CCJ2010Q2 - GT Starting Reliability
CCJ2010Q2 - GT Starting Reliability
CCJ2010Q2 - GT Starting Reliability
S
ome power producers want
to believe that gas-turbine-
based generating facilities
don’t require a rigorous
engineering effort at the design/
specification stage of a project.
Given that the track record of gas
turbines for land-based generation
service industry-wide is excellent,
and that GTs are “standard” facto-
ry-assembled machines, it’s no won-
der that executives who majored in
business and finance think buying
a gas turbine is not much different
than buying a new corporate limo:
Sign the papers, pay, and you’re
ready to go.
But the “standard” engine often
doesn’t quite match actual site and
operating conditions and, conse-
quently, the new plant may not meet
the owner’s expectations regarding 1. Libyan combined-cycle plant has three 2 × 1 power blocks. First four Als-
starting reliability, availability, effi- tom 13E2 gas turbines were installed in 2001, the third block five years later
ciency, etc—critical factors in the
competitive generation business. It’s
rare that a modest investment in 100
engineering and hardware improve-
ments can’t correct the situation. The Rotor speed (100% = 3333 rpm)
90
experience of the General Electricity
Co of Libya (Gecol) that follows is a 80
case in point. Control valve
The utility’s GT fleet includes stroke, torch 2
70
23 Alstom machines—including
these models: 13D, 13E1, 13E1M,
Percent of value
60
13E2MXL, and 8C. One of its
combined-cycle plants, a facility Control valve
50 stroke, torch 1
with three 2 × 1 power blocks and
equipped with distillate-fueled 13E2 TAT (turbine
engines, faced recurring problems 40 exit temperature)
during wintertime starts. It turned Temp of torch 1 tip
to Creative Power Solutions (CPS) 30
for a root-cause analysis and per-
manent solution (Fig 1). Note that 20 Temp of torch 2 tip
Libya, like most Middle Eastern Flame (1 = off; 10 = on)
nations, does not release the names 10
and locations of important indus- TSOV (10 = closed; 0 = open)
trial facilities. 0
0 50 100 150 200 250 300 350 400
For readers unfamiliar with the Time, sec
13E2, it is a robust frame engine with
a 21-stage compressor, five-stage tur- 2. Successful startup, mapped here, often was elusive because of ignition issues
92 COMBINED CYCLE JOURNAL, Second Quarter 2010
ENGINEERED SOLUTIONS
bine, and a 72-burner annular com- neously: distillate and water for NOx
CPS engineers began the proj- Small droplets, shipments for viscosity and flash
ect by examining data provided by rapid vaporization point. Fig 4 shows that high-flash-
Gecol for both successful and failed Large droplets, point fuels also have high viscosities
slow vaporization
starts. Based on this work, hypoth- and, therefore, are more difficult to
eses were put forward and an action atomize than low-flash-point/low-vis-
plan developed to test the hypoth- Kinematic viscosity cosity oils. Variability in flash-point
eses and identify possible solutions. 4. Small droplets of fuel produced by temperatures across the samples was
Next, the preferred solution would good atomization vaporize quickly 36 deg F, confirming in the minds of
be implemented on one engine and, investigators that high viscosity was
after validation, would be installed the underlying reason for at least
on all six 13E2s. detail by analyzing the following: some failed starts.
How the engine is supposed n Fuel properties. To sum up, the CPS investigators
to start (follow curves in Fig 2). n Operating conditions. concluded that the primary reason
First steps in a successful start: The n Ignition torch tests. for low starting reliability was poor
ignition sequencer lights the igni- Here’s what engineers learned: ignition caused by weak gas pilot
tion torch and later presets the oil 1. Low-quality atomization of liq- flames and poor atomization. The
control valves to the system filling uid fuel during engine startup. ideal oil for startup, they agreed,
stroke. When the flame is stable, as 2. Wide variability—36 deg F—in would be one with a low viscosity
indicated by an increase in torch tip the flash point temperature of the to achieve fine droplet sizes during
temperature, the trip shut-off valve light fuel oil burned. atomization and a low flash point to
(TSOV) opens and oil fills the system 3. Ignition torches produced a facilitate ignition. Also that the pilot
up to the sector (pilot) valves. weak flame at the established operat- flame must be strongly “attached”
After a timed delay to fill the ing parameters. to its lance and be sufficiently hot to
system, control valves go to ignition 4. Rapid depletion of bottled pilot vaporize and ignite all possible oils
stroke, the burners ignite, and moni- gas caused a weak torch flame dur- delivered to the plant.
tors detect the main flame. Then the ing startup. (Perhaps the gas bottles Another benefit of prompt igni-
torch is shut off and its tip tempera- were too small or were not being tion and complete combustion dur-
ture drops. refilled fully.) ing startup is the elimination of oil
That’s the plan. But analysis of residue in the combustion chamber
startup data revealed the following The details from failed starts. When that residue
scenarios which caused or contrib- ignites during a successful start the
uted to the failed starts: Fuel nozzles for the Gecol GTs are additional heat may trip the unit on
n Ignition pilot flame either did not designed to inject two fluids simulta- “high TAT.”
ignite or failed after ignition.
n Combustor ignited and the tur-
bine exhaust temperature (TAT)
rose to the alarm limit, accelera- Atomizing
tion dropped below its limit, and air system
the engine tripped. Orifice
n Combustor ignited and operation or valve Ignition torch
was normal—that is, until the
TSOV closed (data offered no clues Pressure gage
as to why this happened) and the
engine tripped on “no fuel.”
n Combustor ignited and opera-
tion was normal—that is, until Flowmeter
the flame monitors no longer saw
the flame (weak signal) and the Fuel gas
bottle
engine tripped on “flame-out.”
Several hypotheses proposed
for the various startup failures
observed were investigated in 5. Test apparatus installed by CPS engineers was simple, effective
COMBINED CYCLE JOURNAL, Second Quarter 2010 93
ENGINEERED SOLUTIONS
Orifice size, mm
Blow-off
Fuel flow
5 Orifice
Air flow
size, mm
Flow too high
4 3
Optimal window Optimal window
3 Inoperable
sector valve 2
2 Flow too low
1 1
Air pressure Fuel pressure
7, 8. Dashed ellipse shows the optimal window for air flow (left), fuel flow (right)
2
Preferred region
of operation (CPS
recommended)
1 Unit 1 modification
by plant operators
OEM design
0
0 0.2 0.4 0.6 0.8 1
Normalized flame temperature
9. Ignition flame produced using the OEM’s gas and air
orifice settings is much too weak to achieve a high start- 10. Operating in the preferred region (upper right)
ing reliability on oil assures high starting reliability
94 COMBINED CYCLE JOURNAL, Second Quarter 2010
plant because the fuel did not meet
the manufacturer’s spec and there
was insufficient gas to create a strong
flame.
Use of orifice sizes specified by
CPS created the flame shown in Fig
11. Use of these orifices on all six
engines restored starting reliability
to fleet-wide numbers. All engines
started on the first attempt. ccj
susie@carahaliosmedia.com
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