poffd_D1 can be represented as (11):
Ns Ns
1 1 1 1
Poffd _ D1 =
Tgrid

n =1 2
U d iRM(n)trr =
Tgrid
 2U
n =1
i t
DCBus RM(n) rr (11)

IRM is the diode peak reverse current and trr is the reverse recovery time.

3.4. Inductor Loss


The copper loss PLCu of filter inductor can be calculated as

1 Tgrid
PLCu =
Tgrid  0
iL2 (t ) RL dt (12)

where iL is the inductor current and the RL is the resistance of the inductor winding.
Figure 6 shows the trajectory of inductor current iL on the B-H plane during one switching cycle.
At the end of the switching cycle, the iL is not the same as the initial value because the inverter is
working in continuous current mode in order to follow the sinusoidal reference. The work mode
leads to the unclosed B-H curve as Figure 6 shows. Accordingly, the traditional hysteresis loss
calculation based on closed B-H curve is not suitable for inverter hysteresis loss calculation. The
unclosed B-H curve should be adopted [21–23].

Figure 6. The B-H curve during on switch cycle.

Magnetic flux density B can be obtained by integral of the inductor voltage uL. The magnetic flux
density at tn can be calculated as:

1 tn
N ⋅ A 0
B(tn ) = uL dt (13)
Energies 2017, 10, 311 8 of 18

where N is the number of winding turns and A is the cross-section area of the inductor core. iL(tn) is
the inductor current at tn, the magnetic field intensity H(t1) can be obtained by:

NiL (t1 )
H (tn ) = (14)
l
where l is the length of the equivalent magnetic circuit. The hysteresis loss Physis can be calculated as:
Ns
1

BP BE
Physis = HdB −  HdB (15)
Tgird n =1
BS BP

3.5. Capacitor Loss


The loss which is caused by the leakage current of the capacitor Pcleak can be calculated as:

Pcleak = Uc ⋅ Icleak (16)

Uc is the voltage on the capacitor, and Icleak is the leakage current of the capacitor, which is a Uc
related parameter and can be found in the datasheet.
Rcs is the resistance of the capacitor lead and electrode, Irip is the ripple current of the capacitor,
and the loss on these conductors can be represented as:
2
Pcs = I rip Rcs (17)

RESR is the equivalent series resistance of the capacitor, which can be deduced form dissipation
factor tanδ:

tan δ
RESR = (18)
2π fC
where f is the frequency which the ESR is calculated at. C is the capacitance of the capacitor. The ESR
loss of the capacitor can be calculated as:
2
PESR = I rip RESR (19)

The total losses on the capacitor is

Pcloss = Pcleak + Pcs + PESR (20)

3.6. Loss Calculation Results


Based on the previous methods, the calculation results of the Full SiC power devices inverter
losses are shown in Figure 7 as calculation Example 1.
As we can see from Figure 7, the switching loss takes the major part of the total loss. The output
capacitance loss POSS, which is often overlooked in low frequency loss analysis, is over 1% and should
be taken account in high frequency application. For the special characteristic of the SiC diode, the
reverse recovery time trr is consider to be 0. Hence, the free-wheeling diode turn-off loss Pdoff is 0. This
superiority, which is proven in later experiment, is vital for the total loss of the inverter. Finally, the
calculation efficiency is 97.32% at rated power of 1 kW.
Two comparative calculation examples are set up. In Example 2, the free-wheeling diodes D1, D2
are replaced by two normal Si diodes. In Example 3, all the power devices are replaced by the normal
Si devices. The loss distribution of the comparative calculation examples are shown in Figure 8.
As Figure 8a shows, when the SiC diodes are replace by the normal Si diodes, the total loss on
the diodes is over 50%. The turn-on loss and the turn-off loss of the diodes contribute the most part
of the losses increase. As a result, the calculation efficiency of Example 2 is down to 93.57% at 1 kW.
Energies 2017, 10, 311 9 of 18

Figure 7. Loss distribution of Example 1.

(a) (b)

Figure 8. Loss distributions of the comparative calculation examples: (a) Example 2; and
(b) Example 3.

After all the power devices are replaced by the Si devices. The losses of the switches become the
major part of the total losses. Consequently, as Figure 8 shows, the total loss of Example 3 is almost
three times larger than Example 2. The calculation efficiency of Example 3 is 85.27% at 1 kW.
The total loss comparison is shown in Figure 9. For Example 2, the diode losses contribute the
most. For Example 3, the losses on the switches are numerous. The total losses difference between the
Full SiC and Full Si power device is over five times. These results are confirmed in later comparative
experiments, which indicate that the Si power devices are not suitable for high frequency application.

Figure 9. Loss comparison between calculation examples.


Energies 2017, 10, 311 10 of 18

4. Improved Simulation Method


A simulation model is often built in software environment in order to verify the validity of
theoretical analyses and accelerate the compensator tuning. In low frequency converting, the
simplified component models are considered to be effective and timesaving. However, as the
switching frequency increases, some details of the switching procedure may have a serious influence
on the simulation, which could make the results become inaccurate, even unreliable. The
inconsistency between the simulation results and experiment results emerges during the design
process. The deviation between PWM control signal and switching response in high frequency
switching is consider to be the reason which cause the inconsistency. The influence of the deviation
on the simulation is verified by experiment. Moreover, based on the theoretical analysis and test
results, a compensator method is proposed in order to minimize the deviation which is caused by the
influence. Consequently, the simulation results are significantly improved. The improved simulation
model is used in prototype design to verify the compensators. The method is proven to be effective
by the experiments in later section.

4.1. Influence of High Frequency Switching


A simulation model is built in software environment of PSIM. The parameters of the components
and control compensator are the same as the experimental prototype. The grid-connecting power
experiments are carried out. The 3P3Z compensator in the current loop, which is designed to follow
the current reference, are tuned and tested on the simulation model. As Figure 10a shows, the
compensation effect is desirable. However, during the experiment, the same compensator, which has
the same parameters, causes the current oscillation during zero-crossing procedure.

(a) (b)
Figure 10. Simulation and Experiment results comparison: (a) simulation waveform before
improving; and (b) experiment waveform.

The same simulation method is used in the previous 50 kHz inverter design and no similar issue
arises. Through analysis, the deviation between PWM control signal and switching response in high
frequency switching, is the main reason which causes the simulation to be inaccurate.

4.2. Equivalent Opening Time


Figure 11 shows the waveforms of a complete switching cycle. The PWM signal is considered to
be an ideal square wave. When the rising edge of the PWM signal begins to turn on the switch, there
is a turn-on propagation delay tpg_on before the G-S voltage starts to rise. The delay is caused by the
drive circuits when converting the PWM signal into drive signal. When VGS rises, the D-S voltage VDS
starts to descend. The time, which is from 10% VGS to 90% VDS, is defined as the turn-on delay td_on.
The time, which is form 90% VDS to 10% VDS, is the rise time trise. The turn-off propagation delay tpg_off,
turn-off delay tdoff and fall time tfall can be obtained by similar definitions. The equivalent opening
time is define as the period which the VDS fall below 90% then rise over 90%. As Figure 11 shows, the
Energies 2017, 10, 311 11 of 18

relationship between PWM opening time tPMW and the equivalent opening time tEQ can be represented
as Eqaution (21)
t EQ = t PWM + [t pg_off − t pg_on ] + [t d_off (VDS ) − t d_on (VDS )] + t rise (VDS ) + t fall (VDS ) (21)

The equivalent opening time tEQ can be regarded as the actual respond of the switch under the
control of PWM signal. In practical circuits, tpg_on and tpg_off are small and assumed to be equal. Hence,
Equation (21) can be simplified as:
t EQ = t PWM + t d_off (VDS ) − t d_on (VDS ) + t rise (VDS ) + t fall (VDS ) = t PWM + t e (VDS ) (22)

where te is the total extend time which is caused by the delay in the switching procedure. td_on, td_off, tfall and
trise are all VDS related parameters provided by the datasheet. It is obvious that the PWM opening time is
extended during the switching procedure. The proportions of the deviation in the equivalent opening
time tEQ under different switching frequencies and duty cycles are shown in Table 1.

Figure 11. Waveforms of the switching operation.

Table 1. The proportion of the deviation.

te fsw Duty Cycle tPWM(ns) tEQ(ns) te/tEQ


2% 400 492 18.70%
50 kHz 50% 10,000 10,092 0.91%
80% 16,000 16,092 0.57%
92 ns
2% 50 142 64.79%
400 kHz 50% 1250 1342 6.86%
80% 2000 2092 4.40%

As Table 1 shows, when the switching frequency is low, the proportion of te in tEQ is very small.
During the practical circuit design, this deviation is often ignored. However, in high frequency
implementation, this time deviation may even larger than tPWM. When the fsw is at 400 kHz, at 2% duty
cycle, the proportion of te is over 50%. tPWM is extended about two times. This deviation may lead to
the inconsistency between the output and control signal. This difference has an error accumulation
effect, which can cause the error response of the controller. As a result, the compensator, which is
tested in the simulation and consider to be valid, will fail on the prototype.
In order to verify the analysis, an off-grid DC experiment is set up, for the deviation is more
obvious when the duty cycle is constant. The difference between the output currents can prove the
pervious analysis. The prototype connects to a 100 Ω resistor instead of the gird, then runs at 50 kHz
and 400 kHz respectively. A constant duty cycle is given to the inverter in order to run the inverter
in DC output mode. The output current itest is tested at each duty cycle at different switching
frequency. Meanwhile, the same test is carried out on the simulation model. As Figure 12 shows, the
output current at the same duty cycle of simulation and experiment are represented by two respective
curves. There is almost no difference between the experiment results and simulation results when the
Energies 2017, 10, 311 12 of 18

switching frequency is at 50 kHz as Figure 12a shows. Because the proportion of the deviation in low
frequency is very small, which can be ignored in traditional analysis. However, when the switching
frequency is at 400 kHz as Figure 12b shows, there are significant differences between the simulation
results and the experiment results. When the test duty cycle is under 45%, the experiment output
current is apparently larger than the simulation results at the same duty cycle. This phenomenon can
be explained as the control PWM signal in the prototype is extended by the delays which we talked
above. The phenomenon is more obvious at low duty cycle which is consistent with previous
analysis.

(a) (b)
Figure 12. The output current responds between simulation and experiment at different frequencies:
(a) 50 kHz; and (b) 400 kHz.

4.3. Compensating Method


Different from other researches, the proposed method focuses on the impact of the switching
procedure on the output power. Instead of simulating the complex switching procedure in detail, a
compensating module is used to improve the simulation results. The proposed method is simple and
effective. Based on Equation (22), dEQ is the duty cycle based on tEQ and can be calculated as:

d ⋅ tsw + td_off (VDS ) − td_on (VDS ) + trise (VDS ) + tfall (VDS )


d EQ = (23)
tsw
where tsw is the switching period, and dPWM is the duty cycle of the input PWM. The compensator is
added between the Linearization module and PWM generating module (Figure 13).

Figure 13. Location of the compensator.

The linearization module [24–26] is used to generate the duty cycle dPWM for controlling the
switches. The duty cycle dPWM is compensated by the duty cycle compensator. In order to test the
compensation effect, the 400 kHz off-grid DC experiment is carried out on the improved simulation
model. The simulation results are shown in Figure 14. Apparently, the compensator module is able
to simulate the prototype output current correctly. The deviation of the output current between the
simulation and experiment is minimized successfully.
Because of the deviation, the characteristic of compensator at low duty cycle have to be adjusted.
Based on the improved simulation model, the characteristic of the inverter is re-analyzed. The
Energies 2017, 10, 311 13 of 18

compensator is redesign accordingly. The oscillation during zero-crossing is restrained by the new
compensator in the simulation. The compensation effect is proven by the further experiment. The
output waveforms of the experiments are shown in the later section.

Figure 14. The current respond between improved simulation and experiment.

5. Experiment Results
A 1-kW prototype is built in the laboratory (Figure 15). The parameters of the components are
shown in Table 2. The control platform is TMS320F28377D from Texas Instruments. It is a high
performance dual-core MCU running at 200 MHz.

Figure 15. Experimental prototype.

Table 2. Parameters of the proposed system.

Component Manufacture Model Value


S1, S2, S3, S4 Wolfspeed C2M0280120D
D 1, D 2 Wolfspeed CVFD20065A
Li1, Li2 Magnetics 77439A7 800 μH
Lg1, Lg2 Magnetics 77548A7 215 μH
Cf WIMA MKP10 0.15 μF

5.1. Grid-Connected Experiment


Figure 16a shows the measured waveforms at 100 W and Figure 16b is the corresponding simulation
waveforms. The output current ig can track the grid voltage very well when the power output is low. The
power factor is 0.99 and THD is 4.8%. The bus voltage is stabilized at 400 V and the ripple is within ±4 V.
Energies 2017, 10, 311 14 of 18

The zero-crossing oscillation which happens in pervious compensator design is efficiently restrained. The
simulation waveforms in Figure 16b match the experiment results well.

(a) (b)
Figure 16. Experimental waveforms of the inverter at low power: (a) experiment waveform; and
(b) simulation waveform.

Figure 17a shows the waveform at 1 kW and Figure 17b is the corresponding simulation
waveforms. The RMS value of ig is 4.5 A. Along with the increase of the output power, the waveform
of the ig rises significantly. The power factor is 0.99 and THD is down to 1.8%. The efficiency of the
inverter is 96.1% at this moment.

(a) (b)
Figure 17. Experimental waveforms of the inverter at rated power: (a) experiment waveform; and
(b) simulation waveform.

Figure 18a shows the waveforms of the switch voltage and grid current at rated power of 1 kW.
Figure 18b is the partial enlarged waveform of Figure 18a. ig is the grid current. vDS is the drain-to-
source voltage of the switch S1. vGS is the drive signal of S1. As the waveform shows, when ig is above
zero, S1 is switched at high frequency of 400 kHz. The voltage stress of S1 is 400 V; when ig is below
zero, S1 is closed.
The relationships between efficiency, THD versus the output power are shown in Figure 19a,b,
respectively. The THD decreases from 4.8% to 1.8% when the output power grows from 100 W to
1000 W, while the efficiency increases from 85.2% to 96.1%. Finally, the efficiency reaches the
maximum efficiency of 96.1% at rated power. Thus, in small renewable energy application, the
proposed inverter achieves an excellent performance, including relatively high conversion efficiency,
high power factor and low THD.
Energies 2017, 10, 311 15 of 18

(a) (b)
Figure 18. Experimental waveforms: (a) Waveform of the switch voltage and grid current at rated
power; and (b) partial enlarged waveform of the switch voltage and grid current.

(a) (b)
Figure 19. Efficiency and grid current THD curves: (a) efficiency under different power level; and (b)
THD under different power level.

5.2. Comparison Experiments of Power Loss


The comparative experiments are set up in order to verify the loss analyses in Section 3. The
power devices of Prototype 1 are all SiC power devices. The free-wheeling diodes D1 and D2 are
replaced by normal Si diodes on Prototype 2. All the power devices are replaced by normal Si devices
on Prototype 3. The power devices used in each Prototype are shown in Table 3.

Table 3. Power Devices of the Prototype.

Prototype D 1, D 2 S1–S4
1 CVFD20065A C2M0280120D
2 BYV29-600 C2M0280120D
3 BYV29-600 IPW60R040C7

The efficiency curves of the comparison experiments are shown in Figure 20. Prototype 1, which
uses power devices that are full SiC components, reaches the rated power at 1 kW. When the
temperature of the components is stable, the efficiency of Prototype 1 is 96.1%. Prototype 2, in which
the diodes are replaced with Si diodes, reaches the rated power of 1 kW. However, the Si diodes break
down within one minute. The efficiency of Prototype 2 at 1 kW is 91.83%. The voltage vdiode and
current idiode waveforms of the free-wheeling diode D1 at 150 W in Prototype 1 and 2 are compared in
Figure 21. Prototype 3 has the highest efficiency when the output power is low because the Si power
devices used in the experiment have a lower conduction loss than the SiC. When the output power
rises, Prototype 3 reaches the highest efficiency of 88.9% at 500 W. Then, the efficiency of Prototype
3 starts to decrease and the Si switches break down at 600 W. The efficiency of Prototype 3 at 1 kW
cannot be measured. The experiment proves that the Si power devices are not suitable for high
switching frequency application.
Energies 2017, 10, 311 16 of 18

Figure 20. Efficiency comparison.

(a) (b)
Figure 21. Voltage and current waveforms of the free-wheeling diode D1: (a) switching transition of
SiC diode; and (b) switching transition of Si diode.

As Figure 21b shows, during the turn-on and turn-off procedure, the voltage and current of the
Si diode in Prototype 2 have a large overlap area and big reverse recovery current, which means the
switching losses of the diodes are very large. Comparing with the Si diode (Figure 21a), the SiC diode
has a faster switching speed, which contributes to a low switching loss. Remarkably, the reverse
recovery current of the SiC diode is not zero in the measured high frequency waveforms, but the
reverse recovery loss is significantly smaller than Si diode due to the extremely short reverse recovery
time.
The comparisons of experiment and calculation efficiencies are shown in Table 4. For prototype
1, the calculation efficiency at 1 kW is 97.32% and the corresponding experiment efficiency is 96.1%.
The deviation between experiment and calculation is 1.02% which may be caused by the unmeasured
losses such as the losses on the relay, fuse and so on. The calculation efficiency of Prototype 2 is
93.57% and the experiment efficiency at 1 kW is 91.83%. The deviation of Prototype 2 is 1.74%.
Because the efficiency experiment of Prototype 2 does not reach a temperature stable state before the
Si diodes breaks down, the unstable state of the main circuit may cause extra loss in Prototype 2.
Prototype 3 cannot reach the rated power and breaks down at 600 W during the experiment; its
efficiency is 88.9% at 500 W. Finally, the deviation between experiment and calculation efficiency is
within acceptable range, which proves that the proposed loss calculation methodology is valid.
Energies 2017, 10, 311 17 of 18

Table 4. Experiment and calculation efficiency.

Calculation Experiment
Prototype Deviation
Efficiency (1 kW) Efficiency (1 kW)
1 97.32% 96.1% 1.22%
2 93.57% 91.83% 1.74%
3 85.27% 88.9% (at 500 W) Unknown

6. Conclusions
A 400 kHz dual-buck full-bridge inverter is proposed for small power renewable energy gird-
connected generation. A current voltage dual-loop control strategy is employed, including a 3P3Z
compensator in the inner current loop and a 2P2Z compensator in the outer voltage loop.
Consequently, the inverter can deliver grid-tie power and regulate the DC bus voltage
simultaneously. A systematic method for calculating the losses of high frequency inverter is
presented. The influences of high frequency switching on loss analysis are discussed in detail. The
loss distribution of the proposed inverter is obtained through the presented method. The simulation
error, which is cause by the deviation between PWM control signal and switching response, is
thoroughly analyzed. An improved simulation method is proposed in order to minimize the
deviation which is caused by the delays of the switch in high frequency switching procedure. The
loss analysis and simulation method are both validated by corresponding experiments. Finally, the
power experiment of the inverter is finished at rated power of 1 kW, with the power factor above 0.99
and THD of 1.8%. The adoption of SiC power devices contributes to the highest efficiency of 96.1%
at rated power. The experiment results prove that the proposed loss calculation method and
improved simulation method is effective and suitable for high frequency inverter.

Acknowledgments: This research was supported by the National Natural Science Foundation of China (Grant:
2015AA050603) and supported by Tianjin Municipal Science and Technology Commission (Grant:
14ZCZDGX00035). The authors would also like to thank the anonymous reviewers for their valuable comments
and suggestions to improve the quality of the paper.

Author Contributions: Zhun Meng and Yi-Feng Wang designed the main parts of the study. Liang Yang and
Wei Li helped in the fabrication.

Conflicts of Interest: The authors declare no conflict of interest.

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